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Crash of a Cessna 501 Citation I in Birmingham

Date & Time: Nov 19, 2010 at 1535 LT
Type of aircraft:
Registration:
G-VUEM
Flight Type:
Survivors:
Yes
Schedule:
Belfast - Birmingham
MSN:
501-0178
YOM:
1981
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7200
Captain / Total hours on type:
3000.00
Copilot / Total flying hours:
1785
Copilot / Total hours on type:
735
Circumstances:
The flight crew reported for duty at Liverpool Airport at 0845 hrs. Their original task was to fly to Belfast City Airport, collect a transplant organ, and take it to Cambridge Airport. However, on their arrival at Belfast the transfer was no longer required, so they were given a new task to fly to Belfast Aldergrove Airport and collect an organ to carry to Birmingham Airport. The aircraft departed Belfast Aldergrove at 1450 hrs with the co-pilot as pilot flying. The flight was uneventful and the aircraft was given a radar vector to intercept the ILS for a straight-in approach to Runway 15 at Birmingham. The Runway 15 ILS course is 149°M. The autopilot was engaged and the aircraft was flying on a track of 135°M, 13 nm from the touchdown zone and at a groundspeed of 254 kt, when it crossed the localiser centreline. The aircraft then turned right onto a corrective track but once again passed through the localiser course. Further corrections were made and the aircraft passed through the localiser once more before becoming established at 5 nm. The co-pilot later reported that, because the autopilot was not capturing the localiser, he had disconnected it and flown the approach manually. When the aircraft was at 10 nm, the radar controller broadcast a message advising of the presence of a fog bank on final approach and giving RVRs of 1,400 m at touchdown and in excess of 1,500 m at both the mid-point and stop end. The airfield was sighted by the commander during the approach but not by the co-pilot. A handover to the tower frequency was made at around 8 nm. When the aircraft was at 6 nm, landing clearance was given and acknowledged. The tower controller then advised the aircraft that there was a fog bank over the airfield boundary, together with the information that the touchdown RVR was 1,400 m. The commander responded, saying: “WE’VE GOT ONE END OF THE RUNWAY”. The aircraft was correctly on the localiser and the glideslope at 4 nm. The Decision Altitude (DA) of 503 feet amsl (200 feet aal) for the approach was written on a bug card mounted centrally above the glare shield. Both pilots recollected that the Standard Operating Procedure (SOP) calls of “500 above” and “100 above” DA were made by the commander. However, neither pilot could recall a call of ‘decision’ or ‘go-around’ being made. At between 1.1 nm and 0.9 nm, and 400 feet to 300 feet aal, the aircraft turned slightly to the right, onto a track of 152°M. This track was maintained until the aircraft struck the glideslope antenna to the right of the runway some 30 seconds later (see Figure 3, page 11). The aircraft came to rest in an upright position on the grass with a fire on the left side. The co-pilot evacuated through the main cabin door, which is located on the left side of the fuselage, and suffered flash burns as he passed through the fire. The commander was trapped in the cockpit for a time.
Probable cause:
The co-pilot’s task of flying the approach would have become increasingly demanding as the aircraft descended and it is probable that his attention was fully absorbed by this. This was confirmed by his erroneous perception that the aircraft was in IMC from below 2,000 feet amsl. The co-pilot reported that during the final stages of the approach, when he noticed he had lost the localiser indication, he had asked the commander whether he should go around. The response he reported he heard of “no, go left” was not what he had expected, and may correspond to the time from which no further control inputs were made. The commander could not recall having given any instructions to the co-pilot after the ‘100 feet above’ call. It is likely that the crew commenced the approach with an expectation that it would be completed visually. However, the weather conditions were unusual and the aircraft entered IMC unexpectedly, late in the approach. As an aircraft gets closer to a runway the localiser and glideslope indications become increasingly sensitive and small corrections have a relatively large effect. The task for the flying pilot becomes more demanding and the role of the monitoring pilot has greater significance. A successful outcome relies on effective crew co-ordination, based on clear SOPs. The monitoring of this approach broke down in the latter stages and the crucial ‘decision’ call was missed, which led to the aircraft’s descent below minima.
Final Report:

Crash of a Short 360-300 off Edinburgh: 2 killed

Date & Time: Feb 27, 2001 at 1731 LT
Type of aircraft:
Operator:
Registration:
G-BNMT
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Edinburgh – Belfast
MSN:
3723
YOM:
1987
Flight number:
LOG670A
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
13569
Captain / Total hours on type:
972.00
Copilot / Total flying hours:
438
Copilot / Total hours on type:
72
Circumstances:
The aircraft landed at Edinburgh Airport, Scotland, at 00:03 and was parked there on Stand 31 in conditions including light and moderate snowfall. After preparation for a Royal Mail charter flight 670A to Belfast, start clearance was given at 15:03. At 15:12 hrs the crew advised ATC they were shutting down due to a technical problem. The crew then advised their company that a generator would not come on line. An avionics technician carried out diagnosis during which both engines were ground-run twice. No fault was found and the flight crew requested taxi clearance at 17:10. A normal take off from runway 06 was carried out followed by a reduction to climb power at 1,200 feet amsl. At 2,200 feet amsl the aircraft anti-icing systems were selected on. Three seconds later the torque on each engine reduced rapidly to zero. A MAYDAY call was made by the crew advising that they had experienced a double engine failure. The aircraft was ditched in the Firth of Forth estuary some 100 meters from the shoreline near Granton Harbour. Both pilots were killed. Weather reported just before the accident with a temperature of +2°C, dewpoint of -3°C, visibility of more then 10 km, broken clouds at 4500 feet and cover at 8000 feet.
Probable cause:
The following causal factors were identified:
1) The operator did not have an established practical procedure for flight crews to fit engine intake blanks (‘bungs’) in adverse weather conditions. This meant that the advice contained in the aircraft manufacturer’s Maintenance Manual ‘Freezing weather-precautions’ was not complied with. Furthermore intake blanks were not provided on the aircraft nor were any readily available at Edinburgh Airport.
2) A significant amount of snow almost certainly entered into the engine air intakes as a result of the aircraft being parked heading directly into strong surface winds during conditions of light to moderate snowfall overnight.
3) The flow characteristics of the engine intake system most probably allowed large volumes of snow, ice or slush to accumulate in areas where it would not have been readily visible to the crew during a normal pre-flight inspection.
4) At some stage, probably after engine ground running began, the deposits of snow, ice or slush almost certainly migrated from the plenum chambers down to the region of the intake anti-ice vanes. Conditions in the intakes prior to takeoff are considered to have caused re-freezing of the contaminant, allowing a significant proportion to remain in a state which precluded its ingestion into the engines during taxi, takeoff and initial climb.
5) Movement of the intake anti-icing vanes, acting in conjunction with the presence of snow, ice or slush in the intake systems, altered the engine intake air flow conditions and resulted in the near simultaneous flameout of both engines.
6) The standard operating procedure of selecting both intake anti-ice vane switches simultaneously, rather than sequentially with a time interval, eliminated a valuable means of protection against a simultaneous double engine flameout.
Final Report:

Crash of a Boeing 737-4Y0 in East Midlands: 47 killed

Date & Time: Jan 8, 1989 at 2025 LT
Type of aircraft:
Operator:
Registration:
G-OBME
Survivors:
Yes
Schedule:
London - Belfast
MSN:
23867
YOM:
1988
Flight number:
BD092
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
118
Pax fatalities:
Other fatalities:
Total fatalities:
47
Captain / Total flying hours:
13176
Captain / Total hours on type:
763.00
Copilot / Total flying hours:
3290
Copilot / Total hours on type:
192
Aircraft flight hours:
521
Circumstances:
British Midland Airways Flight BD092 took off from London-Heathrow Airport at 1952LT on a flight to Belfast, Northern Ireland. Some 13 minutes later, while climbing through FL283, moderate to severe vibration was felt, accompanied by a smell of fire in the cockpit. The outer panel of one of the n°1 engine fan blades detached, causing compressor stalls and airframe shuddering. Believing the n°2 engine had been damaged the crew throttled it back. The shuddering stopped and the n°2 engine was shut down. The crew then decided to divert to East Midlands Airport. The flight was cleared for an approach to runway 27. At 900 feet, 2.4 nm from the runway threshold, the n°1 engine power suddenly suffered a decrease in power. As the speed fell below 125 knots, the stick shaker activated and the aircraft struck trees at a speed of 115 knots. The aircraft continued and impacted the western carriageway of the M1 motorway 10 meters lower and came to rest against a wooded embankment, 1'023 meters short of runway threshold. 47 passengers were killed while all other occupants were injured, some of them seriously.
Probable cause:
The operating crew shut down the n°2 engine after a fan blade had fractured in the n°1 engine. This engine subsequently suffered a major thrust loss due to secondary fan damage after power had been increased during the final approach to land.
The following factors contributed to the incorrect response of the flight crew:
1. The combination of heavy engine vibration, noise, shuddering and an associated smell of fire were outside their training and experience;
2. They reacted to the initial engine problem prematurely and in a way that was contrary to their training;
3. They did not assimilate the indications on the engine instrument display before they throttled back the n°2 engine;
4. As the n°2 engine was throttled back, the noise and shuddering associated with the surging of the n°1 engine ceased, persuading them that they had correctly identified the defective engine;
5. They were not informed of the flames which had emanated from the n°1 engine and which had been observed by many on board, including 3 cabin attendants in the aft cabin.
Final Report:

