Crash of a Howard 500 in Toronto: 3 killed

Date & Time: Jul 9, 1981
Operator:
Registration:
C-GKFN
Flight Phase:
Flight Type:
Survivors:
No
MSN:
500-107
YOM:
1943
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
Shortly after takeoff from Toronto-Lester Bowles Pearson Airport, while in initial climb, the twin engine airplane adopted a nose-up attitude then stalled and crashed, bursting into flames. The aircraft was destroyed and all three occupants were killed.
Probable cause:
It was determined that the aircraft was improperly loaded prior to takeoff and that the CofG was beyond the rear limit.

Crash of a Howard 500 in Key Largo

Date & Time: Jan 4, 1978 at 1440 LT
Registration:
N127LR
Survivors:
Yes
Schedule:
Mobile - Key Largo
MSN:
500-103
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12322
Captain / Total hours on type:
301.00
Circumstances:
Directional control was lost after touchdown at Key Largo-Ocean Reef Airport. The twin engine airplane ground looped and came to rest. All seven occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Ground loop during landing roll after the pilot-in-command failed to maintain directional control due to a poorly maintained runway surface.
Final Report:

Crash of a Howard 500 in Pawhuska

Date & Time: Aug 13, 1977 at 1120 LT
Registration:
N44HH
Survivors:
Yes
Schedule:
Houston - Pawhuska
MSN:
500-115
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8950
Captain / Total hours on type:
50.00
Circumstances:
After touchdown on a wet and short runway 17/35, the airplane encountered difficulties to stop within the remaining distance. It overran, hit obstacles and came to rest in flames. All four occupants were injured, three of them seriously. The aircraft was destroyed by fire.
Probable cause:
Overshoot and crashed on object following improper in-flight decisions. The following contributing factors were reported:
- Misjudged distance and speed,
- Selected wrong runway relative to existing wind,
- Low ceiling,
- Rain,
- Donwind,
- Hydroplaning on wet runway,
- Ran off end of runway.
Final Report:

Crash of a Howard Super Ventura in Egg Harbor: 2 killed

Date & Time: Feb 1, 1975 at 1032 LT
Operator:
Registration:
N234YU
Survivors:
No
Schedule:
Middletown - Atlantic City
MSN:
5283
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2543
Captain / Total hours on type:
965.00
Circumstances:
While descending to Atlantic City-Pomona Airport, the crew completed a 350° turn to join the approach path when control was lost. The airplane stalled and crashed in flames in Egg Harbor, few miles from the airport. The aircraft was destroyed and both pilots were killed.
Probable cause:
Failed to maintain flying speed on initial approach. The following contributing factors were reported:
- Airframe ice,
- Icing conditions including sleet and freezing rain,
- Crashed in steep nose down attitude during a 350° turn heading change to intercept localizer.
Final Report:

Crassh of an Howard 350 in Philadelphia

Date & Time: Oct 15, 1972 at 1127 LT
Operator:
Registration:
N361MC
Survivors:
Yes
Schedule:
Newark – Philadelphia
MSN:
5275
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3768
Captain / Total hours on type:
68.00
Circumstances:
After touchdown at Philadelphia-Intl Airport, the crew inadvertently retracted the gear. The twin engine airplane sank on its belly and slid for several yards before coming to rest in flames. All eight occupants escaped uninjured while the aircraft was partially destroyed by a post crash fire that was caused by the rupture of a fuel tank in the left wing.
Probable cause:
The pilot inadvertently retracted the gear after landing. Left wing tank ruptured.
Final Report:

