Crash of a Boeing 727-100 off Chicago: 30 killed

Date & Time: Aug 16, 1965 at 2120 LT
Type of aircraft:
Operator:
Registration:
N7036U
Survivors:
No
Schedule:
New York – Chicago
MSN:
18328
YOM:
1965
Flight number:
UA389
Crew on board:
6
Crew fatalities:
Pax on board:
24
Pax fatalities:
Other fatalities:
Total fatalities:
30
Captain / Total flying hours:
17142
Captain / Total hours on type:
59.00
Copilot / Total flying hours:
8466
Copilot / Total hours on type:
363
Aircraft flight hours:
611
Circumstances:
A United Air Lines, Inc., Boeing 727-22, N7036U, Flight 389 (UAL 389) was a regularly scheduled domestic passenger/cargo flight from LaGuardia Airport, New York to O'Hare International Airport, Chicago, Illinois. The aircraft had arrived at LaGuardia, on the date of the accident, following a trip from Los Angeles, California, with stops at Sacramento, California, Reno, Nevada, Denver, Colorado, and Chicago, Illinois. The flight crew of UAL 389 reported for duty at LaGuardia Airport one hour before scheduled departure where they prepared for the flight to Chicago. The stewardesses arrived with the aircraft from Chicago. Persons known to have been in contact with the crew prior to their departure from New York noticed nothing unusual about their behavior or appearance. UAL 389 departed LaGuardia at 1952 on an Instrument Flight Rules (IFR) flight plan at FL 350 and estimated their arrival time at O'Hare to be 2127. The crew reported at FL 350 at 2011.35. At 2102 UAL 389 came under control of the Chicago Air Route Traffic Control Center (ARTCC) reporting its altitude as FL 350 and was cleared to the O'Hare Airport via Pullman VORTAC direct to the Northbrook VORTAC, direct O'Hare and to maintain FL 350. This clearance was acknowledged correctly and the crew was advised that radar contact had been established. At 2103 the ARTCC controller cleared UAL 389 to descend to FL 240 and to "start descent now through 31" (FL 310). UAL 389 replied "...down to 240, leaving three five." At 2106 UAL 389 was cleared to continue its descent to 14,000 feet and given an altimeter setting of 29.90 inches for O'Hare. This message was acknowledged immediately and in reply to the controller's inquiry the crew reported they were leaving FL 280 "now." At 2109 the flight was instructed to change frequencies and within the same minute reported out of FL 260 descending to fourteen thousand. This was the last altitude information received from the crew. At 2111 the flight was cleared to descend to 6,000 feet and the clearance was immediately acknowledged correctly. At 2118:35 control of the flight was passed to Chicago Approach Control (ORD). The radar target of UAL 389 was in the vicinity of the Sturgeon Intersection (intersection of the 011 radial of Chicago Heights and 076 radial of Northbrook VORTAC, 28 miles east of Northbrook VORTAC). At 2118:38 the target was observed approximately 2 miles east of the intersection. At 2119:36 the crew contacted ORD and was advised that radar contact had been established. At this time the aircraft target was 2-3 miles west of Sturgeon. UAL 389 was cleared to maintain 6,000 feet and to depart the Northbrook VORTAC on a heading of 240 degrees. The flight was advised that instrument landing system approaches were in progress on runway 14R at O'Hare and that the current O'Hare altimeter setting was 29.93. The pilot read back the altimeter setting incorrectly, the controller corrected him, and the pilot repeated it correctly. This was the last communication received from the flight and ended at 2120:03. The airplane crashed into Lake Michigan and exploded upon impact. All 30 occupants were killed.
Probable cause:
The Board is unable to determine the reason for the aircraft not being leveled off at its assigned altitude of 6,000 feet.
Final Report:

