Crash of a Learjet 35A in Freeport: 9 killed

Date & Time: Nov 9, 2014 at 1652 LT
Type of aircraft:
Registration:
N17UF
Survivors:
No
Site:
Schedule:
Nassau - Freeport
MSN:
258
YOM:
1979
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
13800
Copilot / Total flying hours:
996
Aircraft flight hours:
12046
Aircraft flight cycles:
10534
Circumstances:
The aircraft crashed into a garbage and metal recycling plant after striking a towering crane in the Grand Bahama Shipyard, while attempting a second landing approach to runway 06 at Freeport International Airport (MYGF), Freeport, Grand Bahama, Bahamas. The aircraft made an initial ILS instrument approach to Runway 06 at the Freeport International Airport but due to poor visibility and rain at the decision height, the crew executed a go around procedure. The crew requested to hold at the published holding point at 2,000 feet while they waited for the weather to improve. Once cleared for the second ILS approach, the crew proceeded inbound from the holding location to intercept the localizer of the ILS system associated with the instrument approach. During the approach, the crew periodically reported their position to ATC, as the approach was not in a radar environment. The crew was given current weather conditions and advised that the conditions were again deteriorating. The crew continued their approach and descended visually while attempting to find the runway, until the aircraft struck the crane positioned at Dock #2 of the Shipyard at approximately 220 feet above sea level, some 3.2 nautical miles (nm) from the runway threshold. A fireball lasting approximately 3 seconds was observed as a result of the contact between the aircraft and the crane. The right outboard wing, right landing gear and right wingtip fuel tank, separated from the aircraft on impact. This resulted in the aircraft travelling out of control, some 1,578 feet (526 yards) before crashing inverted into a pile of garbage and other debris in the City Services Garbage and Metal Recycling Plant adjacent to the Grand Bahama Shipyard. Both crew and 7 passengers were fatally injured. No person on the ground was injured. The crane in the shipyard that was struck received minimal damages while the generator unit and other equipment in the recycling plant received extensive damages.
Probable cause:
The Air Accident Investigation & Prevention Unit (AAIPU) determines that the probable cause(s) of this accident were:
- The poor decision making of the crew in initiating and continuing a descent in IMC below the authorized altitude, without visual contact with the runway environment.
Contributing Factors includes:
- Improper planning of the approach,
- Failure of the crew to follow the approved ILS approach while in IMC conditions,
- Insufficient horizontal or vertical situational awareness,
- Poor decision making,
- Deliberate actions of the crew by disabling the terrain alert warning system,
- Inadequate CRM practice.
Final Report:

Crash of a Cessna 340A off Freeport: 4 killed

Date & Time: Aug 18, 2014 at 1002 LT
Type of aircraft:
Registration:
N340MM
Flight Type:
Survivors:
No
Schedule:
Ormond Beach - Freeport
MSN:
340A-0635
YOM:
1978
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Aircraft flight hours:
5572
Circumstances:
On 18 August, 2014 at 10:02am local time (1402Z) UTC a fixed wing, twin-engine, Cessna 3 4 0 A aircraft, United States registration N340MM, serial number 340A0635, crashed into waters while on a left base to runway 06 at Grand Bahama International Airport (MYGF) Freeport, Grand Bahama, Bahamas. The aircraft departed Ormond Beach Municipal Airport (KOMN) at 8:51am local time (1251Z) for Grand Bahama International Airport (MYGF) on an Instrument Flight Rules (IFR) flight plan with the pilot and three passengers aboard. Sometime after 9:00am (1300Z) an IFR inbound flight plan on N340MM was received by Freeport Approach Control from Miami Center. Upon initial contact with Freeport Approach Control the pilot was given weather advisory, re-cleared to Freeport VOR and told to maintain four thousand feet and report at JAKEL intersection. He was also advised to expect an RNAV runway six approach. After the pilot’s acknowledgement of the information he later acknowledged his position crossing JAKEL. Freeport Approach then instructed the aircraft to descend to two thousand feet and cleared him direct to JENIB intersection for the RNAV runway six (6) approach. After descending to two thousand feet the pilot indicated to Freeport Approach that he had the field in sight and was able to make a visual approach. Freeport Approach re-cleared the aircraft for a visual approach and instructed the pilot to contact Freeport Control Tower on frequency 118.5. At 9:57am (1357Z) N340MM established contact with Freeport Tower and was cleared for the visual approach to runway six; he was told to join the left base and report at five (5) DME. At 10:01am (1401Z) the pilot reported being out of fuel and his intention was to dead stick the aircraft into the airport from seven miles out at an altitude of one thousand five hundred feet. A minute later the pilot radioed ATC to indicate they “were going down and expected to be in the water about five miles north of the airport.” Freeport Tower tried to get confirmation of the last transmission but was unable to. Several more calls went out from Freeport Tower to N340MM but communication was never reestablished. Freeport Control Tower then made request of aircrafts departing and arriving to assist in locating the lost aircraft by over flying the vicinity of the last reported position to see if visual contact could be made. An inbound aircraft reported seeing an aircraft down five miles from the airport on the 300 degree radial of the ZFP VOR. Calls were made to all the relevant agencies and search and rescue initiated. The aircraft was located at GPS coordinates 26˚ 35.708’N and 078˚ 47. 431 W. The aircraft received substantial damage as a result of the impact and crash sequence. There were no survivors.
Probable cause:
The probable cause of this accident has been determined as a lack of situational awareness resulting in a stalled condition and loss of control while attempting to remedy a fuel exhaustion condition at a very low altitude.
Contributing factors:
- The pilot’s incorrect fuel calculations which resulted in fuel exhaustion to both engines.
- Stalled aircraft.
- Loss of situational awareness.
Final Report:

Crash of a Cessna 501 Citation I/SP in Stella Maris

Date & Time: Feb 15, 2014 at 1640 LT
Type of aircraft:
Operator:
Registration:
C-GKPC
Survivors:
Yes
Schedule:
Fort Lauderdale - Stella Maris
MSN:
501-0253
YOM:
1983
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
4579
Circumstances:
The aircraft belly landed at Stella Maris-Estate Airport, Bahamas. No one was hurt but the aircraft was damaged beyond repair. Apparently, the approach checklist was interrupted by the crew for unknown reason and the landing procedure was performed with the landing gear still retracted. The aircraft was owned by the private Canadian company Kelly Panteluk Construction and the airplane was inbound from Fort Lauderdale-Executive.

Crash of a Piper PA-46R-350T Matrix off Cat Cay

Date & Time: Aug 25, 2013 at 1406 LT
Registration:
N720JF
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cat Cay - Kendall-Miami
MSN:
46-92004
YOM:
2008
Location:
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12250
Captain / Total hours on type:
210.00
Aircraft flight hours:
1000
Circumstances:
According to the pilot, he applied full power, set the flaps at 10 degrees, released the brakes, and, after reaching 80 knots, he rotated the airplane. The pilot further reported that the engine subsequently lost total power when the airplane was about 150 ft above ground level. The airplane then impacted water in a nose-down, right-wing-low attitude about 300 ft from the end of the runway. The pilot reported that he thought that the runway was 1,900 ft long; however, it was only 1,300 ft long. Review of the takeoff ground roll distance charts contained in the Pilot’s Operating Handbook (POH) revealed that, with flap settings of 0 and 20 degrees, the ground roll would have been 1,700 and 1,150 ft, respectively. Takeoff ground roll distances were not provided for use of 10 degrees of flaps; however, the POH stated that 10 degrees of flaps could be used. Although the distance was not specified, it is likely that the airplane would have required more than 1,300 ft for takeoff with 10 degrees of flaps. Examination of the engine revealed saltwater corrosion throughout it; however, this was likely due to the airplane’s submersion in water after the accident. No other mechanical malfunctions or abnormalities were noted. Examination of data extracted from the multifunction display (MFD) and primary flight display (PFD) revealed that the engine parameters were performing in the normal operating range until the end of the recordings. The data also indicated that, 7 seconds before the end of the recordings, the airplane pitched up from 0 to about 17 degrees and then rolled 17 degrees left wing down while continuing to pitch up to 20 degrees. The airplane then rolled 77 degrees right wing down and pitched down about 50 degrees. The highest airspeed recorded by the MFD and PFD was about 70 knots, which occurred about 1 second before the end of the recordings. The POH stated that, depending on the landing gear position, flap setting, and bank angle, the stall speed for the airplane would be between 65 and 71 knots. Based on the evidence, it is likely that the engine did not lose power as reported by the pilot. As the airplane approached the end of the runway and the pilot realized that it was not long enough for his planned takeoff, he attempted to lift off at an insufficient airspeed and at too high of a pitch angle, which resulted in an aerodynamic stall at a low altitude. If the pilot had known the actual runway length, he might have used a flap setting of 20 degrees, which would have provided sufficient distance for the takeoff.
Probable cause:
The pilot’s attempt to rotate the airplane before obtaining sufficient airspeed and his improper pitch control during takeoff, which resulted in the airplane exceeding its critical angle-of-attack and subsequently experiencing an aerodynamic stall at a low altitude. Contributing to the accident was the pilot’s lack of awareness of the length of the runway, which led to his attempting to take off with the airplane improperly configured.
Final Report:

Crash of a Saab 340 in Marsh Harbour

Date & Time: Jun 13, 2013 at 1345 LT
Type of aircraft:
Operator:
Registration:
C6-SBJ
Survivors:
Yes
Schedule:
Fort Lauderdale – Marsh Harbour
MSN:
316
YOM:
1992
Flight number:
SBM9561
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
21
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8500
Captain / Total hours on type:
4700.00
Aircraft flight hours:
45680
Aircraft flight cycles:
49060
Circumstances:
On Thursday June 13, 2013 at approximately 1750UTC (1:50pm local time), a fixed wing, twin turboprop regional airliner, was involved in an accident as a result of a runway excursion while landing during heavy rain showers at Marsh Harbor Int’l Airport, Marsh Harbor, Abaco, Bahamas. The aircraft, a SAAB 340B aircraft was operated by SkyBahamas Airlines and bore Bahamas registration C6-SBJ, serial number 316. C6-SBJ departed Fort Lauderdale Int’l Airport (KFLL), Fort Lauderdale, Florida in the USA as Tropical Sky 9561. The airline, SkyBahamas Airline is a Bahamas Air Operator Certificate Holder with approved scheduled operations to and from Fort Lauderdale International Airport, Florida USA (KFLL) and Marsh Harbor Int’l Airport, Marsh Harbor, Abaco in the Bahamas. The crew received weather information and IFR route clearance from KFLL Control Tower. This passenger carrying flight departed KFLL at 1706UTC (1:06pm local) on an instrument flight rules (IFR) flight plan. The point of intended landing was Marsh Harbor International Airport, Abaco, Bahamas (MYAM). The crew selected runway 09 at MYAM for landing. At 17:45:30, the aircraft leveled off at 1,500 feet ASL on a heading of 096 degrees magnetic, with airspeed of 236 knots indicated (KIAS). The flaps were extended to 15 degrees at 17:47:18 with the aircraft level at 1,300 feet ASL, approximately 4.2 nm on the approach. The autopilot was disconnected at 17:47:26 with the aircraft level at 1,300 feet ASL, approximately 3.8 nm on the approach. Heading was 097 degrees magnetic and airspeed was 166 KIAS. The Landing Gear was extended and in the down and locked position by 17:48:01 as the aircraft descended through 730 feet ASL. At 17:48:03, the flaps were extended to landing flap 20 degrees with the aircraft approximately 1.9 nm from the runway on the approach. At 17:48:47, as the aircraft approached the threshold, the power levers were retarded (from 52 degrees) and the engine torques decreased from approximately 20%. Approximately one second later, the aircraft crossed the threshold at a radio altitude of 50 feet AGL on a heading 098 degrees magnetic and airspeed of 171 KIAS. The crew encountered rain showers and a reduction in visibility. The aircraft initially touched down at 17:49:02 with a recorded vertical load factor of +2.16G, approximately 14 seconds after crossing the threshold. There were no indications on the runway to indicate where the initial touchdown had occurred. Upon initial landing however, the aircraft bounced and became airborne, reaching a calculated maximum height of approximately 15 feet AGL. The aircraft bounced a second time at 17:49:07 with a recorded vertical load factor of +3.19* G. During this second bounce, the pitch attitude was 1.8 degrees nose down, heading 102 degrees magnetic and airspeed 106 KIAS. The aircraft made consecutive contact with the runway approximately three times. The third and final bounce occurred at 17:49:14 with a recorded vertical load factor of +3.66G*. During the third bounce, the pitch attitude was 2.2 degrees nose down, heading 099 degrees magnetic and airspeed 98 KIAS. As a result of the hard touchdown, damage was sustained to the right wing and right hand engine/propeller. The right hand engine parameters recorded a rapid loss of power with decreasing engine speed and torque, and subsequent propeller stoppage. The aircraft veered off to the right at approximate time of 17:49:20 on a heading of 131 degrees magnetic at a point approximately 6,044 feet from the threshold of runway 09. The recorded airspeed was 44 KIAS with the left hand engine torque at 26 % and the right hand engine torque at 0%. The aircraft came to a full stop at approximate time 17:49:25 on a heading of 231 degrees magnetic. When the aircraft came to a stop, the flight and cabin crew and twenty-one (21) passengers evacuated the aircraft. The evacuation was uneventful using the main entrance door. Due to the damage sustained by the right wing and engine, evacuation on the right side was not considered. The evacuation occurred during heavy rainfall. No injuries were reported as a result of the accident or evacuation process. The airplane sustained substantial damage as a result of the impact sequence. The elevation of the accident site was reported as approximately 10 feet Mean Sea Level (MSL). Instrument Meteorological Conditions (IMC) prevailed at the time of the accident. The cockpit voice recorder (CVR) uncovered that this crew used no crew resource management or adherence to company standard operating procedures. During the final seconds of the flight, there was complete confusion on the flight deck as to who was in control of the aircraft. After failure of the windshield wiper on the left side of the aircraft, the captain continued to maneuver the aircraft despite having no visual contact of the field due to heavy rain. Sterile Cockpit procedures were not adhered to by this crew as they continued with non-essential conversation throughout the flight regime from engine start up in KFLL up until the “before landing checklist” was requested prior to landing.
Probable cause:
Contributing factors:
- Inexperienced and undisciplined crew,
- Lack of crew resource management training,
- Failure to follow company standard operating procedures,
- Condition known as “get-home-itis” where attempt is made to continue a flight at any cost, even if it means putting aircraft and persons at risk in order to do so,
- Failure to retrieve, observe and respect weather conditions,
- Thunderstorms at the airfield.
Final Report:

Crash of a Cessna 402C II in Mayaguana: 3 killed

Date & Time: Apr 4, 2013 at 0100 LT
Type of aircraft:
Operator:
Registration:
C6-BGJ
Flight Type:
Survivors:
Yes
Schedule:
Nassau - Mayaguana
MSN:
402C-0106
YOM:
1979
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
On Thursday April 4, 2013 at approximately1:00AM DST (0500 UTC) a fixed wing, twin-engine, Cessna 402C aircraft Bahamas registration C6-BGJ, serial number 402C0106, crashed into obstacles (vehicles) while landing on Runway 06 at Mayaguana International Airport (MYMM), Abraham’s Bay, Mayaguana, Bahamas. The pilot in command stated that on April 3, 2013, he received a call at approximately 9:30PM from the Princess Margaret Hospital requesting emergency air ambulance services out of Mayaguana. The local police on the island was contacted to confirm lighting approval and availability in order to conduct the emergency flight. After confirming lighting arrangements with Nassau Air Traffic Control Services, and obtaining the necessary clearance, the pilot in command, along with a copilot and one passenger, (a nurse), proceeded with the flight to Mayaguana. The flight departed Lynden Pindling International Airport at approximately 1:30PM DST (0330UTC). The destination was Abraham’s Bay, Mayaguana, Bahamas. The pilot in command also reported “about 1 hour and 40 minutes later we arrived at Mayaguana Airport, leveled off at 1500 feet and about 4 miles left base Runway 06, we had the runway in sight via lighting from vehicles.” The crew continued with the landing procedures. The aircraft touch down approximately 300 feet from the threshold on runway 06, the pilot in command reported that prior to the nose gear making contact with the runway “the right wing hit an object (vehicle), causing the aircraft to veer out of control to the right eventually colliding with a second vehicle approximately 300 to 400 feet on the right side (southern) of Runway 06.” The impact of the right wing of the aircraft with the second vehicle, caused the right wing (outboard of the engine nacelle) and right fuel sealed wet wing tank to rupture releasing the aircraft fuel in that wing, which caused an explosion engulfing the vehicle in flames. The force of the impact with the second vehicle caused the right main gear to break away from the aircraft and it was flung ahead and to the left side of the runway approximately 200 feet from the point of impact with the truck. As the right main gear of the aircraft was no longer attached, the aircraft collapsed on its right side, slid onto the gravel south (right) of the runway and somewhere during this process, the nose gear also collapsed. The pilot immediately shut off the fuel valve of the aircraft and once the engines and the aircraft came to a stop, the three occupants evacuated the aircraft. The occupants of the aircraft did not sustain any visible injuries requiring medical attention or hospitalization. However, three (3) occupants of the second vehicle that was struck, were fatally injured. The airplane sustained substantial damages as a result of the impact and post impact crash sequence. The impact with the first vehicle occurred at approximately 427 feet from the threshold of runway 06 and at coordinates 28˚ 22’30”N and 073˚ 01’15’W. The flight was operated on an Instrument Flight Rules flight plan. Instrument Meteorological Conditions (night) prevailed at the time of the accident.
Probable cause:
Breakdown in communication during the planning and execution of an unapproved procedure has been determined to be the probable cause of this accident.
Other contributing factors:
- Use of an unapproved procedure to aid in a maneuver that was critical,
- Too many persons were planning the maneuver and not coordinating their actions,
- Failure of planners of the maneuver to verify whether participants were in the right position,
- Inexperienced persons used in the execution of a maneuver that was not approved,
- Vehicle parked to close to the side of the runway,
- Vehicle left with engine running while parked near the runway.
Final Report:

Crash of a Beechcraft A100 King Air in Deadmans Cay

Date & Time: Mar 9, 2012 at 1410 LT
Type of aircraft:
Operator:
Registration:
N70JL
Survivors:
Yes
Schedule:
Nassau - Deadmans Cay
MSN:
B-87
YOM:
1971
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine aircraft was operating a taxi flight from Nassau-Lynden Pindling Airport to Deadmans Cay, and departed Nassau around 1 pm. On approach to Deadmans Cay, the crew encountered technical problems and was unable to lower the gear. The captain decided to perform a belly landing. The aircraft skidded on runway for several yards then veered off runway before coming to rest. There was no fire. While all occupants escaped uninjured, the aircraft was damaged beyond repair.

Crash of a Beechcraft C-45 Expeditor off Nassau: 2 killed

Date & Time: Dec 14, 2010 at 1510 LT
Type of aircraft:
Operator:
Registration:
N38L
Flight Type:
Survivors:
No
Schedule:
Fort Lauderdale – Nassau
MSN:
6323
YOM:
1944
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
While approaching Nassau-Lynden Pindling Airport runway 27 in poor weather conditions (cold front), the twin engine aircraft crashed into the sea few km offshore. Some debris were found floating on water north of Nassau. Both pilots were killed.

Crash of a Cessna 402C in Nassau: 9 killed

Date & Time: Oct 5, 2010 at 1236 LT
Type of aircraft:
Operator:
Registration:
C6-NLH
Flight Phase:
Survivors:
No
Schedule:
Nassau – Cockburn Town
MSN:
402C-0458
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
12000
Captain / Total hours on type:
10000.00
Circumstances:
On October 5, 2010 about 1636 UTC / 12:36pm Eastern Daylight Time (EDT), C6-NLH a Cessna 402C aircraft registered to Lebocruise Air Limited and operated by Acklins Blue Air Charter/Nelson Hanna crashed into lake Killarney shortly after becoming airborne from runway 14 at Lynden Pindling International Airport, Nassau, New Providence, Bahamas. The airplane sustained substantial damages by impact forces. The pilot, copilot and seven (7) passengers aboard the airplane received fatal injuries. The aircraft was on a passenger carrying flight from Lynden Pindling Intl Airport (MYNN) to Cockburn Town, San Salvador, Bahamas (MYSM). The aircraft was on a visual flight rules flight plan. Visual meteorological conditions prevailed at the time of the accident. The official notification of the accident was made to the Manager of the Flight Standards Inspectorate at Lynden Pindling Intl Airport, Nassau, N. P., Bahamas shortly thereafter. The investigation began the same day at approximately 1655 UTC upon notification of the IIC. The investigation was conducted by the Bahamas Civil Aviation Department [BCAD], Inspector Delvin R. Major (Investigator-in-Charge) of the Air Accident Investigation and Prevention Unit (AAIPU), Management of BCAD and Flight Standards Inspectorate (FSI), Airworthiness Inspectors, Operations Inspectors, Human Factors and other administrative staff. Valuable assistance was also received from the National Transportation Safety Board (NTSB), the Federal Aviation Administration (FAA) and Manufacturers of the aircraft and engine components. Three (3) Air Operator Certificate (AOC) holders at the Domestic Section of Lynden Pindling Intl Airport stated that on the day of the accident flight; one of the victims of the accident aircraft approached each of them individually at different times, requesting a quote and their availability to conduct a charter flight to Cockburn Town, San Salvador, Bahamas. Each AOC holder reported that they declined to conduct the charter because by looking at the amount of luggage and other equipment that accompanied the passengers and the size of the passengers that wanted to travel, in their estimation the combined weight appeared to be in excess of the weight that their respective aircraft (Cessna 402C and Hawker Beechcraft B100) can accommodate. After the AOC holders declined to conduct the charter, sometime thereafter, the same individual that was arranging the flight with the previous AOC holders made contact with Nelson Hanna / Acklins Blue Air Charter where arrangements were made to conduct the charter flight. The aircraft type certificate allowed for the aircraft to be operated by one (1) pilot, but the fatal flight was operated by a crew of two (2) pilots (according to eyewitness reports). The aircraft actual weight and center of gravity was unknown. As far as could be determined, the takeoff weight exceeded the maximum weight allowed of 6,850 pounds by more than 500 pounds. This excess in weight also placed the center of gravity of the aircraft outside of the safe envelope / limits for flight allowed by the manufacturer. The flight crew was given instructions by ATC to taxi from the business aviation apron (Executive Flight Support) for a takeoff on Runway 14 at intersection Foxtrot. (Intersection Foxtrot is 2,000 feet beyond the threshold of Runway 14, with a take-off run available of 9,353 feet. (Runway 14 - 11,353 feet long by 150 feet wide, see Appendix 5.15). According to eyewitness reports, from the initiation of takeoff power up to the point when the aircraft lost control white smoke was observed trailing behind the left engine of the aircraft. Eyewitnesses also reported that the take off appeared normal with gear being retracted shortly after takeoff and the aircraft seemed to be struggling to climb. The aircraft was seen at a low height, turning in a left direction over the lake as if trying to return for a landing at the airport. The bank of the aircraft changed from shallow to very steep to almost perpendicular to the ground, gears were extended and almost immediately the aircraft lost control and nose dived into the lake inverted. It cart wheeled, coming to rest upright, approximately ¼ mile from the approach end of runway 27. The aircraft came to rest on an approximate heading of 210 degrees. Eyewitness also reported hearing the engine run for a few seconds after the aircraft made contact with the water of the lake. There were no reports from the pilot to ATC of an emergency or any abnormalities with the aircraft or its systems after takeoff. The flight plan form filed for this flight listed one (1) soul on board; however, there were 7 additional occupants including a “second pilot” discovered onboard the accident flight the day of the accident. The aircraft's recovery and search for luggage, equipment and additional victims commenced shortly after the accident. This effort however, was hampered by inclement weather, rough lake conditions and darkness. On October 6th, the day after the crash, aircraft recovery continued. Family members of an additional person believed to be on board, advised the authorities that there was a ninth (9th) person on board. Search to recover any additional bodies continued but search and recovery efforts proved fruitless. On October 7th, the second day after the crash, the body of the ninth (9th) victim was found in the marshes and recovered from the southwestern end of the lake in the vicinity of where the fatal crash occurred.
Probable cause:
The following findings were identified:
1. Acklins Blue Air Charter was advertising and operating as a Bahamas air taxi operator without having undergone the certification process in contravention of Bahamas Civil Aviation (Safety) Regulations Schedule 12.
2. The airplane was issued a Certificate of Airworthiness on May 19, 2010, by the Bahamas Flight Standards Inspectorate, and was being operated by Acklins Blue Air Charter.
3. The Cessna 402C aircraft is classified in the performance Group C. This requires rapid feathering of the propeller of a failed engine and the raising of flap and the landing gear in order to achieve maximum climb performance.
4. The airplane maintenance records were not located; therefore, no determination could be made whether the airplane was being maintained in accordance with Bahamas Civil Aviation Regulations.
5. The 12,000 hour pilot and second pilot were not qualified to operate in Bahamas commercial air taxi operations.
6. No determination could be made whether the pilot or second pilot had completed required training and had accomplished a satisfactory recurrent flight check of their flying ability as required by CASR Schedule 12 and 14 for aircraft operating in commercial air transportation as well as the stipulation by the insurance policy.
7. Post-accident weight and balance calculations indicate the airplane was being operated approximately 523 pounds over maximum certificated takeoff weight (6,850 lb)
8. The pilot was advised by an air traffic controller that white smoke was trailing the left engine during takeoff; the pilot did not declare an emergency or advise the controller of any engine failure or mechanical abnormality.
9. The airplane's left engine could not produce rated shaft horsepower during takeoff.
10. Several factors contributing to the degradation of the airplane's performance and its inability to maintain flight include the wind-milling propeller, the pilot's intentional initiation of a steep turn to return to the departure airport, and his intentional lowering of the landing gear during the turn to return.
11. While turning to return, the airplane stalled, pitched nose down, and impacted in a lake.
12. The search and rescue efforts were timely and appropriate; however, the lack of accurate information on the pilot submitted flight plan delayed recovery of all victims.
13. The left propeller was not feathered.
14. The No. 2 cylinder of the left engine failed due to fatigue that originated in the root of the cylinder head thread that was engaged with the first thread on the barrel.
15. Post-accident inspection of the cockpit revealed several switches for the right engine were secured; however, no determination could be made when the switches were placed / moved in those positions.
16. No evidence of failure of the airplane's structures or flight control system contributed to the accident.
17. Existing regulations did not require the aircraft to be fitted with flight recorders. The lack of any recorded data about the aircraft's performance or the flight crew conversations deprived the investigation team of essential factual information.
18. Current Civil Aviation Department personnel and budget resources may not be sufficient to ensure that the quality of surveillance for certified as well as uncertified air carrier operations will improve.
19. Airside access procedures are inadequate at Fixed Base Operators. Access to the secure airside occurring without any check of individuals to challenge whether they have a legitimate reason for accessing the secure airside. FBO door to access airside is not secured or locked continuously; persons observed walking in and out without being challenged.
20. Flight Plan Forms are being accepted and transmitted to ATC with incomplete information. This information is vital for search and rescue purposes.
21. Weather was not a factor in the accident.
22. ATC was not a factor in the accident.
23. Currently flight plans for private flights are only required for international operations.
24. The pilot was aware of discrepancy associated with the manifold pressure reading of the left engine prior to takeoff. This discrepancy was brought to his attention by a client from the flight immediately preceding the accident flight.
25. The exact center of gravity of the accident airplane could not be calculated accurately as no indication of what seat each passenger occupied in the airplane and no indication of where luggage or equipment were placed on the aircraft could be determined. However, due to the exceedance of weight limits the aircraft was already outside the allowable center of gravity envelope developed by the manufacturer.
26. The pilot had insufficient time to prepare for the approach to runway 27 before beginning the approach. The airplane pitched up quickly into a stall, after extension of gear, recovery before ground impact was unlikely once the stall began.
27. Post accident inspection did not reveal any mechanical evidence or problems with the right hand engine.
28. The pilot's decision to return to the airfield was reasonable. Once the aircraft began to lose height a return to the airfield became impractical and a forced landing in the direction of flight should have been attempted.
29. The right propeller was never recovered from the lake.
The following causal factors were identified:
1. The left engine suffered a mechanical failure of the #2 cylinder, and therefore could not produce rated shaft horsepower. No indication of total loss of power with the left engine reported.
2. Right Engine electrical and engine control switches were found in the “OFF” position, therefore the aircraft was incapable of climbing on the power of one engine alone.
3. The excess weight above the maximum weight allowed for takeoff may have been an important factor in the aircraft's inability to gain adequate altitude after takeoff.
4. The pilot secured the right engine which was mechanically capable of producing power resulting in a total loss of thrust. He then sometime thereafter initiated a steep turn with gear down and the left engine already not developing sufficient shaft horsepower to sustain lift.
5. The pilot attempted to return to the departure airfield but lost control of the aircraft during a turn to the left.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in South Bimini

Date & Time: Sep 19, 2010 at 1440 LT
Operator:
Registration:
N84859
Survivors:
Yes
Schedule:
South Bimini - Fort Lauderdale
MSN:
31-7305043
YOM:
1973
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On September 19, 2010, at 1440 eastern daylight time, a Piper PA31-350, N84859, registered to Spirit Air Inc, and operated by Pioneer Air Service was on initial climb out when the lower half of the main cabin door came open. The pilot reversed his course and returned to the departure airport, landing on runway 27. The right main landing gear tire blew out on the landing roll. The airplane went off the right side of the runway, struck a tree, caught fire and came to a complete stop. Visual meteorological conditions prevailed and an instrument flight plan was filed. The commercial pilot and five passengers were not injured and the airplane received substantial damage. The flight originated from Bimini Airport, South Bimini Island, Bahamas, at 1435, and was operated in accordance with 14 Code of Federal Regulations Part 135.