Crash of an Avro 696 Shackleton MR.3 in Inverness

Date & Time: Jan 10, 1964
Type of aircraft:
Operator:
Registration:
XF710
Flight Type:
Survivors:
Yes
Schedule:
Kinloss – Belfast
YOM:
1959
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Few minutes after takeoff from RAF Kinloss, en route to Belfast, the crew informed ATC that the engin number three oversped and caught fire. Shortly later, the engine detached and the crew was forced to shut down the engine number four. In such conditions, the crew decided to divert to Inverness Airport but out of control, the airplane lost height and crashed in a field located in Culloden Moor, about 4 miles southwest of the airport. People taking part to an open air party were able to evacuate all five crew members who were injured. The aircraft was destroyed.
Crew:
F/Lt J. Gladstone, pilot,
F/O Jim Lee, copilot,
John Mepham, flight engineer,
Jamie Hamilton,
John R. Hudson.
Probable cause:
Engine fire.

Crash of an Avro 19/2 in Leeds

Date & Time: Apr 9, 1963
Type of aircraft:
Operator:
Registration:
G-ALXH
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Leeds-Bradford - Belfast
MSN:
1731
YOM:
1950
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after take-off from Leeds-Bradford Airport, for a positioning flight to Belfast, the cabin filled with smoke which issued from the camera hatch near the starboard wing root. The aircraft was, by this time, about 800 feet above the downwind end of the runway from which it had taken off, and the pilot closed the throttles and began a descending turn to port. At about 400 feet, power was applied for a base leg and short final but, despite full throttle, the airspeed began to fall. Because he found it necessary to apply an increasing amount of left rudder, the pilot concluded that the starboard engine had failed and he decided to make a forced landing in a field outside the airport. During the approach, the aircraft was dived, and turned, in an attempt to avoid HT wires, but it collided with a port and struck the ground heavily. The airplane was damaged beyond repair and all three occupants escaped uninjured.
Source: https://aviation-safety.net/wikibase/wiki.php?id=24985

Crash of an Avro 652 Anson C.19 in Belfast

Date & Time: Sep 17, 1956
Type of aircraft:
Operator:
Registration:
VS589
Flight Type:
Survivors:
Yes
Schedule:
Belfast - Belfast
Location:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot was performing a local training sortie at Belfast City Airport and was completing a single engine approach when he was forced to attempt an emergency landing for unknown reason. The aircraft crash landed in a field located south of Castlereagh and was damaged beyond repair. The pilot J. Fothergill, a civilian working for Short Brothers and Harland, was uninjured.

Crash of a Miles M.57 Aerovan IV off Southport

Date & Time: Mar 25, 1948
Type of aircraft:
Registration:
G-AJKJ
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Belfast – Liverpool
MSN:
6406
YOM:
1947
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While flying over the Irish Sea, enroute from Belfast to Liverpool, the pilot was forced to ditch the aircraft off Southport. He was quickly rescued while the aircraft sank and was lost.

Crash of a Consolidated B-24J-1-FO Liberator in Ballyshannon: 2 killed

Date & Time: Jun 19, 1944 at 0920 LT
Operator:
Registration:
42-50721
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Goose Bay – Belfast
MSN:
2606
Country:
Region:
Crew on board:
10
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was performing a ferry flight from Goose Bay to Belfast-Nutts Corner Airport. While approaching Ireland, the navigator informed the captain that the fuel reserve seems to be insufficient to reach the destination while the radio operator was unable to contact ground. The captain was approaching St Angelo but the airfield was closed due to fog and clouds so he decided to fly back to find a clear zone near Ballyshannon for an emergency landing. After touchdown, the bomber hit a concrete wall and was wrecked. Eight crew members were injured while two others were killed.
Crew:
2/Lt Arthur H. Dittmer,
2/Lt Marvin J. Reddick,
2/Lt Arnold A. H. Grueber,
2/Lt Wayne R. Davis,
S/Sgt Lester M. Clark,
Sgt Edward J. Friedl,
Sgt Carlos F. Maestas, †
Sgt George H. Smith,
Cpl James O. E. Harvey,
Cpl Riley W. Cannon. †
Source: http://www.csn.ul.ie/~dan/war/42-50721.htm
Probable cause:
Forced landing due to fuel exhaustion.

Crash of an Avro 504N into the Irish Sea: 1 killed

Date & Time: Jan 21, 1937
Type of aircraft:
Operator:
Registration:
G-AEIJ
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Belfast – Liverpool
MSN:
J8507
YOM:
1936
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The engine failed in flight, forcing the crew to ditch the aircraft into the Irish Sea. The crew from a ship named 'Corrib' arrived on scene and was able to evacuate the mechanic uninjured while the pilot was killed when the aircraft sank. His body was never recovered.
Probable cause:
Engine failure.