Crash of a Howard Super Ventura in Austin

Date & Time: Aug 3, 1972 at 0923 LT
Operator:
Registration:
N446DD
Survivors:
Yes
Schedule:
Laredo - Dallas
MSN:
5696
YOM:
1943
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
20470
Captain / Total hours on type:
308.00
Circumstances:
En route from Laredo to Dallas, one of the engine lost power due to oil exhaustion. The pilot was cleared to divert to Austin-Robert Mueller Airport but following a wrong approach configuration, the aircraft was not properly aligned. After touchdown on a wet runway, the airplane suffered hydroplaning then veered off runway and came to rest. All three occupants were uninjured while the aircraft was damaged beyond repair.
Probable cause:
In-flight engine failure or malfunction. The following factors were reported:
- Inadequate maintenance and inspection,
- Oil exhaustion, engine lubrication system,
- Improper IFR operation,
- Failed to initiate a go-around,
- Lack of familiarity with aircraft,
- Wet runway,
- Rain,
- Poorly planned approach,
- Not aligned with runway,
- Hydroplaning on wet runway,
- Partial loss of power on one engine,
- Cause of oil exhaustion not determined,
- Annual maintenance check performed the day before the accident,
- Other runway available,
- Wrong switch used for wipers.
Final Report:

Crash of an Howard Eldorado 700 in Philadelphia

Date & Time: Sep 11, 1971 at 0922 LT
Registration:
N25YC
Survivors:
Yes
Schedule:
Reading – Philadelphia
MSN:
5598
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
19000
Captain / Total hours on type:
400.00
Circumstances:
On approach to Philadelphia International Airport, the crew encountered poor weather conditions with thunderstorm activity, heavy rain falls and turbulences. On short final, the captain decided to make a go-around when the airplane struck the ground and crashed few miles short of runway. All six occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Improper IFR operation on part of the crew who descended below MDA while encountering severe turbulences and heavy rain from a thunderstorm cell. The weather was slightly worse than forecast.
Final Report:

Crash of an Howard 350 in Miami

Date & Time: Aug 18, 1970 at 2018 LT
Registration:
N350Q
Flight Type:
Survivors:
Yes
Schedule:
Brooksville - Miami
MSN:
5892
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7600
Captain / Total hours on type:
211.00
Circumstances:
Following an uneventful positioning flight from Brooksville-Hernando County Airport, the crew started the approach to Miami-Opa Locka Airport. The twin engine airplane landed on its belly and slid for several yards before coming to rest in flames. Both crew members escaped without injuries while the aircraft was destroyed.
Probable cause:
The exact cause of the accident could not be determined with certainty. The crew reported that the gear was lowered prior to touchdown while the gear handle was found in up position.
Final Report:

Crash of a Howard 500 in Charleston

Date & Time: Jul 10, 1969 at 1948 LT
Operator:
Registration:
N320L
Survivors:
Yes
Schedule:
Washington DC – Dallas
MSN:
500-117
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7053
Captain / Total hours on type:
289.00
Circumstances:
While in cruising altitude, en route from Washington-Dulles Airport to Dallas, the crew encountered technical problems with the right engine. Decision was taken to shut down the engine and to feather the propeller. The crew was then cleared to divert to Charleston-Kanawha Airport for an emergency landing. During the final approach, the pilot supervisor interfered verbally in the process and the airplane landed 3,000 feet down the runway 23 which is 5,600 feet long. Unable to stop within the remaining distance, the airplane overran and came to rest in flames on a dirt bank. All seven occupants evacuated safely and the aircraft was destroyed.
Probable cause:
The exact cause of the powerplant failure could not be determined. However, it was reported that the pilot-in-command misjudged distance and speed upon landing.
Final Report:

Crash of a Howard 500 in Gaylord

Date & Time: Mar 2, 1969 at 1707 LT
Operator:
Registration:
N3403
Flight Phase:
Survivors:
Yes
MSN:
5249
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10000
Captain / Total hours on type:
4000.00
Circumstances:
During the takeoff roll at Gaylord-Otsego County Airport, the twin engine aircraft swerved on runway then struck a five foot snow bank located on the side of the runway before coming to rest. All seven occupants were uninjured while the aircraft was considered as damaged beyond repair.
Probable cause:
The crew failed to maintain directional control and the airplane ground looped due to sunglare and airport conditions.
Final Report: