Crash of a Cessna 402C in Nassau: 9 killed

Date & Time: Oct 5, 2010 at 1236 LT
Type of aircraft:
Operator:
Registration:
C6-NLH
Flight Phase:
Survivors:
No
Schedule:
Nassau – Cockburn Town
MSN:
402C-0458
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
12000
Captain / Total hours on type:
10000.00
Circumstances:
On October 5, 2010 about 1636 UTC / 12:36pm Eastern Daylight Time (EDT), C6-NLH a Cessna 402C aircraft registered to Lebocruise Air Limited and operated by Acklins Blue Air Charter/Nelson Hanna crashed into lake Killarney shortly after becoming airborne from runway 14 at Lynden Pindling International Airport, Nassau, New Providence, Bahamas. The airplane sustained substantial damages by impact forces. The pilot, copilot and seven (7) passengers aboard the airplane received fatal injuries. The aircraft was on a passenger carrying flight from Lynden Pindling Intl Airport (MYNN) to Cockburn Town, San Salvador, Bahamas (MYSM). The aircraft was on a visual flight rules flight plan. Visual meteorological conditions prevailed at the time of the accident. The official notification of the accident was made to the Manager of the Flight Standards Inspectorate at Lynden Pindling Intl Airport, Nassau, N. P., Bahamas shortly thereafter. The investigation began the same day at approximately 1655 UTC upon notification of the IIC. The investigation was conducted by the Bahamas Civil Aviation Department [BCAD], Inspector Delvin R. Major (Investigator-in-Charge) of the Air Accident Investigation and Prevention Unit (AAIPU), Management of BCAD and Flight Standards Inspectorate (FSI), Airworthiness Inspectors, Operations Inspectors, Human Factors and other administrative staff. Valuable assistance was also received from the National Transportation Safety Board (NTSB), the Federal Aviation Administration (FAA) and Manufacturers of the aircraft and engine components. Three (3) Air Operator Certificate (AOC) holders at the Domestic Section of Lynden Pindling Intl Airport stated that on the day of the accident flight; one of the victims of the accident aircraft approached each of them individually at different times, requesting a quote and their availability to conduct a charter flight to Cockburn Town, San Salvador, Bahamas. Each AOC holder reported that they declined to conduct the charter because by looking at the amount of luggage and other equipment that accompanied the passengers and the size of the passengers that wanted to travel, in their estimation the combined weight appeared to be in excess of the weight that their respective aircraft (Cessna 402C and Hawker Beechcraft B100) can accommodate. After the AOC holders declined to conduct the charter, sometime thereafter, the same individual that was arranging the flight with the previous AOC holders made contact with Nelson Hanna / Acklins Blue Air Charter where arrangements were made to conduct the charter flight. The aircraft type certificate allowed for the aircraft to be operated by one (1) pilot, but the fatal flight was operated by a crew of two (2) pilots (according to eyewitness reports). The aircraft actual weight and center of gravity was unknown. As far as could be determined, the takeoff weight exceeded the maximum weight allowed of 6,850 pounds by more than 500 pounds. This excess in weight also placed the center of gravity of the aircraft outside of the safe envelope / limits for flight allowed by the manufacturer. The flight crew was given instructions by ATC to taxi from the business aviation apron (Executive Flight Support) for a takeoff on Runway 14 at intersection Foxtrot. (Intersection Foxtrot is 2,000 feet beyond the threshold of Runway 14, with a take-off run available of 9,353 feet. (Runway 14 - 11,353 feet long by 150 feet wide, see Appendix 5.15). According to eyewitness reports, from the initiation of takeoff power up to the point when the aircraft lost control white smoke was observed trailing behind the left engine of the aircraft. Eyewitnesses also reported that the take off appeared normal with gear being retracted shortly after takeoff and the aircraft seemed to be struggling to climb. The aircraft was seen at a low height, turning in a left direction over the lake as if trying to return for a landing at the airport. The bank of the aircraft changed from shallow to very steep to almost perpendicular to the ground, gears were extended and almost immediately the aircraft lost control and nose dived into the lake inverted. It cart wheeled, coming to rest upright, approximately ¼ mile from the approach end of runway 27. The aircraft came to rest on an approximate heading of 210 degrees. Eyewitness also reported hearing the engine run for a few seconds after the aircraft made contact with the water of the lake. There were no reports from the pilot to ATC of an emergency or any abnormalities with the aircraft or its systems after takeoff. The flight plan form filed for this flight listed one (1) soul on board; however, there were 7 additional occupants including a “second pilot” discovered onboard the accident flight the day of the accident. The aircraft's recovery and search for luggage, equipment and additional victims commenced shortly after the accident. This effort however, was hampered by inclement weather, rough lake conditions and darkness. On October 6th, the day after the crash, aircraft recovery continued. Family members of an additional person believed to be on board, advised the authorities that there was a ninth (9th) person on board. Search to recover any additional bodies continued but search and recovery efforts proved fruitless. On October 7th, the second day after the crash, the body of the ninth (9th) victim was found in the marshes and recovered from the southwestern end of the lake in the vicinity of where the fatal crash occurred.
Probable cause:
The following findings were identified:
1. Acklins Blue Air Charter was advertising and operating as a Bahamas air taxi operator without having undergone the certification process in contravention of Bahamas Civil Aviation (Safety) Regulations Schedule 12.
2. The airplane was issued a Certificate of Airworthiness on May 19, 2010, by the Bahamas Flight Standards Inspectorate, and was being operated by Acklins Blue Air Charter.
3. The Cessna 402C aircraft is classified in the performance Group C. This requires rapid feathering of the propeller of a failed engine and the raising of flap and the landing gear in order to achieve maximum climb performance.
4. The airplane maintenance records were not located; therefore, no determination could be made whether the airplane was being maintained in accordance with Bahamas Civil Aviation Regulations.
5. The 12,000 hour pilot and second pilot were not qualified to operate in Bahamas commercial air taxi operations.
6. No determination could be made whether the pilot or second pilot had completed required training and had accomplished a satisfactory recurrent flight check of their flying ability as required by CASR Schedule 12 and 14 for aircraft operating in commercial air transportation as well as the stipulation by the insurance policy.
7. Post-accident weight and balance calculations indicate the airplane was being operated approximately 523 pounds over maximum certificated takeoff weight (6,850 lb)
8. The pilot was advised by an air traffic controller that white smoke was trailing the left engine during takeoff; the pilot did not declare an emergency or advise the controller of any engine failure or mechanical abnormality.
9. The airplane's left engine could not produce rated shaft horsepower during takeoff.
10. Several factors contributing to the degradation of the airplane's performance and its inability to maintain flight include the wind-milling propeller, the pilot's intentional initiation of a steep turn to return to the departure airport, and his intentional lowering of the landing gear during the turn to return.
11. While turning to return, the airplane stalled, pitched nose down, and impacted in a lake.
12. The search and rescue efforts were timely and appropriate; however, the lack of accurate information on the pilot submitted flight plan delayed recovery of all victims.
13. The left propeller was not feathered.
14. The No. 2 cylinder of the left engine failed due to fatigue that originated in the root of the cylinder head thread that was engaged with the first thread on the barrel.
15. Post-accident inspection of the cockpit revealed several switches for the right engine were secured; however, no determination could be made when the switches were placed / moved in those positions.
16. No evidence of failure of the airplane's structures or flight control system contributed to the accident.
17. Existing regulations did not require the aircraft to be fitted with flight recorders. The lack of any recorded data about the aircraft's performance or the flight crew conversations deprived the investigation team of essential factual information.
18. Current Civil Aviation Department personnel and budget resources may not be sufficient to ensure that the quality of surveillance for certified as well as uncertified air carrier operations will improve.
19. Airside access procedures are inadequate at Fixed Base Operators. Access to the secure airside occurring without any check of individuals to challenge whether they have a legitimate reason for accessing the secure airside. FBO door to access airside is not secured or locked continuously; persons observed walking in and out without being challenged.
20. Flight Plan Forms are being accepted and transmitted to ATC with incomplete information. This information is vital for search and rescue purposes.
21. Weather was not a factor in the accident.
22. ATC was not a factor in the accident.
23. Currently flight plans for private flights are only required for international operations.
24. The pilot was aware of discrepancy associated with the manifold pressure reading of the left engine prior to takeoff. This discrepancy was brought to his attention by a client from the flight immediately preceding the accident flight.
25. The exact center of gravity of the accident airplane could not be calculated accurately as no indication of what seat each passenger occupied in the airplane and no indication of where luggage or equipment were placed on the aircraft could be determined. However, due to the exceedance of weight limits the aircraft was already outside the allowable center of gravity envelope developed by the manufacturer.
26. The pilot had insufficient time to prepare for the approach to runway 27 before beginning the approach. The airplane pitched up quickly into a stall, after extension of gear, recovery before ground impact was unlikely once the stall began.
27. Post accident inspection did not reveal any mechanical evidence or problems with the right hand engine.
28. The pilot's decision to return to the airfield was reasonable. Once the aircraft began to lose height a return to the airfield became impractical and a forced landing in the direction of flight should have been attempted.
29. The right propeller was never recovered from the lake.
The following causal factors were identified:
1. The left engine suffered a mechanical failure of the #2 cylinder, and therefore could not produce rated shaft horsepower. No indication of total loss of power with the left engine reported.
2. Right Engine electrical and engine control switches were found in the “OFF” position, therefore the aircraft was incapable of climbing on the power of one engine alone.
3. The excess weight above the maximum weight allowed for takeoff may have been an important factor in the aircraft's inability to gain adequate altitude after takeoff.
4. The pilot secured the right engine which was mechanically capable of producing power resulting in a total loss of thrust. He then sometime thereafter initiated a steep turn with gear down and the left engine already not developing sufficient shaft horsepower to sustain lift.
5. The pilot attempted to return to the departure airfield but lost control of the aircraft during a turn to the left.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in South Bimini

Date & Time: Sep 19, 2010 at 1440 LT
Operator:
Registration:
N84859
Survivors:
Yes
Schedule:
South Bimini - Fort Lauderdale
MSN:
31-7305043
YOM:
1973
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On September 19, 2010, at 1440 eastern daylight time, a Piper PA31-350, N84859, registered to Spirit Air Inc, and operated by Pioneer Air Service was on initial climb out when the lower half of the main cabin door came open. The pilot reversed his course and returned to the departure airport, landing on runway 27. The right main landing gear tire blew out on the landing roll. The airplane went off the right side of the runway, struck a tree, caught fire and came to a complete stop. Visual meteorological conditions prevailed and an instrument flight plan was filed. The commercial pilot and five passengers were not injured and the airplane received substantial damage. The flight originated from Bimini Airport, South Bimini Island, Bahamas, at 1435, and was operated in accordance with 14 Code of Federal Regulations Part 135.

Ground accident of a Saab 340A in Nassau

Date & Time: Jan 7, 2010 at 1145 LT
Type of aircraft:
Operator:
Registration:
C6-SBE
Flight Phase:
Survivors:
Yes
Schedule:
Nassau - Marsh Harbour
MSN:
99
YOM:
1987
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Two crew took place in the cockpit to prepare the aircraft for a scheduled commercial service to Marsh Harbour. In unknown circumstances, all three landing gear retracted, causing the aircraft to fall on the ground. Both occupants were uninjured while the aircraft was damaged beyond repair. It is unknown if the retraction of the undercarriage was the consequence of a mechanical failure or a mishandling from the crew.

Crash of a Dassault Falcon 20D in Matthew Town: 2 killed

Date & Time: Dec 17, 2009 at 1930 LT
Type of aircraft:
Operator:
Registration:
N28RK
Flight Type:
Survivors:
No
Schedule:
Oranjestad – La Isabela – Fort Lauderdale
MSN:
206
YOM:
1969
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
26525
Copilot / Total flying hours:
4800
Circumstances:
On December 17, 2009 at approximately 7:30 pm local (2330UTC), N28RK a Dassault Sud, Falcon Fan Jet, Mystere 20, Series D aircraft which departed Joaquin Balaguer Int’l Airport (MDJB) in the Dominican Republic, for Ft Lauderdale Executive Airport, (FXE) Ft Lauderdale, Florida, USA, crashed in a remote area of Matthew Town, Great Inagua, Bahamas. The accident occurred approximately 11.5 miles due east of Great Inagua International Airport at coordinates N 20˚ 58’ 30” latitude and W 073˚ 40’ 00.7” longitude. The aircraft made contact with the terrain on a heading of approximately 105 degrees magnetic. The accident occurred in area that was not accessible by land and the investigation team had to be airlifted by helicopter to the site. Witnesses on the island of Great Inagua reported hearing a loud bang that rattled doors and windows of their homes, but they did not report seeing the aircraft fall from the sky. The aircraft was under the command of Captain Harold Roy Mangels and First Office Freddy Castro. The aircraft reportedly departed Aruba, in the Netherland Antilles and made a fuel stop at Dr. Joaquin Balaguer Int’l Airport, Santo Domingo in the Dominican Republic. The final destination filed by the crew was Ft. Lauderdale Executive Airport, Ft Lauderdale Florida. The accident occurred approximately 6 mile off the filed flight path. ATC records and instructions were for the aircraft N28RK to maintain 28,000 ft (FL280). The aircraft transponder was reported as inoperative. It begun a rapid descent, with no report of an emergency declared or mayday call out. Investigation of the crash site indicates the airplane made contact with the terrain at a high rate of speed and approximately a 45 degree angle. The aircraft was destroyed on impact. The crew of a United States Coast Guard helicopter was on a training mission in the Great Inagua area at the time of the accident. They reported hearing a loud bang and noticed a huge explosion and fireball emanating from the ground in an area close to their location. The crew of the US Coast Guard helicopter reported that they did not see any in-flight fire prior to the fireball that they saw. The post impact fire engulfed approximately five (5) acres of trees and brush in the National Wildlife Refuge at Great Inagua. The coast guard helicopter crew stated that they discontinued their training mission and went to the site to investigate. Upon arrival at the site the crew reported that they lowered rescue personnel to the ground to investigate and search for survivors, but, due to the heat and extent of the fire on the ground, they had to discontinue the search. They reported the accident to authorities at Great Inagua. This information was further passed along to the National Transportation Safety Board who alerted the accident investigation unit of the Bahamas Civil Aviation Department. Night time conditions prevailed at the time of the accident. The crew of the aircraft received fatal injuries. A search of the area discovered no distinguishable human remains. Approximately less than 1% of what is believed to be possible human flesh / internal body parts were recovered. In addition clothing (piece of a pant with belt buckle fastened) was recovered, which possibly may have been worn by a member of the crew at the time of the accident. All recovered remains and clothing retrieved were gathered by officers of the Royal Bahamas Police Force that accompanied the investigation team and sent to the Forensic Science Laboratory at the Royal Bahamas Police Force, Nassau Bahamas for DNA analysis and possible identification. The aircraft broke into many pieces after contact with the terrain. Debris was spread over a large area of rough terrain. What remained of the aircraft post impact was either not found or possibly further destroyed by the post impact fire. The “four corners” of the airplane were confirmed in the area downstream of where the initial ground impact occurred. However, engine cowling parts were found prior to the point of initial ground impact. This may suggest an aircraft over-speed condition prior to ground impact. Less than 10% of the aircraft was recovered. An explosion occurred when N28RK made contact with the terrain. A post impact fire ensued. Approximately 5 acres of the national park was destroyed by the fire. Parts of the aircraft including personal effect, aircraft parts and furnishing, seat and seat cushions were also destroyed in the post impact fire.
Probable cause:
The probable cause of this accident has been determined as loss of control. Insufficient wreckage of the aircraft were recovered to make a conclusive determination as to the cause of the accident.
Final Report:

Crash of a Rockwell Shrike Commander 500S off Alice Town

Date & Time: Jun 9, 2008 at 1401 LT
Operator:
Registration:
N501AP
Flight Type:
Survivors:
Yes
Schedule:
Nassau – Fort Lauderdale
MSN:
500-3224
YOM:
1974
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On June 9, 2008, about 1401 eastern daylight time, an Aero Commander 500S, N501AP, registered to and operated by Gramar 500, Inc., experienced a loss of engine power in both engines and was ditched in the Atlantic Ocean about 1/2 mile south of North Bimini, Bahamas. Visual meteorological conditions prevailed in the area and a visual flight rules flight plan was filed for the 14 Code of Federal Regulations (CFR) Part 91 personal flight from Nassau International Airport (MYNN), Nassau, Bahamas, to Ft. Lauderdale Executive Airport (FXE), Ft. Lauderdale, Florida. The airplane was destroyed due to salt water immersion, and the airline transport rated pilot, the sole occupant, was not injured. The pilot stated that when the flight was past Bimini, the right engine started running rough and losing power. He turned southeast to enter a left base for runway 09 at South Bimini Airport, and the left engine also began to run rough and lost power. The pilot ditched the aircraft, evacuated into a life raft, and was rescued by a pleasure boater. The pilot also stated that 25 gallons of fuel were added while at MYNN, for a total fuel supply of 90 gallons. Both engines were test run 8 days after the accident using a test propeller. Both engines ran to near maximum RPM. One magneto from each engine was replaced prior to the test run.

Crash of a Cessna 208B Grand Caravan off Chub Cay

Date & Time: Dec 20, 2007 at 1700 LT
Type of aircraft:
Operator:
Registration:
N954PA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
La Isabela - West Palm Beach
MSN:
208B-0556
YOM:
1996
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
7390
Circumstances:
On December 20, 2007 at approximately 1630EST, N954PA a Cessna 208B Caravan aircraft, owned and operated by Agape Flight Inc [United States FAR Part 91 Operator] enroute from Santo Domingo, Dominican Republic to West Palm Beach, Florida incurred sudden engine stoppage. At the time N954PA was flying at 12,000 ft. The aircraft was diverted to the nearest airport but was unable to glide the required distance and landed 30 nautical miles (NM) West North West (WNW) of Chub Cay. There were 2 crew members on board the aircraft. No injuries were reported by the crew. The aircraft is submerged in approximately eighteen to twenty feet of water, with the aircraft tail being visible at low tide. Both crews were qualified in accordance with the United States Code of Federal Regulations.
Probable cause:
The engine power loss was caused by a loss of fuel pressure resulting from a loss of drive to the fuel pump. The drive loss was caused by worn and cracked splines on the drive shaft. The damage to the splines of the fuel pump drive shaft was likely caused by cracking below the chrome plating covering the splines, which deteriorated into spalling and wear leading to decouple between the
accessories gearbox and fuel pump. The remaining engine damage was caused by exposure to salt water.
Contributing factors:
Maintenance changed the fuel control unit and coupling shaft on July 17, 2007 due to original FCU failing emergency power checks. However there is no record to show whether or not the splines of fuel pump drive shaft inspection as per P&WC’s applicable Maintenance Manual has been accomplished.
Final Report:

Crash of a Britten-Norman BN-2A Islander in Nassau

Date & Time: Jun 27, 2007 at 1721 LT
Type of aircraft:
Operator:
Registration:
N133RS
Flight Type:
Survivors:
Yes
Schedule:
Little White Cay - Nassau
MSN:
606
YOM:
1970
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
9010
Circumstances:
On June 27, 2007 about 1721 eastern daylight time (2121Z) a Pilatus Britten Norman Islander, N133RS registered to and owned by FYP LTP, and operated by Golden Wings Charter, Windsor Field, Nassau, Bahamas, had crashed short of runway 14. Just prior to crashing, approximately 1718 eastern daylight time (2118Z), the pilot of aircraft N133RS reported the left engine had failed. At approximately 1721 eastern daylight time (2121Z), the pilot reported he was unable to make runway 14 and crashed approximately ½ mile short of Runway 14. The State of Manufacture and State of Design along with the State of Registry were notified of the accident on June 28, 2007. They were invited to participate in the investigation in accordance with Annex 13 and CASR 2001 Schedule 18. Visual Meteorological Conditions prevailed at the time of the accident. The flight originated from Lynden Pindling International Airport, Nassau [MYNN] to Little Whale Cay, Berry Island [MYBX] and returned to Nassau [MYNN], the incident leg. The airplane sustained substantial damage. The Pilot was the only person aboard the aircraft. The Pilot in Command holds a current United States Commercial Pilot Rating. No serious injuries or fatalities were reported.
Probable cause:
The Flight Standards Inspectorate determined that the probable cause of this accident was Propulsion System Malfunction due to fuel exhaustion of the left engine, followed by inappropriate crew response (fuel mismanagement).
Contributing Factors:
- Pilot’s unfamiliarity with aircraft fuel system.
- Pilot’s limited command experience. (He was a new hire, low time pilot)
- Pilot’s failure to conduct a proper preflight inspection of his aircraft. (did not visually check fuel tanks despite knowing that the gauges were faulty)
- Pilot’s complacency with documentation of defects. (Pilot never advised maintenance or management that the gauges were faulty)
- Pilot’s reliance on indications that he admitted were erroneous.
- Pilot’s lack of situational awareness.
- Pilot’s failure to recognize that his problem was fuel exhaustion and not engine failure and neglected to use cross-feed procedure.
Final Report:

Crash of a De Havilland Dash-8-301 in Governor's Harbour

Date & Time: Apr 20, 2007 at 1708 LT
Operator:
Registration:
C6-BFN
Survivors:
Yes
Schedule:
Nassau – Governor’s Harbour
MSN:
159
YOM:
1989
Flight number:
UP353
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
48
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
29570
Aircraft flight cycles:
52653
Circumstances:
Following an uneventful flight (service UP353) from Nassau, the crew started the descent to Governor’s Harbour. After landing on runway 15, the left main gear collapsed. The aircraft slid for few dozen metres then turn slightly to the left and came to rest on the main runway. All 51 occupants evacuated safely, nevertheless, few passengers suffered minor injuries. The aircraft was damaged beyond repair.
Probable cause:
The probable Cause has been determined as an over-center Torque Link condition that culminated in a single cycle failure of the cylinder. The over center torque links condition occur as a result of the over extension of the shock strut.
Possible Contributory factors to the over extension of the shock strut includes:
Possible Cause for Loss of Damping
• The failure to install the dampening ring when the landing gear was assembled.
• Improper servicing of the landing gear shock strut with Mil-H-5606 hydraulic fluid plus nitrogen during initial assembly.
• Improper servicing of landing gear shock strut during line maintenance and inadequate post servicing follow up per AMM Chapter 12. See attached report Appendix A-30 From Bombardier
• Under-serviced shock strut (low oil volume)
• A broken damper ring
• No damper ring
• Disengaged damper ring.
Final Report:

Crash of a Piper PA-46-310P Malibu off Bird Cay: 2 killed

Date & Time: Apr 10, 2007 at 1703 LT
Registration:
N444JH
Flight Phase:
Survivors:
No
Schedule:
Fort Lauderdale – Nassau
MSN:
46-8608014
YOM:
1986
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
9818
Aircraft flight hours:
6912
Circumstances:
The pilot obtained two data user access terminal service (DUATS) preflight weather briefings for the intended flight from the U.S. to Nassau, Bahamas; the briefings included information that thunderstorms were forecasted. The pilot did not request a weather briefing with DUATS or Lockheed Martin flight service station before departure on the return accident flight. Although there was no way to tell whether he received a preflight weather briefing with Nassau Flight Service Station before departure on the accident flight, thunderstorms with associated severe turbulence were forecasted for the accident area well in advance of the aircraft's departure, and would have been available had the pilot requested/obtained a preflight weather briefing. After takeoff, and while in contact with Nassau terminal radar approach control, which had inoperative primary radar, the flight climbed to approximately 8,000 feet mean sea level and proceeded on a northwesterly heading with little deviation. The airplane, which was equipped with color weather radar and a stormscope, penetrated level 6 radar returns with numerous lightning strikes in the area, and began a steep descent. Prior to that there was no request by the pilot to air traffic control for weather avoidance assistance or weather deviation. Radar and radio communications were lost, and the wreckage and occupants were not recovered.
Probable cause:
The pilot's poor in-flight weather evaluation, which resulted in flight into a level 6 thunderstorm.
Final Report:

Crash of a De Havilland DHC-3 Otter off Flamingo Bay

Date & Time: Dec 9, 2006
Type of aircraft:
Registration:
N335AK
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
263
YOM:
1958
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Flamingo Bay, the single engine aircraft crashed in the sea few dozen metres offshore. The pilot was injured and the aircraft was destroyed.