Crash of a Beechcraft C-45H Expeditor in Long Beach: 8 killed

Date & Time: Aug 7, 1965 at 0209 LT
Type of aircraft:
Operator:
Registration:
N88Q
Flight Phase:
Survivors:
No
MSN:
AF-710
YOM:
1954
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
7000
Circumstances:
Shortly after takeoff from Long Beach Airport, while climbing by night and a limited visibility due to fog, one of the engine failed. Unable to maintain a safe altitude, the twin engine aircraft struck power cables, stalled and crashed in flames in Lakewood. The airplane was totally destroyed by impact forces and a post crash fire and all 8 occupants were killed.
Probable cause:
Investigations were unable to determined the exact cause of the engine failure.
Final Report:

Crash of a Beechcraft Queen Air 65 in Iron Mountain

Date & Time: Jul 27, 1965 at 2005 LT
Type of aircraft:
Registration:
N575K
Flight Type:
Survivors:
Yes
Schedule:
Iron Mountain - Iron Mountain
MSN:
LC-173
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9402
Captain / Total hours on type:
52.00
Circumstances:
On final approach to Iron Mountain-Ford Airport, while on a local training mission, the crew voluntarily shut down one engine to simulate a failure. Due to insufficient speed, the airplane stalled and crashed in a field located few miles short of runway. While both occupants were slightly injured, the airplane was damaged beyond repair.
Probable cause:
The crew failed to maintain a sufficient speed on approach.
Final Report:

Crash of a Convair CV-440 Metropolitan in Williamsport

Date & Time: Jul 23, 1965 at 1506 LT
Operator:
Registration:
N8415H
Flight Phase:
Survivors:
Yes
Schedule:
Pittsburgh-Du Bois-Phillipsburg-Williamsport-Wilkes-Barre-Newark
MSN:
125
YOM:
1953
Flight number:
AL604
Crew on board:
4
Crew fatalities:
Pax on board:
36
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10071
Captain / Total hours on type:
1296.00
Copilot / Total flying hours:
5061
Copilot / Total hours on type:
1410
Aircraft flight hours:
26266
Circumstances:
Allegheny Airlines, Inc., Flight 604, a Convair 340/440, N8415H, crashed 5 miles east-northeast of the Williamsport-Lycoming County Airport, Montoursville, Pennsylvania, on July 23, 1965. The 36 passengers, 3 crew members, and 1 jumpseat rider survived but received varying degrees of injuries. The flight, regularly scheduled from Pittsburgh, Pennsylvania to Newark, New Jersey, with intermediate stops at Dubois, Phillipsburg, Williamsport and Wilkes-Barre, Pennsylvania, departed Runway 09 at 1503. e.d.t. Shortly after takeoff smoke and fire were observed coming from the right engine and at approximately 1505:30 the captain advised "Six oh four is coming back in, we've got the right engine feathered.” The crash occurred moments later on the crest of a ridge approximately 600 feet above the airport elevation. The aircraft was destroyed by fire. The failure of the right engine is attributed to the failure of the front row master rod and all the associated link rods. Damage to the rod ends precluded any determination of the cause of the master rod failure.
Probable cause:
The Board determines that the probable cause of this accident was the failure of the crew to implement proper procedures for an engine failure on takeoff.
Final Report:

Crash of a Travel Air 4000 in Alamo: 1 killed

Date & Time: Jul 22, 1965 at 1130 LT
Type of aircraft:
Registration:
N8140
Flight Phase:
Survivors:
No
Schedule:
Alamo - Alamo
MSN:
914
YOM:
1929
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot was engaged in a crop spraying mission on cotton fields. While flying at low height in marginal weather conditions, the single engine aircraft went out of control and crashed in flames. The aircraft was destroyed and the pilot was killed.
Probable cause:
Loss of control caused by local whirlwind.
Final Report:

Crash of a Beechcraft C18S in Houston

Date & Time: Jul 18, 1965 at 0845 LT
Type of aircraft:
Operator:
Registration:
N445N
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
7858
YOM:
1944
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4500
Captain / Total hours on type:
3000.00
Circumstances:
After takeoff, while in initial climb, one of the engine failed. The pilot reduced his altitude and attempted an emergency landing. The airplane belly landed in a field and came to rest in flames. All four occupants escaped uninjured while the airplane owned by George J. Darneille was destroyed by fire.
Probable cause:
Engine failure for undetermined reason.
Final Report:

Crash of a Beechcraft C-45G Expeditor in Parkersburg: 5 killed

Date & Time: Jul 13, 1965 at 1502 LT
Type of aircraft:
Registration:
N2818G
Flight Phase:
Survivors:
No
MSN:
AF-336
YOM:
1953
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
6500
Captain / Total hours on type:
151.00
Circumstances:
Shortly after takeoff from Parkersburg-Wood County Airport, while climbing, the twin engine aircraft went out of control and crashed in flames in a field. The airplane was destroyed and all five occupants were killed.
Probable cause:
It was determined that the pilot suffered a heart attack and lost control of the airplane.
Final Report:

Crash of a Beechcraft C18S Expeditor off Marathon

Date & Time: Jul 10, 1965 at 0500 LT
Type of aircraft:
Operator:
Registration:
N7871B
Flight Phase:
Survivors:
Yes
Schedule:
Marathon - Marathon
MSN:
8103
YOM:
1944
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12800
Captain / Total hours on type:
900.00
Circumstances:
Shortly after takeoff from Marathon Airport, while in initiale climb, both engines failed simultaneously. The aircraft stalled and crashed into the sea few dozen yards off shore. The pilot was uninjured and quickly rescued while the airplane was lost.
Probable cause:
Double engine caused by an inadequate preflight preparation on part of the pilot. The fuel selector was positioned between tanks.
Final Report:

Crash of a Beechcraft C-45H Expeditor in Salmon: 2 killed

Date & Time: Jul 9, 1965 at 1545 LT
Type of aircraft:
Operator:
Registration:
N9327Z
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Salmon - Salmon
MSN:
AF-716
YOM:
1954
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1266
Captain / Total hours on type:
72.00
Circumstances:
The crew was engaged in a firefighting mission in the region of Salmon, Idaho. While cruising a low height, the crew failed to realize his speed was too low when the airplane stalled and crashed in flames. The aircraft was destroyed and both crew members were killed.
Probable cause:
The crew failed to maintain flying speed. Unfavorable wind conditions and downdraft/updraft as well as inherent high risk flight operation were considered as contributing factor.
Final Report:

Crash of a Boeing 707-124 in Kansas City

Date & Time: Jul 1, 1965 at 0529 LT
Type of aircraft:
Operator:
Registration:
N70773
Survivors:
Yes
Schedule:
Los Angeles – Kansas City – Chicago
MSN:
17609
YOM:
1959
Flight number:
CO012
Crew on board:
6
Crew fatalities:
Pax on board:
60
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
18729
Captain / Total hours on type:
850.00
Copilot / Total flying hours:
3178
Copilot / Total hours on type:
428
Aircraft flight hours:
25263
Circumstances:
The aircraft made a "firm" landing, in heavy rain, about 1,050 feet past the approach end of runway 18. When the crew's efforts to stop the aircraft were ineffective, and the captain was convinced that they were going off the end of the runway, he used differential power and rudder to cock the aircraft to the left. The aircraft slid off the end of the runway, went through the US localizer antenna building, struck a dirt blast mound, slid up over the mound, and came to rest with the nose section in the perimeter road between the blast mound and a river levee. Of the 60 passengers and 6 crew members aboard, three passengers and two crew members received minor injuries. The aircraft received substantial damage although no major fire occurred. The passengers and crew evacuated the aircraft without major difficulty.
Probable cause:
The Board determines that the probable cause of this accident was hydroplaning of the landing gear wheels that precluded braking effectiveness.
Final Report: