Crash of a Cessna 421C Golden Eagle III in Las Cruces: 4 killed

Date & Time: Aug 27, 2014 at 1903 LT
Registration:
N51RX
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Las Cruces – Phoenix
MSN:
421C-0871
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
2432
Captain / Total hours on type:
52.00
Aircraft flight hours:
8181
Circumstances:
According to the line service technician who worked for the fixed-base operator (FBO), before taking off for the air ambulance flight with two medical crewmembers and one patient onboard, the pilot verbally asked him to add 40 gallons of fuel to the airplane, but the pilot did not specify the type of fuel. The line service technician drove a fuel truck to the front of the airplane and added 20 gallons of fuel to each of the multiengine airplane's wing tanks. The pilot was present during the refueling and helped the line service technician replace both fuel caps. Shortly after takeoff, a medical crewmember called the company medical dispatcher and reported that they were returning to the airport because smoke was coming from the right engine. Two witnesses reported seeing smoke from the airplane Several other witnesses reported seeing or hearing the impact and then immediately seeing smoke or flames. On-scene evidence showed the airplane was generally eastbound and upright when it impacted terrain. A postimpact fire immediately ensued and consumed most of the airplane. Investigators who arrived at the scene the day following the accident reported clearly detecting the smell of jet fuel. The airplane, which was equipped with two reciprocating engines, should have been serviced with aviation gasoline, and this was noted on labels near the fuel filler ports, which stated "AVGAS ONLY." However, a postaccident review of refueling records, statements from the line service technician, and the on-scene smell of jet fuel are consistent with the airplane having been misfueled with Jet A fuel instead of the required 100LL aviation gasoline, which can result in detonation in the engine and the subsequent loss of engine power. Postaccident examination of the engines revealed internal damage and evidence of detonation. It was the joint responsibility of the line technician and pilot to ensure that the airplane was filled with aviation fuel instead of jet fuel and their failure to do so led to the detonation in the engine and the subsequent loss of power during initial climb.In accordance with voluntary industry standards, the FBO's jet fuel truck should have been equipped with an oversized fuel nozzle; instead, it was equipped with a smaller diameter nozzle, which allowed the nozzle to be inserted into the smaller fuel filler ports on airplanes that used aviation gasoline. The FBO's use of a small nozzle allowed it to be inserted in the accident airplane's filler port and for jet fuel to be inadvertently added to the airplane.
Probable cause:
The misfueling of the airplane with jet fuel instead of the required aviation fuel, and the resultant detonation and a total loss of engine power during initial climb. Contributing to the accident were the line service technician's inadvertent misfueling of the airplane, the pilot's inadequate supervision of the fuel servicing, and the fixed-base operator's use of a small fuel nozzle on its jet fuel truck.
Final Report:

Crash of a Piper PA-31-325 Navajo in Grand Manan Island: 2 killed

Date & Time: Aug 16, 2014 at 0512 LT
Type of aircraft:
Operator:
Registration:
C-GKWE
Flight Type:
Survivors:
Yes
Schedule:
Saint John - Grand Manan Island
MSN:
31-7812037
YOM:
1978
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
17400
Copilot / Total flying hours:
304
Copilot / Total hours on type:
67
Circumstances:
The Atlantic Charters Piper PA-31aircraft had carried out a MEDEVAC flight from Grand Manan, New Brunswick, to Saint John, New Brunswick. At 0436 Atlantic Daylight Time, the aircraft departed Saint John for the return flight to Grand Manan with 2 pilots and 2 passengers. Following an attempt to land on Runway 24 at Grand Manan Airport, the captain carried out a go-around. During the second approach, with the landing gear extended, the aircraft contacted a road perpendicular to the runway, approximately 1500 feet before the threshold. The aircraft continued straight through 100 feet of brush before briefly becoming airborne. At about 0512, the aircraft struck the ground left of the runway centreline, approximately 1000 feet before the threshold. The captain and 1 passenger sustained fatal injuries. The other pilot and the second passenger sustained serious injuries. The aircraft was destroyed; an emergency locator transmitter signal was received. The accident occurred during the hours of darkness.
Probable cause:
Findings as to causes and contributing factors:
1. The captain commenced the flight with only a single headset on board, thereby preventing a shared situational awareness among the crew.
2. It is likely that the weather at the time of both approaches was such that the captain could not see the required visual references to ensure a safe landing.
3. The first officer was focused on locating the runway and was unaware of the captain’s actions during the descent.
4. For undetermined reasons, the captain initiated a steep descent 0.56 nautical mile from the threshold, which went uncorrected until a point from which it was too late to recover.
5. The aircraft contacted a road 0.25 nautical mile short of the runway and struck terrain.
6. The paramedic was not wearing a seatbelt and was not restrained during the impact sequence.
Findings as to risk:
1. If cockpit data recordings are not available to an investigation, then the identification and communication of safety deficiencies to advance transportation safety may be precluded.
2. If crew members are unable to communicate effectively, then they are less likely to anticipate and coordinate their actions, which could jeopardize the safety of flight.
3. If crew resource management training is not provided, used and continuously fostered, then there is a risk that pilots will be unprepared to avoid or mitigate crew errors encountered during flight.
4. If an actual weight and balance cannot be determined, then the aircraft may be operating outside of its approved limits, which could affect the aircraft’s performance characteristics.
5. If pre-computed weight and balance forms do not include standard items, then it increases the likelihood of omissions in weight and balance calculations, which increases the risk of inadvertently overloading or incorrectly loading the aircraft.
6. If organizations carry out a maintenance task that they consider to be elementary work and the task is not approved as an elementary work task, then there is a risk that the aircraft will not conform to its type design, which could jeopardize the safety of flight.
7. If individuals are performing maintenance tasks for which they have not received approved training, then there is a risk that the task will not be performed in accordance with the manufacturer’s instructions.
8. If components are not installed in accordance with the manufacturer’s instructions, then occupants are at a greater risk of injury or death during an incident or accident if these components are not properly secured.
9. If organizations do not record when maintenance is carried out, then the proper completion of tasks cannot be confirmed, and there is a risk that the aircraft will not conform to its type design, which could jeopardize the safety of flight.
10. If an aircraft is modified without regulatory approval and without supporting documentation, then the aircraft is not in compliance with all applicable standards of airworthiness, which could jeopardize the safety of flight.
11. If an operator undertakes unapproved changes to a supplemental type certificate, then there is a risk that the aircraft will not be airworthy, which could jeopardize the safety of flight.
12. If organizations do not use modern safety management practices, then there is an increased risk that hazards will not be identified and risks mitigated.
13. If Transport Canada does not adopt a balanced approach that combines thorough inspections for compliance with audits of safety management processes, unsafe operating practices may not be identified, thereby increasing the risk of accidents.
14. If organizations contract aviation companies to provide a service with which the organizations are not familiar, then there is an increased risk that safety deficiencies will go unnoticed, which could jeopardize the safety of the organizations’ employees.
15. If passengers are not provided with a regular safety briefing, then there is an increased risk that they will not use the available safety equipment or be able to perform necessary emergency functions in a timely manner to avoid injury or death.
16. If passengers are not properly restrained, then there is an increased risk of injuries and death to those passengers and the other occupants in the event of an accident.
17. If carry-on baggage, equipment or cargo is not restrained, then occupants are at a greater risk of injury or death if these items become projectiles in a crash.
18. If carry-on baggage, equipment or cargo is not restrained, then there is an increased risk that the occupants’ access to normal and emergency exits, and to safety equipment, will be completely or partially blocked.
19. If pilots continue an approach below published minimum descent altitudes without seeing the required visual references, then there is a risk of collision with terrain and/or obstacles.
20. If current charts and databases are not used, then navigational accuracy and obstacle avoidance cannot be assured.
21. If GPS (global positioning system) approaches are conducted without the approved Operations Specification, then there is a risk that the pilot’s training and knowledge will be inadequate to safely conduct the approach.
22. If medical symptoms/conditions are not reported to Transport Canada, then it negates some of the safety benefit of examinations and increases the risk that pilots will continue to fly with a medical condition that poses a risk to safety.
Other findings:
1. The pilot who installed the air ambulance system did not have approved training, nor was the pilot approved to carry out elementary work.
2. Atlantic Charters was not approved to install the air ambulance system as an elementary work task.
3. Atlantic Charters’ pre-computed weight and balance form did not include a line item to indicate nacelle fuel.
4. The semi-annual safety training offered to paramedics in lieu of safety briefings prior to flights did not meet regulatory requirements.
Final Report:

Crash of a Beechcraft C90 King Air in Villavicencio: 5 killed

Date & Time: Mar 12, 2014 at 0633 LT
Type of aircraft:
Operator:
Registration:
HK-4921
Flight Type:
Survivors:
No
Schedule:
Bogotá – Araracuara
MSN:
LJ-721
YOM:
1977
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
3013
Captain / Total hours on type:
538.00
Copilot / Total flying hours:
1341
Copilot / Total hours on type:
483
Aircraft flight hours:
9656
Circumstances:
The twin engine aircraft departed Bogotá-El Dorado Airport at 0600LT on an ambulance flight to Araracuara, State of Caquetá, carrying two doctors, one patient and two pilots. Fifteen minutes into the flight, the crew contacted ATC, reported problems and was cleared to divert to Villavicencio. On approach to Villavicencio-La Vanguardia Airport, the aircraft stalled and crashed in a wooded area parallel to a road, bursting into flames. The aircraft was destroyed by a post crash fire and all five occupants were killed.
Probable cause:
The following factors were identified:
- The lack of technical knowledge published in the POH for the execution of the pertinent actions during the failure of the engine in flight, together with the unwise decisions made by the crew in that situation.
- The haste of the crew members to land caused them to act in an uncoordinated manner and without the assertiveness required for the execution of the procedures contemplated by the manufacturer, the navigation charts and the published approach procedures.
- The omissions, reactions and deviations inappropriate to conduct the flight safely to the runway.
- The turning to the runway on the same side of the inoperative (critical) engine and maximum power on the operational engine during the unstabilized approach to the runway threshold which led to loss of control of the aircraft in low altitude flight.
Final Report:

Crash of an Antonov AN-26 in Grombalia: 11 killed

Date & Time: Feb 21, 2014 at 0130 LT
Type of aircraft:
Operator:
Registration:
5A-DOW
Flight Type:
Survivors:
No
Schedule:
Mitiga - Tunis
MSN:
118 09
YOM:
1981
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
11
Circumstances:
The aircraft was on approach to Tunis-Carthage Airport by night when it crashed in flames in an open field located near Grombalia, some 35 km southeast of Tunis. All 11 occupants were killed and the aircraft was destroyed by a post crash fire. The aircraft was completing an ambulance flight from Mitiga, carrying six crew members, three doctors and two patients.

Crash of a Britten-Norman BN-2A-27 Islander in Petreasa: 2 killed

Date & Time: Jan 20, 2014 at 1547 LT
Type of aircraft:
Operator:
Registration:
YR-BNP
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Bucharest - Oradea
MSN:
822
YOM:
1977
Flight number:
111
Location:
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
15261
Captain / Total hours on type:
42.00
Copilot / Total flying hours:
886
Copilot / Total hours on type:
21
Aircraft flight hours:
3335
Circumstances:
The twin engine aircraft departed Bucharest-Baneasa Airport on an ambulance flight to Oradea, carrying a medical team, one patient and two pilots. Doctors should go to Oradea to obtain transplant organs from a patient who just passed away. While cruising at an altitude of 6,300 feet vertical to the Apuseni Mountain Range, the crew encountered marginal weather conditions with icing conditions but continued when both engines lost power and failed. The crew attempted an emergency landing when the aircraft collided with trees and crashed in a snowy and wooded hillside at an altitude of 1,400 metres. A pilot and a passenger were killed while five other occupants were injured. The aircraft was destroyed.
Probable cause:
Double engine failure in flight due to carburetor icing. The following contributing factors were identified:
- Erroneous assessment of the risk factors specific to the conduct of this flight,
- Lack of crew experience on this type of aircraft,
- Erroneous decision of the captain to continue the flight in meteorological conditions that caused the carburetor icing,
- Erroneous decision of the captain to continue to fly for a long period of time in icing conditions,
- Erroneous decision of the captain to continue the mission under the AMA, under conditions of BMI flight according to IFR flight rules,
- Erroneous decision of the crew to initiate the flight while the total weight of the aircraft was above MTOW and the CofG was outside the prescribed limits.
Final Report:

Crash of a Britten Norman BN-2A-3 Islander in Aldeia Pikany: 5 killed

Date & Time: Dec 4, 2013 at 1130 LT
Type of aircraft:
Operator:
Registration:
PT-WMY
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Aldeia Pikany – Novo Progresso
MSN:
314
YOM:
1974
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
530
Captain / Total hours on type:
58.00
Circumstances:
Shortly after takeoff from The Pikany Indian Reserve Airfield, while in initial climb, the twin engine aircraft lost height, collided with trees and crashed in a wooded area located on km from the airstrip. The aircraft was destroyed and all five occupants were killed, among them Indian Kayapo who were flying to Novo Progresso to have urgent care.
Probable cause:
The following factors were identified:
- The utilization of an aircraft not included in the Operating Specifications and of a runway neither registered nor approved, with a pilot who did not have the amount of hours necessary nor specific training, disclose a culture based on informal practices, which led to operation below the minimum safety requirements.
- It is possible that the pilot forgot to verify the quantity of fuel in the tanks of the aircraft before takeoff.
- The lack of specific training for the pilot and for the coordinator who, possibly, assumed the function of instructor may have compromised their operational performance during the preparation and conduction of the flight, since they were not effectively prepared for the activity.
- It is possible that the pilot failed to comply with the prescriptions of the legislation relatively to the minimum amount of fuel required for the flight leg. The operation of the aircraft by a pilot with expired qualifications and without the required training goes against the prescriptions at the time, but it was not determined whether this pilot (coordinator) was in the aircraft controls at the moment of the accident. The transport of a cylinder onboard the aircraft also configures flight indiscipline, since it goes against the legislation which prohibits the transport of such material.
- The lack of training of the differences may have contributed to the forgetting to verify the fuel tanks, a procedure that is prescribed in the aircraft manual. Likewise, lack of training may have deprived the pilots from acquiring proficiency for the operation of the aircraft in a single engine condition.
- The fact of conducting a flight to provide assistance in an emergency situation may have contributed to the pilot having forgotten to check safety parameters, such as the amount of fuel necessary.
- The pilot’s intention to earn his operational promotion may have stimulated him excessively, to the point of disregarding the minimum safety requirements for the operation. In addition, the emergency nature of the flight request possibly added to the motivation of the pilot and the coordinator.
- It is possible that, due to having little total experience either both of flight and in the aircraft, the pilot lost control of the aircraft when faced with the situation of in-flight engine failure after the takeoff.
- It is possible that the pilot and the coordinator prioritized the emergency requirement of the situation, failing to evaluate other aspects relevant for the safety of the flight, such as planning, for example.
- The lack of control on the part of the company’s management in relation to the flights operating outside of the main base allowed the pilot and the base manager to conduct a flight without the operating sector authorization. The lack of supervision of the air transport service provision by the contracting organizations allowed the company to provide services without the minimum conditions required by the legislation. Such conditions exposed the passengers to the risks of an irregular operation.
Final Report:

Crash of a Lockheed C-130J-30 Super Hercules at Shank AFB

Date & Time: May 19, 2013 at 1420 LT
Type of aircraft:
Operator:
Registration:
04-3144
Flight Type:
Survivors:
Yes
Schedule:
Kandahar – Shank AFB
MSN:
5560
YOM:
2004
Location:
Country:
Region:
Crew on board:
11
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total hours on type:
904.00
Copilot / Total hours on type:
252
Circumstances:
On 19 May 2013, at approximately 0950 Zulu (1420 local), a C-130J, tail number (T/N) 04-3144, assigned to the 41st Airlift Squadron, 19th Airlift Wing, Little Rock Air Force Base (AFB), Arkansas, ran off the end of a runway at Forward Operating Base (FOB) Shank, Northeast, Afghanistan, struck a ditch which collapsed the nose gear and eventually ripped the right main landing gear from the fuselage. The right outboard engine struck the ground, pressurized fuel and oil lines were broken, fluid was sprayed over the cracked engine casing, and the right wing caught fire. The mishap aircraft (MA) came to a full stop at approximately 544 feet (ft) off the end of the paved runway surface. The mishap crew (MC), Aeromedical Evacuation (AE) crew and two ambulatory patients safely evacuated the aircraft through the top flight-deck emergency escape hatch meeting 600 ft off the nose of the aircraft. There were no fatalities, significant injuries or damage to civilian property. The total estimated loss is $73,990,265. The MA was on an AE mission and included five active duty C-130J crewmembers from the 772nd Expeditionary Airlift Squadron (19th Airlift Wing deployed), Kandahar Air Base (AB), Afghanistan. Additionally, the MA had aboard six reserve AE crewmembers from the 651st Expeditionary Aeromedical Evacuation Squadron (349th Air Mobility Wing and 433rd Airlift Wing deployed), Kandahar AB, Afghanistan. The mishap sortie happened on the third of five planned legs that day to an airfield that was at 6,809 ft Mean Sea Level (MSL) and experiencing winds varying from 200 to 250 degrees gusting from 6 to 28 knots. On the second attempted landing, the MA touched down approximately 1,500 ft down the runway but was 27 knots indicated airspeed (KIAS) faster than computed touchdown landing speed leading to the aircraft going off the end of the runway at approximately 49 KIAS.
Probable cause:
On the second landing attempt at a high altitude airfield (6,809 ft MSL), poor CRM coupled with a late power reduction by MP1 caused the MA to touchdown 27 KIAS faster than computed touchdown landing speed leading to the aircraft going off the end of the runway at approximately 49 KIAS. Because of unique aircraft performance characteristics when operating into and out of high altitude airfields, there was no way that the MA could perform a 50% flap landing (in accordance with T.O. 1C-130(C)J-1-1 landing assumptions, nose wheel landing gear speed restrictions and power level transition speed restrictions) at FOB Shank and land 27 KIAS fast. The MA’s actual landing speed simply overtasked the aircrafts capability to stop within the runway available.
Several factors substantially contributed to this mishap, including:
- Channelized attention,
- Risk assessment during operation,
- Delayed necessary action,
- Response set,
- Procedural error.
Final Report:

Crash of a Cessna 402C II in Mayaguana: 3 killed

Date & Time: Apr 4, 2013 at 0100 LT
Type of aircraft:
Operator:
Registration:
C6-BGJ
Flight Type:
Survivors:
Yes
Schedule:
Nassau - Mayaguana
MSN:
402C-0106
YOM:
1979
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
On Thursday April 4, 2013 at approximately1:00AM DST (0500 UTC) a fixed wing, twin-engine, Cessna 402C aircraft Bahamas registration C6-BGJ, serial number 402C0106, crashed into obstacles (vehicles) while landing on Runway 06 at Mayaguana International Airport (MYMM), Abraham’s Bay, Mayaguana, Bahamas. The pilot in command stated that on April 3, 2013, he received a call at approximately 9:30PM from the Princess Margaret Hospital requesting emergency air ambulance services out of Mayaguana. The local police on the island was contacted to confirm lighting approval and availability in order to conduct the emergency flight. After confirming lighting arrangements with Nassau Air Traffic Control Services, and obtaining the necessary clearance, the pilot in command, along with a copilot and one passenger, (a nurse), proceeded with the flight to Mayaguana. The flight departed Lynden Pindling International Airport at approximately 1:30PM DST (0330UTC). The destination was Abraham’s Bay, Mayaguana, Bahamas. The pilot in command also reported “about 1 hour and 40 minutes later we arrived at Mayaguana Airport, leveled off at 1500 feet and about 4 miles left base Runway 06, we had the runway in sight via lighting from vehicles.” The crew continued with the landing procedures. The aircraft touch down approximately 300 feet from the threshold on runway 06, the pilot in command reported that prior to the nose gear making contact with the runway “the right wing hit an object (vehicle), causing the aircraft to veer out of control to the right eventually colliding with a second vehicle approximately 300 to 400 feet on the right side (southern) of Runway 06.” The impact of the right wing of the aircraft with the second vehicle, caused the right wing (outboard of the engine nacelle) and right fuel sealed wet wing tank to rupture releasing the aircraft fuel in that wing, which caused an explosion engulfing the vehicle in flames. The force of the impact with the second vehicle caused the right main gear to break away from the aircraft and it was flung ahead and to the left side of the runway approximately 200 feet from the point of impact with the truck. As the right main gear of the aircraft was no longer attached, the aircraft collapsed on its right side, slid onto the gravel south (right) of the runway and somewhere during this process, the nose gear also collapsed. The pilot immediately shut off the fuel valve of the aircraft and once the engines and the aircraft came to a stop, the three occupants evacuated the aircraft. The occupants of the aircraft did not sustain any visible injuries requiring medical attention or hospitalization. However, three (3) occupants of the second vehicle that was struck, were fatally injured. The airplane sustained substantial damages as a result of the impact and post impact crash sequence. The impact with the first vehicle occurred at approximately 427 feet from the threshold of runway 06 and at coordinates 28˚ 22’30”N and 073˚ 01’15’W. The flight was operated on an Instrument Flight Rules flight plan. Instrument Meteorological Conditions (night) prevailed at the time of the accident.
Probable cause:
Breakdown in communication during the planning and execution of an unapproved procedure has been determined to be the probable cause of this accident.
Other contributing factors:
- Use of an unapproved procedure to aid in a maneuver that was critical,
- Too many persons were planning the maneuver and not coordinating their actions,
- Failure of planners of the maneuver to verify whether participants were in the right position,
- Inexperienced persons used in the execution of a maneuver that was not approved,
- Vehicle parked to close to the side of the runway,
- Vehicle left with engine running while parked near the runway.
Final Report:

Crash of a Britten-Norman BN-2A-7 Islander in La Yesca

Date & Time: Dec 7, 2012
Type of aircraft:
Operator:
Registration:
XC-UPJ
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
La Yesca - Zapopan AFB
MSN:
307
YOM:
1971
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine aircraft was engaged in an ambulance flight from La Yesca to the Zapopan Air Base, carrying two soldiers who were injured in a car crash, and one pilot. During the takeoff roll, the airplane encountered strong crosswinds and went out of control. It veered off runway to the right and came to rest in a wooded area. All three occupants were rescued while the aircraft was damaged beyond repair.

Crash of a Piper PA-42-720 Cheyenne III off Grand Case: 4 killed

Date & Time: May 5, 2012 at 0240 LT
Type of aircraft:
Registration:
F-GXES
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Grand Case - Fort-de-France
MSN:
42-8001043
YOM:
1980
Flight number:
TIF520
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
3950
Captain / Total hours on type:
513.00
Aircraft flight hours:
7593
Aircraft flight cycles:
7830
Circumstances:
The twin engine aircraft was engaged in an ambulance flight between Grand Case and Fort-de-France and was carrying a pilot, a nurse, a doctor and a patient, a Greek citizen in honeymoon in Saint Martin who suffered a heart attack. He normally should be transferred to Fort-de-France from Saint Martin-Princess Juliana Airport with another Operator but the aircraft suffered technical problem prior to departure and the patient was transferred to Grand Case Airport. Piper PA-42 left Grand Case-L'Espérance runway 12 at 02H39. One minute later, during initial climb, it lost height and crashed into the Caribbean Sea, some three NM off the airport, off Tintamarre Island. Around 1000LT in the morning, a wheel and some others debris were found floating in water and no trace of the four occupants was found. They were later considered as deceased.
Probable cause:
The French BEA said in its final report that no technical anomaly to affect significantly the performance of the airplane or its pitch control could be demonstrated. It appears that the pilot had consumed alcohol before the flight and was awake since 0630LT and did not sleep over 20 hours, which could affect his capabilities. In conclusion, the investigation did not determine the cause of the accident, but the following factors may have contributed:
- aircraft's operation with one pilot only,
- absence of regulation does not allow the Civil Aviation Authority to ensure the adequacy of the operational objectives of an operator and its capacity to maintain its activity. This failure could not ensure that the pilot was able to conduct the flight.
- the presence of a flight recorder would probably help to understand the circumstances of the accident with more precision. Important data failed to the investigation, which was not able to identify all possible measures to avoid a similar accident in the future.
Final Report: