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Crash of a Piper PA-31T Cheyenne II in Lafayette: 5 killed

Date & Time: Dec 28, 2019 at 0921 LT
Type of aircraft:
Registration:
N42CV
Flight Phase:
Survivors:
Yes
Site:
Schedule:
Lafayette - Atlanta
MSN:
31T-8020067
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1531
Captain / Total hours on type:
730.00
Aircraft flight hours:
5954
Circumstances:
The personal flight departed from Lafayette Regional Airport/Paul Fournet Field (LFT), Lafayette, Louisiana, and entered the clouds when the airplane was at an altitude of about 200 ft above ground level. Before takeoff, the controller issued an instrument flight rules clearance to the pilot, instructing him to turn right onto a heading of 240° and climb to and maintain an altitude of 2,000 ft mean sea level (msl) after takeoff. Automatic dependent surveillance-broadcast (ADS-B) data for the accident flight started at 0920:05, and aircraft performance calculations showed that the airplane was climbing through an altitude of 150 ft msl at that time. The calculations also showed that the airplane then turned slightly to the right toward the assigned heading of 240° and climbed at a rate that varied between 1,000 and 2,400 ft per minute and an airspeed that increased from about 151 to 165 knots. At 0920:13, the airplane started rolling back toward wings level and, 7 seconds later, rolled through wings level and toward the left. At that time, the airplane was tracking 232° at an altitude of 474 ft and an airspeed of 165 knots. The airplane’s airspeed remained at 165 knots for about 10 seconds before it started increasing again, and the airplane continued to roll steadily to the left at an average roll rate of about 2° per second. The aircraft performance calculations further showed that, at 0920:40, the airplane reached a peak altitude of 925 ft msl. At that time, the airplane was tracking 200°, its bank angle was about 35° to the left, and its airspeed was about 169 knots. The airplane then started to descend while the left roll continued. At 0920:55, the airplane reached a peak airspeed of about 197 knots, which then started decreasing. At 0920:57, the airplane descended through 320 ft at a rate of descent of about 2,500 ft per minute and reached a bank angle of 75° to the left. At 0920:58, the controller issued a low altitude alert, stating that the pilot should “check [the airplane’s] altitude immediately” because the airplane appeared to be at an altitude of 300 ft msl. The pilot did not respond, and no mayday or emergency transmission was received from the airplane. The last ADS-B data point was recorded at 0920:59; aircraft performance calculations showed that, at that time, the airplane was descending through an altitude of 230 ft msl at a flightpath angle of about -7°, an airspeed of 176 knots, and a rate of descent of about 2,300 ft per minute. (The flightpath angle is in the vertical plane—that is, relative to the ground. The ground track, as discussed previously, is in the horizontal plane—that is, relative to north.) The airplane struck trees and power lines before striking the ground, traveled across a parking lot, and struck a car. The car rolled several times and came to rest inverted at the edge of the parking lot, and a postcrash fire ensued. The airplane continued to travel, shedding parts before coming to rest at the far end of an adjacent field. At the accident site, the surviving passenger told a local police officer that “the plane went straight up and then straight down.”
Probable cause:
The pilot’s loss of airplane control due to spatial disorientation during the initial climb in instrument meteorological conditions.
Final Report:

Crash of a Socata TBM-850 in Fayetteville

Date & Time: Oct 5, 2014 at 1255 LT
Type of aircraft:
Operator:
Registration:
N536EM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Atlanta – Pine Mountain
MSN:
536
YOM:
2010
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4244
Captain / Total hours on type:
411.00
Aircraft flight hours:
719
Circumstances:
The private pilot was conducting a personal cross-country flight. The pilot reported that, during cruise flight at 6,000 ft mean sea level, he observed a crew alerting system oil pressure message, followed by a total loss of engine power. An air traffic controller provided vectors to a local airport; however, the pilot reported that the airplane would not reach the runway. He did not attempt to restart the engine. He feathered the propeller and placed the power lever to "idle" and the condition lever to "cut off." The pilot subsequently attempted a forced landing to a sports field with the gear and flaps retracted. The airplane collided with trees and the ground and then came to rest upright. Examination of the engine revealed that it displayed contact signatures to its internal components and evidence of ingested unburned organic debris, consistent with the engine likely being unpowered and the engine gas generator and power sections wind-milling at the time of impact. No evidence of any preimpact mechanical anomalies or malfunctions to any of the engine components was found that would have precluded normal operation. Recorded GPS flight track and systems data showed that the loss of engine power was preceded by about 5 minutes of flight on a constant heading and altitude with an excessive lateral g force of about 0.17 g and a bank angle between about 8 and 10 degrees, consistent with a side-slip flight condition. The airplane then entered a right turn with the autopilot engaged, and it lost power at the end of the turn. The data indicated that, even though the autopilot was engaged, the lateral g forces increased as the airplane leveled off and accelerated, indicating that the automatic rudder trim feature of the yaw damper system was not engaged. Given that the yaw damper system operated normally after the flight, it is likely that the pilot inadvertently and unknowingly disengaged the yaw damper during flight with the autopilot engaged. During a postaccident interview, the pilot stated that he was not aware of a side-slip condition before the loss of engine power. Although the fuel tank system was designed to prevent unporting of the fuel lines during momentary periods of uncoordinated flight, it was not intended to do so for extended periods of uncoordinated flight. Therefore, the fuel tank feed line likely unported during the prolonged uncoordinated flight, which resulted in the subsequent loss of engine power. If the pilot had recognized the side-slip condition, he could have returned to coordinated flight and prevented the engine power loss. Also, once the airplane returned to coordinated flight, an engine restart would have been possible.
Probable cause:
The pilot's inadvertent deactivation of the yaw damper in flight, which resulted in a prolonged side-slip condition that led to fuel starvation and the eventual total loss of engine power. Contributing to the accident was the pilot's failure to attempt to restart the engine.
Final Report:

Crash of a Beechcraft Beechjet 400A in Atlanta

Date & Time: Jun 18, 2012 at 1006 LT
Type of aircraft:
Operator:
Registration:
N826JH
Survivors:
Yes
Schedule:
Gadsden - Atlanta
MSN:
RK-70
YOM:
1993
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10800
Captain / Total hours on type:
1500.00
Copilot / Total flying hours:
3500
Copilot / Total hours on type:
150
Aircraft flight hours:
4674
Circumstances:
The second-in-command (SIC) was the pilot flying for most of the flight (takeoff, climb, cruise, and descent) and was in the left seat, while the pilot-in-command (PIC) was the pilot monitoring for most of the flight and was in the right seat. Before takeoff, the PIC calculated reference speed (Vref) for the estimated landing weight and flaps 30-degree extension was 120 knots, with a calculated landing distance of 3,440 ft. Further, before takeoff, there were no known mechanical difficulties with the brakes, flaps, antiskid, or traffic alert and collision avoidance (TCAS) systems. After takeoff and for most of the flight, the PIC coached/instructed the SIC, including instructions on how to set the airspeed command cursor, a request to perform the after-takeoff checklist, and a comment to reduce thrust to silence an overspeed warning aural annunciation. When the flight was northwest of Dekalb Peachtree Airport (PDK), Atlanta, Georgia, on a right base leg for a visual approach to runway 20L with negligible wind, air traffic controllers repeatedly announced the location and distance of a Cessna airplane (which was ahead of the Beech 400A on a straight-in visual approach to runway 20R). Because the Beech 400A flight crew did not see the other airplane, the controllers appropriately instructed them to maintain their altitude (which was 2,300 ft mean sea level [msl]) for separation until they had the traffic in sight; radar data indicated the Beech 400A briefly descended to 2,200 ft msl then climbed back to 2,300 ft msl. According to the cockpit voice recorder (CVR) transcript, at 1004:42, which was about 12 seconds after the controller instructed the Beech 400A flight crew to maintain altitude, the on board TCAS alerted "traffic traffic." While the Beech 400A did climb back to 2,300 ft msl, this was likely a response to the air traffic control (ATC) instruction to maintain altitude and not a response to the TCAS "traffic traffic" warning. At 1004:47, the CVR recorded the SIC state, "first degree of," likely referring to flap extension, but the comment was not completed. The CVR recorded an immediate increase in background noise, which was likely due to the landing gear extension. The PIC then advised the local controller that the flight was turning onto final approach. The CVR did not record any approach briefing or discussion of runway length or Vref speed. After landing on runway 20L at Atlanta-DeKalb Peachtree Airport, aircraft did not stop as expected. It overrun the runway, went through a fence and came to rest near a road, broken in two. All four occupants were injured, both pilots seriously.
Probable cause:
The flight crew's failure to obtain the proper airspeed for landing, which resulted in the airplane touching down too fast with inadequate runway remaining to stop and a subsequent
runway overrun. Contributing to the accident were the failure of either pilot to call for a go-around and the flight crew's poor crew resource management and lack of professionalism.
Final Report:

Crash of a Socata TBM-700 in Morristown: 5 killed

Date & Time: Dec 20, 2011 at 1005 LT
Type of aircraft:
Operator:
Registration:
N731CA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Teterboro - Atlanta
MSN:
332
YOM:
2005
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1400
Aircraft flight hours:
702
Circumstances:
Although the pilot filed an instrument flight rules flight plan through the Direct User Access Terminal System (DUATS), no evidence of a weather briefing was found. The flight departed in visual meteorological conditions and entered instrument meteorological conditions while climbing through 12,800 feet. The air traffic controller advised the pilot of moderate rime icing from 15,000 feet through 17,000 feet, with light rime ice at 14,000 feet. The controller asked the pilot to advise him if the icing worsened, and the pilot responded that he would let them know and that it was no problem for him. The controller informed the pilot that he was coordinating for a higher altitude. The pilot confirmed that, while at 16,800 feet, "…light icing has been present for a little while and a higher altitude would be great." About 15 seconds later, the pilot stated that he was getting a little rattle and requested a higher altitude as soon as possible. About 25 seconds after that, the flight was cleared to flight level 200, and the pilot acknowledged. About one minute later, the airplane reached a peak altitude of 17,800 feet before turning sharply to the left and entering a descent. While descending through 17,400 feet, the pilot stated, "and N731CA's declaring…" No subsequent transmissions were received from the flight. The airplane impacted the paved surfaces and a wooded median on an interstate highway. A postaccident fire resulted. The outboard section of the right wing and several sections of the empennage, including the horizontal stabilizer, elevator, and rudder, were found about 1/4 mile southwest of the fuselage, in a residential area. Witnesses reported seeing pieces of the airplane separating during flight and the airplane in a rapid descent. Examination of the wreckage revealed that the outboard section of the right wing separated in flight, at a relatively low altitude, and then struck and severed portions of the empennage. There was no evidence of a preexisting mechanical anomaly that would have precluded normal operation of the airframe or engine. An examination of weather information revealed that numerous pilots reported icing conditions in the general area before and after the accident. At least three flight crews considered the icing "severe." Although severe icing was not forecasted, an Airmen's Meteorological Information (AIRMET) advisory included moderate icing at altitudes at which the accident pilot was flying. The pilot operating handbook warned that the airplane was not certificated for flight in severe icing conditions and that, if encountered, the pilot must exit severe icing immediately by changing altitude or routing. Although the pilot was coordinating for a higher altitude with the air traffic controller at the time of the icing encounter, it is likely that he either did not know the severity of the icing or he was reluctant to exercise his command authority in order to immediately exit the icing conditions.
Probable cause:
The airplane’s encounter with unforecasted severe icing conditions that were characterized by high ice accretion rates and the pilot's failure to use his command authority to depart the icing conditions in an expeditious manner, which resulted in a loss of airplane control.
Final Report:

Crash of an IAI 1125 Astra APX in Atlanta

Date & Time: Sep 14, 2007 at 1719 LT
Type of aircraft:
Operator:
Registration:
N100G
Survivors:
Yes
Schedule:
Coatesville - Atlanta
MSN:
092
YOM:
1998
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10800
Captain / Total hours on type:
2200.00
Copilot / Total flying hours:
16042
Copilot / Total hours on type:
1500
Aircraft flight hours:
4194
Circumstances:
The pilot-in-command (PIC) of the of the airplane was the flight department's chief pilot, who was in the right seat and monitoring the approach as the non-flying pilot. The second-in-command (SIC) was a captain for the flight department, who was in the left seat and the flying pilot. On arrival at their destination, they were vectored for an instrument-landing-system (ILS) approach to a 6,001-foot-long runway. Visibility was 1-1/4 miles in rain. The autopilot was on and a coupled approach was planned. After the autopilot captured the ILS, the airplane descended on the glideslope. The PIC announced that the approach lights were in sight and the SIC stated that he also saw the lights and disengaged the autopilot. The SIC turned on the windshield wipers and then lost visual contact with the runway. He announced that he lost visual contact, but the PIC stated that he still saw the runway. The SIC considered a missed approach, but continued because the PIC still had visual contact. The PIC stated, "I have the lights" and began to direct the SIC. He then "took over the controls." The airplane touched down, the speed brakes extended and, approximately 1,000 feet later, the airplane overran the runway. The PIC stated that he was confused as to who was the PIC, and that he and the SIC were "co-captains." When asked about standard operating procedures (SOPs), the PIC advised that they did not have any. They had started out with one pilot and one airplane, and they now had five pilots and two airplanes. The PIC later stated that they probably should have gone around when the flying pilot could not see out the window. The PIC added that the windshields had no coating and did not shed water. One year prior, while flying in rain, his vision through the windshield was blurred but he did not report it to their maintenance provider. Manufacturer's data revealed that the windshield was coated to enhance vision during rain conditions. The manufacturer advised that the coating might not last the life of the windshield and provided guidance to determine both acceptable and unacceptable rain repellent performance.
Probable cause:
The pilot's failure to initiate a missed approach and his failure to obtain the proper touchdown point while landing in the rain. Contributing to the accident were the operator's lack of standard operating procedures and the inadequate maintenance of the windshield.
Final Report:

Crash of a Beechcraft B60 Duke in Atlanta:1 killed

Date & Time: Aug 18, 2000 at 2244 LT
Type of aircraft:
Operator:
Registration:
N8WD
Flight Type:
Survivors:
No
Schedule:
Houston – Atlanta-DeKalb-Peachtree
MSN:
P-258
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1800
Aircraft flight hours:
2665
Circumstances:
The pilot had experienced engine problems during a flight and requested maintenance assistance from the local maintenance repair station. Before the maintenance personnel signed off and completed the repairs, the pilot refueled the airplane, and attempted an instrument flight back to the originating airport. While enroute, the pilot reported a low fuel situation, and deviated to a closer airport. During the approach, the airplane lost engine power on both engines, collided with trees, and subsequently the ground, about a half of a mile short of the intended runway. There was no fuel found in the fuel system at the accident site. No mechanical problems were discovered with the airplane during the post-accident examination. This accident was the second time the pilot had exhausted the fuel supply in this airplane.
Probable cause:
The pilot's failure to preflight plan adequate fuel for the flight that resulted in fuel exhaustion and the subsequent loss of engine power.
Final Report:

Crash of a Piper PA-61P Aerostar (Ted Smith 601P) in Chesapeake: 4 killed

Date & Time: Jan 2, 1997 at 1937 LT
Operator:
Registration:
N3CD
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Chesapeake – Atlanta
MSN:
61-0353-108
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
2100
Aircraft flight hours:
1949
Circumstances:
The airplane departed the airport and crashed shortly thereafter. Before departure, the airplane was fueled with 120 gallons of 100LL aviation fuel. According to the refueler, the airplane had full fuel tanks. The refueler also indicated the pilot had stated he wanted to be airborne prior to the arrival of bad weather. After the accident, the engines and propellers were disassembled and examined. No engine or propeller discrepancies were noted, except (post impact) heat damage.
Probable cause:
Failure of the pilot to maintain proper altitude/clearance above the ground after takeoff. A related factor was the pilot's self-induced pressure to depart before the arrival of bad weather.
Final Report:

Crash of a Beechcraft A100 King Air in Atlanta: 1 killed

Date & Time: Jan 18, 1990 at 1904 LT
Type of aircraft:
Operator:
Registration:
N44UE
Flight Type:
Survivors:
Yes
Schedule:
Atlanta - Atlanta
MSN:
B-140
YOM:
1973
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1653
Circumstances:
During arrival at night, Beechcraft A100 (King Air, N44UE) was cleared for an ILS runway 26R approach behind Continental flight 9687, then Eastern Airline (EA) flight 111 (Boeing 727, N8867E) was cleared for the same approach behind the King Air. After landing, flight 9687 had a radio problem and the tower controller had difficulty communicating with flight 9687. Meanwhile, the King Air landed and its crew had moved the aircraft to the right side of the runway near taxiway Delta (the primary taxiway for general aviation aircraft). The turnoff for taxiway Delta was about 3,800 feet from the approach end of runway 26R. Before the King Air was clear of the runway, EA111 landed and converged on the King Air. The crew of EA111 did not see the King Air until moments before the accident. The captain tried to avoid a collision, but the Boeing's right wing struck the King Air, shearing the top of its fuselage and cockpit. Some of the King Air's strobe/beacon lights were inoperative, though they most likely would have been extinguished for the IMC approach. The local controller did not issue a traffic advisory to EA111 with the landing clearance. One of the pilot on board the King Air was killed while the second was seriously injured.
Probable cause:
1) Failure of the Federal Aviation Administration to provide air traffic control procedures that adequately take into consideration human performance factors such as those which resulted in the failure of the north local controller to detect the developing conflict between N44UE and EA111, and
2) the failure of the north local controller to ensure the separation of arriving aircraft which were using the same runway.
Contributing to the accident was the failure of the north local controller to follow the prescribed procedure of issuing appropriate traffic information to EA111, and failure of the north final controller and the radar monitor controller to issue timely speed reductions to maintain adequate separation between aircraft on final approach.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) in Lithia Springs: 3 killed

Date & Time: Jun 21, 1989 at 0823 LT
Registration:
N83AT
Flight Phase:
Survivors:
No
Schedule:
Atlanta – Memphis
MSN:
61-0296-074
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
10000
Aircraft flight hours:
1454
Circumstances:
Eleven minutes after departure the pilot reported smoke and a right engine problem, then said 'going down'. Right wing and engine assemblies separated in flight. Fire damage vicinity of right engine left turbocharger; tailpipe assembly had separated. Heavy smoke and heat damage between right wing forward and aft wing spars. Tailpipe had failed in fatigue near flange where attached to turbocharger exhaust port. Evidence of non-uniformly seated gasket between flanges. Also, right engine lower left engine mount deteriorated; significant portion of rubber missing. Piper sb #818 (ad87-07-09) accomplished 5/21/88; requires removal and inspection of exhaust system for cracks and reinstallation with new flange gaskets.
Probable cause:
Inflight engine/wing fire due to a failure of the right engine's left exhaust tailpipe. The exhaust tailpipe failed in fatigue as a result of fluctuating stresses induced by a deteriorated engine mount in conjunction with unevenly distributed clamping loads caused by an improperly seated gasket.
Final Report:

Crash of a Beechcraft 200 Super King Air in Pensacola: 3 killed

Date & Time: Apr 10, 1989 at 1300 LT
Registration:
N30PC
Flight Phase:
Survivors:
No
Schedule:
Pensacola - Atlanta
MSN:
BB-702
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
14200
Captain / Total hours on type:
3000.00
Aircraft flight hours:
6351
Circumstances:
The aircraft was routinely flown to Pensacola to pickup a gulf power executive for a flight to Atlanta. The pax had 4 bags, 2 placed in the aft baggage area by the ground crew, the other 2 carried onboard by the pax. After takeoff the CVR recorded the pax stating that there was a fire. The fire in the aft cabin area was confirmed by the 1st officer. An emergency was declared to the personnel ATCT. Subsequently, the aircraft was seen descending out of the overcast streaming dark smoke behind it. The aircraft impacted an apartment complex and a post crash fire destroyed it. No evidence of a lightning strike, aircraft system malfunction, or incendiary device was found during the investigation. Forensic chemical tests showed traces of hydrochloric and sulphuric acid on pax articles but none on the cabin interior. Metallurgical exam of broken fuel line showed overload failure and post heat distress. The interior of the cockpit windows were severely sooted. The flight crew did not don available oxygen masks.
Probable cause:
An in flight cabin fire of undetermined origin, and smoke (toxic condition) in the crew compartment, which resulted in physical impairment of the flight crew.
Final Report: