Crash of a Piper PA-31-310 Navajo in Taplin: 3 killed

Date & Time: May 6, 1977 at 0615 LT
Type of aircraft:
Registration:
N7439L
Flight Phase:
Survivors:
No
Schedule:
Taplin - Ambler
MSN:
31-328
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
18000
Captain / Total hours on type:
1000.00
Circumstances:
The takeoff was initiated in adverse weather conditions with fog. After takeoff, the twin engine airplane descended and crashed half a mile east of the airfield. The aircraft was destroyed and all three occupants were killed.
Probable cause:
Controlled flight into terrain during climb after the pilot initiated flight in adverse weather conditions. The exact cause of the accident could not be determined. The following findings were reported:
- Fog,
- Visibility 1/4 mile or less.
Final Report:

Crash of a Rockwell Aero Commander 560A in Davis: 2 killed

Date & Time: Jan 21, 1976 at 1146 LT
Operator:
Registration:
N91NR
Flight Phase:
Survivors:
No
Schedule:
Berkley Springs - Charleston
MSN:
560-234
YOM:
1955
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3096
Captain / Total hours on type:
457.00
Circumstances:
En route from Berckley Springs to Charleston, while in normal cruise, both engines failed. The crew elected to make an emergency landing when control was lost. The airplane crashed and was destroyed upon impact, killing both occupants.
Probable cause:
Uncontrolled descent following a double engine failure caused by a fuel exhaustion. The following contributing factors were reported:
- Inadequate preflight preparation,
- Mismanagement of fuel,
- Fuel exhaustion,
- Failed to maintain flying speed,
- Failure to provide adequate directives, manual, equipment,
- Fuel gauge read approximately 10 gallons high,
- Did not use positive method for checking fuel.
Final Report:

Crash of a Beechcraft C90 King Air in Charleston: 6 killed

Date & Time: Nov 4, 1975 at 0814 LT
Type of aircraft:
Registration:
N221MJ
Flight Phase:
Survivors:
No
Schedule:
Charleston - Wilmington
MSN:
LJ-512
YOM:
1971
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
4596
Captain / Total hours on type:
3923.00
Circumstances:
At liftoff, one of the engine failed. The crew lost control of the airplane that lost height and crashed in flames in woods downhill of dirt bank. The aircraft was destroyed and all six occupants have been killed.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported.
- Delayed action in aborting takeoff.
Final Report:

Crash of a Beechcraft 65 Queen Air in Williamstown: 4 killed

Date & Time: Feb 24, 1974 at 1452 LT
Type of aircraft:
Registration:
N9535Q
Flight Type:
Survivors:
No
Schedule:
Venice – Columbia – Wheeling
MSN:
LC-226
YOM:
1966
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
2300
Captain / Total hours on type:
17.00
Circumstances:
While descending to Williamstown, the pilot encountered poor weather conditions with low ceiling, snow falls and icing conditions. At an altitude of 8,000 feet, the left engine failed and the pilot continued the approach on one engine until he was forced to initiate a go-around manoeuvre. While in traffic pattern-circling, the airplane went out of control, stalled and crashed few miles from the airfield. The aircraft was destroyed and all four occupants were killed.
Probable cause:
Engine failure on approach. The following factors were reported:
- Improper operation of powerplant,
- Improper operation or failed to use anti-icing/deicing equipment,
- Ice carburetor,
- Improper in-flight decisions,
- Failed to maintain flying speed,
- Conditions conducive to carburetor/induction system icing,
- Low ceiling and snow,
- Lack of familiarity with aircraft,
- Reported ram ice at 8,000 feet.
Final Report:

Crash of a Rockwell Grand Commander 690 in Wellsburg: 3 killed

Date & Time: Aug 14, 1972 at 1010 LT
Registration:
N1NR
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pittsburgh – Wheeling
MSN:
690-11024
YOM:
1972
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
5507
Captain / Total hours on type:
7.00
Circumstances:
The crew was completing a training mission from Pittsburgh to Wheeling. While cruising at an altitude of 5,000 feet, the crew decided to perform several stalls when control was lost. The airplane entered a dive and crashed in flames in an open field located near Wellsburg. The aircraft was totally destroyed and all three occupants were killed.
Probable cause:
Loss of control in stall maneuver for unknown reason. Control not recovered before impact.
Final Report:

Crash of a Douglas DC-9-31 in Huntington: 75 killed

Date & Time: Nov 14, 1970 at 1936 LT
Type of aircraft:
Operator:
Registration:
N97S
Survivors:
No
Schedule:
Kinston - Huntington
MSN:
47245/510
YOM:
1969
Flight number:
SO932
Crew on board:
4
Crew fatalities:
Pax on board:
71
Pax fatalities:
Other fatalities:
Total fatalities:
75
Captain / Total flying hours:
18557
Captain / Total hours on type:
2194.00
Copilot / Total flying hours:
5872
Copilot / Total hours on type:
1196
Aircraft flight hours:
3667
Circumstances:
The airplane departed Kinston-Stallings Field, North Carolina, at 1838LT on a charter flight to Huntington, West Virginia, carrying players and fans of the Marshall University Football Team based in Huntington. Following an uneventful flight, the crew contacted Huntington Approach Control at 1923LT and was cleared for a runway 11 localizer approach. At 1934LT, the airplane passed the Outer Marker and the crew was cleared to land. In marginal weather conditions (mist and rain), the airplane descended below the minimum descent altitude and the crew failed to realize his altitude was too low when the aircraft struck trees and crashed in flames on the slope of a hill located one mile short of runway 11 threshold. The aircraft was totally destroyed by impact forces and a post crash fire and none of the 75 occupants survived the crash. At the time of the accident, there were scattered clouds at 300 feet, broken overcast at 500 feet and solid overcast at 1,000 feet. Among the 75 occupants were 36 players, nine coaches and administrators, 26 fans and four crew members.
Probable cause:
The descent below Minimum Descent Altitude during a non precision approach under adverse weather conditions, without visual contact with the runway environment. The Board has been unable to determine the reason for this descent, although the two most likely explanations are: a) improper use of cockpit instrument data; or b) an altimetry system error.
Final Report:

Crash of a Beechcraft U-8F Seminole in Huntington: 3 killed

Date & Time: Oct 29, 1970
Type of aircraft:
Operator:
Registration:
62-3865
Flight Type:
Survivors:
Yes
Schedule:
Fort Meade - Huntington
MSN:
LF-63
YOM:
1962
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The twin engine airplane was completing a liaison flight from Fort Meade, MD, to Huntington, WV. While approaching Huntington-Tri-State Airport by night and in heavy rain falls, the aircraft went out of control and crashed on final. One passenger was injured while three other occupants were killed, among them Major General Edwin H. Burba, Deputy Commander of the 1st Army.
Crew:
Cw2 Paul R. Burtt, pilot,
Cw3 Maynard V. Reisinger, copilot.
Passengers:
MG Edwin H. Burba +1.
Probable cause:
The accident was the consequence of a fatal design flaw in the fuel cross feed system.

Crash of a Howard 500 in Charleston

Date & Time: Jul 10, 1969 at 1948 LT
Operator:
Registration:
N320L
Survivors:
Yes
Schedule:
Washington DC – Dallas
MSN:
500-117
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7053
Captain / Total hours on type:
289.00
Circumstances:
While in cruising altitude, en route from Washington-Dulles Airport to Dallas, the crew encountered technical problems with the right engine. Decision was taken to shut down the engine and to feather the propeller. The crew was then cleared to divert to Charleston-Kanawha Airport for an emergency landing. During the final approach, the pilot supervisor interfered verbally in the process and the airplane landed 3,000 feet down the runway 23 which is 5,600 feet long. Unable to stop within the remaining distance, the airplane overran and came to rest in flames on a dirt bank. All seven occupants evacuated safely and the aircraft was destroyed.
Probable cause:
The exact cause of the powerplant failure could not be determined. However, it was reported that the pilot-in-command misjudged distance and speed upon landing.
Final Report:

Crash of a Fairchild-Hiller FH-227B in Charleston: 35 killed

Date & Time: Aug 10, 1968 at 0857 LT
Type of aircraft:
Operator:
Registration:
N712U
Survivors:
Yes
Schedule:
Cincinnati - Charleston
MSN:
557
YOM:
1967
Flight number:
PI230
Crew on board:
3
Crew fatalities:
Pax on board:
34
Pax fatalities:
Other fatalities:
Total fatalities:
35
Captain / Total flying hours:
6884
Captain / Total hours on type:
2809.00
Copilot / Total flying hours:
3722
Copilot / Total hours on type:
403
Aircraft flight hours:
2197
Circumstances:
Flight 230 was a scheduled domestic flight from Louisville, Kentucky, to Roanoke, Virginia, with en-route stops at Cincinnati, Ohio and Charleston, Kanawha County Airport, West Virginia. The flight to Cincinnati was routine. At 0805 hours eastern daylight time the flight departed Cincinnati on an IFR clearance to Charleston via Victor Airways 128 south to York, thence Victor 128 to Charleston, to maintain 9 000 ft. At 0835 hours the flight contacted the Charleston Tower to request the latest weather information, which was provided as: sky partially obscured, visibility 4 mile fog and smoke, runway 23 visibility less than 1/8 of a mile. Shortly thereafter it was cleared by the Indianapolis ARTCC to the Milton Intersection (10 miles west-northwest of the Charleston VORTAC on Victor 128) and to descend to and maintain 5 000 ft. At approximately 0841 hours the flight contacted Charleston Approach Control and reported leaving 6 000 for 5 000 ft. The controller advised the flight that radar contact had been established and instructed the flight to take a 070' heading for a vector to the holding pattern at the ILS outer marker. The latest weather was also given at this time as: sky partially obscured, visibility 4 mile, fog and smoke, runway visibility runway 23 zero, altimeter setting 29.94 in. The flight was then provided with holding instructions to be followed upon arrival over the outer marker compass locator (LOM) and was given an expected approach time of 0915 hours subject to weather conditions. At 0850 hours prior to reaching the LOM, the flight was instructed to turn right to a heading of 140°, cleared to descend to 2 400 ft and advised that the runway visibility for runway 23 had improved to seven-eighths of a mile. At 0851 hours the flight was advised that it was seven miles northeast of the outer locator, instructed to turn right to a 200' heading and cleared for an ILS approach. The flight acknowledged the clearance and it shortly thereafter was advised by the approach controller that the glide path was out of service. At 0852 hours the flight was advised that it was 5 miles from the LOM and instructed to contact Charleston Tower on 120.3 MHz. At 0853 hours radio contact with the flight was established by the tower local 'controller who cleared the flight to land. By that time the landing check had been completed by the crew and descent was established at a fairly constant rate of descent of approximately 620 ft/min. At 0854:40 hours the flight reported passing the outer marker inbound and requested the wind which was given as being 230°/4 kt. At 0855:55 hours the flight asked the tower if the approach lights and high intensity runway lights were turned all the way up and the controller replied in the affirmative, adding "a little fog right off the end there and its wide open after you get by that, it's more than a mile and a half on the runway". This was the last known radio communication from the flight. At 0856:09 hours the pilot-in-command mentioned to the co-pilot that he was going to hold the present altitude which was approximately 1 250 ft AMSL (350 ft above the elevation of runway 23 threshold). At 0856:24 hours the co-pilot informed the pilot-in-command that he had the lights in sight "down low" and asked him if he could see them. The pilot-in-command replied he had them in sight and requested landing flaps. The co-pilot then commented "I got to get to the chart right here we're likely to lose it". At 0856:42 hours the co-pilot asked the pilot-in-command if he saw the lights "there", the pilot-in-command replied in the affirmative and shortly thereafter reduced the power and 2 sec later increased it - 1 sec later the co-pilot commented "watch it". About 1 sec later the aircraft crashed. The controller observed a column of smoke rising near the approach end of the runway and immediately activated the crash siren and called for the dispatch of airport emergency equipment. The aircraft struck the steep hillside about 250 ft short of the runway threshold at an elevation of 865 ft AMSL (approximately 33 ft below the elevation of the threshold). The aircraft then careened up and over the side of the hill and on to the airport, coming to rest off the right side of runway 23. The accident occurred at 0856:53 hours during daylight. Two passengers were seriously injured while 35 other occupants were killed.
Probable cause:
The Board determined that the probable cause of this accident was an unrecognized loss of altitude orientation during the final portion of an approach into shallow, dense fog. The disorientation was caused by a rapid reduction in the ground guidance segment available to the pilot, at a point beyond which a go-around could not be successfully effected. The following findings were reported:
- The aircraft was being operated in visual meteorological conditions until approximately 6 sec before the crash, when it entered a shallow fog overlying the approach lights and the approach end of runway 23,
- Visual range in the final portion of the approach zone and over the runway 23 threshold was 500 ft or less in the fog,
- Because of the visual guidance segment available in the initial part of the approach, the pilot would have no way of judging the visual range in fog until the moment of penetration,
- Descent below MDA into the restricted visibility was permissible under present regulations.
Final Report:

Crash of a Cessna 402 in Beverly: 2 killed

Date & Time: Jul 20, 1968 at 0028 LT
Type of aircraft:
Operator:
Registration:
N4090Q
Flight Phase:
Flight Type:
Survivors:
No
Site:
MSN:
402-0190
YOM:
1968
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1671
Captain / Total hours on type:
193.00
Circumstances:
While cruising by night, the crew encountered poor visibility due to fog. At ant insufficient altitude, the twin engine aircraft struck the slope of a mountain located near Beverly. The aircraft was destroyed upon impact and both pilots were killed.
Probable cause:
The accident was the probable consequence of the following factors:
- Improper flight decision,
- Controlled flight into terrain.
Final Report: