Crash of a Dassault Falcon 10 in Detroit

Date & Time: Jan 24, 1996 at 1018 LT
Type of aircraft:
Operator:
Registration:
N191MC
Survivors:
Yes
Schedule:
Philadelphia - Flint
MSN:
30
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11163
Captain / Total hours on type:
1330.00
Aircraft flight hours:
9829
Circumstances:
The pilot reported getting an unsafe indication on the right main landing gear when the landing gear was lowered. The crew recycled the landing gear and got the same unsafe indication. The crew retracted the gear and diverted to Detroit. On arrival, the crew performed the 'landing gear abnormal extension checklist,' but the unsafe indication remained. The air traffic control tower reported that the gear appeared normal. During the landing, the right main landing gear retracted. The airplane slid sideways, striking a runway marker as it departed the runway, and came to rest in a field. Examination revealed that the right landing gear downlock mechanism could be overcome with physical force. Examination of the right landing gear actuator revealed that one of the six shims which separate the spacers and help guide the safety lock switch was out of position and lying on top of the lock assembly.
Probable cause:
Failure of the right landing gear locking mechanism.
Final Report:

Crash of a Learjet 25XR in Columbus

Date & Time: Jul 1, 1991 at 2152 LT
Type of aircraft:
Operator:
Registration:
N458J
Survivors:
Yes
Schedule:
Philadelphia - Columbus
MSN:
25-106
YOM:
1973
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9450
Captain / Total hours on type:
4156.00
Circumstances:
N458J was landing during a rain shower. As the airplane started to flare for landing, the wind caused it to drift to the right. The pilot started to correct this drift, as the rain became heavier. During the touchdown, the pilot lost visual reference with the runway, yet he continued with the landing roll. The airplane drifted off the left side of the runway and ran into soft terrain. Both pilots escaped uninjured and the aircraft was damaged beyond repair.
Probable cause:
The failure of the pilot to maintain visual reference with the runway during a landing, which resulted in a loss of directional control. Also causal to the accident was the pilot's failure to initiate a go-around, after he lost sight of the runway during the touchdown. Factors related to the accident were the heavy rain and the lack of runway centerline lights.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) in Merion: 3 killed

Date & Time: Apr 4, 1991 at 1210 LT
Registration:
N3645D
Survivors:
No
Site:
Schedule:
Williamsport – Philadelphia
MSN:
61-0844-8162153
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
1876
Aircraft flight hours:
2739
Circumstances:
Piper Aerostar 601, N3645D, was arriving as Bell 412 (helicopter), N78S, was departing. N3645D reported the aircraft's nose gear indicator light did not illuminate to verify the nose gear was down and locked. Crew of N78S heard the communication and saw N3645D as they crossed beneath N3645D's approach path. They reported N3546D's nose gear appeared to be extended. N3645D flew past the tower and tower personnel also reported the nose gear appeared to be extended. As N3645D was cleared to turn downwind, N78S offered to join for a closer look. Captain of N3645D accepted the offer. During joinup, N78S converged from left rear, then reported they would pass around the right side and look at everything as they went by. They reported that everything looked ok. Moments later, the two aircrafts collided and crashed to the ground. No mechanical reason was found that would have resulted in the accident. None of the pilots had training for flight in close proximity to another aircraft. There were indications the captain of N3645D lacked training in aircraft systems and that his employer (the operator) lacked surveillance by the FAA. The emergency procedure section of the Aerostar flight manual lacked info on emergency gear extension. All three occupants were killed as well as both pilots on board the helicopter. Four other people on the ground were injured, one seriously.
Probable cause:
The poor judgement by the captain of the airplane to permit the inflight inspection after he had determined to the best of his ability that the nose landing gear was fully extended, the poor judgment of the captain of the helicopter to conduct the inspection, and the failure of the flightcrew of the helicopter to maintain safe separation. Contributing to the accident was the incomplete training and checking that the flightcrew of N3645D received from lycoming air service and the faa principal operations inspector assigned to the operator.
Final Report:

Crash of a Beechcraft C90 King Air in Beaufort: 2 killed

Date & Time: Nov 30, 1987 at 0946 LT
Type of aircraft:
Operator:
Registration:
N4463W
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Savannah - Philadelphia
MSN:
LJ-633
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
14000
Aircraft flight hours:
2092
Circumstances:
At 0938, while climbing thru 9,000 feet, the pilot was cleared to climb to FL210. Approximately 10 minutes later, the ATC controller noted the aircraft's mode C return wasn't being displayed on his scope. He tried to advise the pilot, but couldn't establish radio contact. The aircraft broke up in flight and the wreckage was found submerged in a creek and on marshland. A large piece of the right outboard wing panel was found about 2 miles east of the main wreckage. The right engine was found approximately 800 feet to 1,200 feet northeast of the main wreckage in 4 feet of water. There was evidence the right outboard wing had failed from upward and aft overload. No pre-accident mechanical failure or malfunction was found that would have resulted in an in-flight break-up. Radar data showed the aircraft was climbing at 115 knots and 1,100 feet/minute; at approximately 16,000 feet msl, rate of climb slowed to approximately 750 feet/minute, then increased to 1,200 feet/minute. Peak altitude was approximately 18,200 feet. Aircraft then entered a steep descent and crashed. At the approximately time and place of peak altitude, primary targets appeared on radar and remained for several minutes. Organic material was found on left engine inlet screen, but source was not determined. Accident occurred along bird flyway. Both occupants were killed.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: climb
Findings
1. (c) reason for occurrence undetermined
2. Design stress limits of aircraft - exceeded
3. Wing - overload
4. Wing - separation
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
5. Terrain condition - water
Final Report:

Crash of a Piper PA-46-310P Malibu in West Mifflin: 2 killed

Date & Time: Aug 15, 1986 at 2247 LT
Registration:
N27EE
Flight Phase:
Survivors:
Yes
Schedule:
Pittsburgh – Philadelphia
MSN:
46-8608036
YOM:
1986
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1166
Captain / Total hours on type:
127.00
Aircraft flight hours:
349
Circumstances:
At 2232 edt, the aircraft was climbing to 15,000 feet when the pilot reported a low oil pressure light. ATC advised Jimmy Stewart Field is about eleven thirty and 15 miles. After the pilot asked, 'is that a Tower Field?', ATC advised he did not know, Westmoreland County is at two o'clock and about 15 miles, turn right 180°, descend and maintain 4,000 feet. At 2233 edt, ATC said that they believe Westmoreland County Tower is closed down. The pilot said that he was thinking of where he should go and ATC advised Pittsburgh's 35 miles away if you can make that. At 2234:35 edt, the aircraft was returning to Pittsburgh when the pilot reported zero oil pressure and an oil light. At 2237:27 edt, the pilot reported an emergency. Flight was cleared to Allegheny County Airport and advised Monroeville Airport 230 heading and 5 miles. The aircraft crashed at 2247 edt. The investigation showed a loose flange nut on left turbocharger feed line finger tight. Test produced a steady leak. At site oil covered bottom of fuselage and empennage. Two passengers were killed while two other occupants were injured.
Probable cause:
Occurrence #1: loss of engine power (partial) - mech failure/malf
Phase of operation: climb - to cruise
Findings
1. (c) lubricating system, oil tubing - loose
2. (c) maintenance - inadequate - other maintenance personnel
3. (c) fluid, oil - exhaustion
4. (c) engine assembly - failure, partial
5. (f) emergency procedure - delayed - pilot in command
----------
Occurrence #2: forced landing
Phase of operation: maneuvering - turn to landing area (emergency)
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: maneuvering - turn to landing area (emergency)
Findings
6. (c) in-flight planning/decision - poor - pilot in command
Final Report:

Crash of a Douglas DC-9-15 in Philadelphia

Date & Time: Feb 6, 1985 at 2351 LT
Type of aircraft:
Operator:
Registration:
N926AX
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Philadelphia - Wilmington
MSN:
47002
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7500
Captain / Total hours on type:
1800.00
Circumstances:
After landing, the aircraft was parked on the ramp for approximately 39 minutes to load cargo. During that time, light freezing drizzle was falling, intermittently mixed with ice pellets and snow. The crew checked the aircraft surfaces from the cockpit and entry door, but observed no ice or snow adhering to the tops of the wings, nose section, windshield or above the door. The captain declined an offer to de-ice, two other aircraft were being de-iced. The takeoff was normal (18° nose up attitude) until just after lift-off, then the aircraft entered an uncommanded left roll and both engines compressor stalled. The captain corrected with left aileron and rudder, then began aborting the takeoff. The aircraft touched down left of the runway on the tail skid and right wing tip, approximately 5,600 feet from the threshold and on a 070° heading. It then traveled another 2,025 feet in a sweeping right arc, hitting 2 runway signs and came to rest heading west with the right pylon bent down. Investigations revealed a thin layer of ice (est 0.15 inch thick) would have been on the wings, raising the aircraft's stall speed. When DC-9-15 aircraft stall, engines are susceptible to compressor stalls.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
1. (f) weather condition - rain
2. (f) weather condition - snow
3. (f) weather condition - icing conditions
4. (f) light condition - dark night
5. (c) wing - ice
6. (c) ice/frost removal from aircraft - not performed - pilot in command
7. (f) visual/aural detection - pilot in command
8. (c) stall - inadvertent - pilot in command
----------
Occurrence #2: loss of engine power (total) - nonmechanical
Phase of operation: takeoff - initial climb
Findings
9. Aborted takeoff - initiated - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: takeoff
----------
Occurrence #4: on ground/water collision with object
Phase of operation: other
Final Report:

Crash of a Lockheed L-188CF Electra at Dobbins AFB

Date & Time: Jan 29, 1985 at 0936 LT
Type of aircraft:
Operator:
Registration:
N854U
Flight Type:
Survivors:
Yes
Schedule:
Philadelphia - Charlotte
MSN:
2009
YOM:
1959
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6900
Captain / Total hours on type:
303.00
Aircraft flight hours:
47765
Circumstances:
During gear retraction after takeoff, the right main gear became jammed in a partially retracted position and the respective in-transit gear light would not extinguish. Attempts to recycle the gear were unsuccessful. The flight crew diverted to Atlanta, GA; then decided to land at Dobbins AFB, where there was a long, wide runway that could be foamed. Foam was applied to approximately 300 feet of runway 29. The aircraft was landed with the nose and left main gear extended and the right main gear partially retracted. Subsequently, the aircraft veered to the right and stopped with the nose gear approximately 70 feet off the runway. Fire erupted in the area of the right main gear; however, the fire was quickly extinguished by fire dept personnel. An investigation revealed the clearance between the main landing gear door hook, pn 803845-1, and the strut roller was excessive. The reason for the improper clearance was not determined. Lockheed service bulletin 88/sb-558 warned that excessive clearance combined with a drop in hydraulic pressure, gust or maneuver could result in the gear jamming. All three crew members were uninjured.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: takeoff - initial climb
Findings
1. Door, landing gear - assembly
2. (c) door, landing gear - clearance
3. (c) door, landing gear - exceeded
4. (c) landing gear, normal retraction/extension assembly - jammed
5. (c) landing gear, main gear - movement restricted
6. Gear down and locked - not possible
----------
Occurrence #2: dragged wing, rotor, pod, float or tail/skid
Phase of operation: landing - roll
----------
Occurrence #3: loss of control - on ground/water
Phase of operation: landing
Findings
7. Directional control - not possible
8. Ground loop/swerve - uncontrolled
Final Report:

Crash of a Beechcraft H18 in Allentown: 2 killed

Date & Time: Nov 25, 1983 at 0808 LT
Type of aircraft:
Registration:
N105PE
Flight Type:
Survivors:
No
Schedule:
Philadelphia - Wilkes Barre
MSN:
BA-672
YOM:
1964
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3800
Captain / Total hours on type:
145.00
Aircraft flight hours:
7046
Circumstances:
While en route, the pilot encountered icing conditions, then reported he was unable to maintain altitude and was having engine problems. He diverted toward Allentown, PA, then advised he had lost power in the left engine. Approach control began issuing vectors for a VOR approach; however, the pilot advised he was unable to open his approach plates and requested a surveillance radar approach. Radar vectors and advisories were provided until the pilot reported he had the airport in sight. Several witnesses observed that the left prop was feathered as the aircraft approached the airport. The pilot maneuvered the aircraft to a left downwind for runway 24 at about 400 feet agl with the landing gear extended. Witnesses reported the aircraft's nose pitch up, then down, then the aircraft rolled to the left and crashed. In a trailer court it hit a mobile home and a propane tank and burned. A person in the mobile home was fatally injured. An exam of the wreckage revealed the left prop blades were at the low pitch stops. No preimpact failures were found.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: cruise - normal
Findings
1. (f) weather condition - carburetor icing conditions
2. (f) planning/decision - improper - pilot in command
----------
Occurrence #2: loss of engine power (total) - nonmechanical
Phase of operation: cruise
Findings
3. (f) delayed - pilot in command
4. (f) fuel system, ram air/induction air - ice
5. (f) fuel system, ram air/induction air - blocked (total)
----------
Occurrence #3: loss of control - in flight
Phase of operation: approach - VFR pattern - downwind
Findings
6. Precautionary landing - initiated - pilot in command
7. (c) airspeed (vmc) - not maintained - pilot in command
----------
Occurrence #4: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
8. Emergency procedure - attempted - pilot in command
Final Report:

Crash of a Rockwell Sabreliner 65 in Toronto: 5 killed

Date & Time: Jan 11, 1983
Type of aircraft:
Operator:
Registration:
N99S
Survivors:
No
Schedule:
Philadelphia - Toronto
MSN:
465-64
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
On approach to Toronto-Lester Bowles Pearson Airport following an uneventful flight from Philadelphia, the airplane rolled left and right then lost altitude and crashed in a field, bursting into flames. The wreckage was found 13 km from runway 24R threshold. The aircraft was destroyed by impact forces and a post crash fire and all five occupants were killed, among them Ross Henningar, President and CEO of Sun Oil Company (Sunoco).
Probable cause:
Loss of control on approach following an internal failure in the low pressure compressor of the right engine while the left engine flamed out and was windmilling at impact. Investigations were unable to determine the cause of these occurrences. It was also noted that the anti-icing systems were not activated prior to the accident while icing conditions have been forecasted.

Crash of a Piper PA-31-350 Navajo Chieftain in Philadelphia: 3 killed

Date & Time: Jul 25, 1980 at 0713 LT
Operator:
Registration:
N5MS
Survivors:
No
Schedule:
Reading - Philadelphia
MSN:
31-7405138
YOM:
1974
Flight number:
501
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3670
Captain / Total hours on type:
117.00
Circumstances:
The aircraft crashed while making a visual approach to runway 27R at Philadelphia International Airport. The aircraft, a scheduled commuter flight from Reading, Pennsylvania, arrived in the Philadelphia Approach Control area as a VFR 'pop up' flight and was sequenced to land behind United flight 555, a Boeing 727 IFR arrival, on runway 27R. Witnesses stated that, when flight 501 was about 1/2 mile on final approach, it rolled from side to side, pitched up, rolled inverted to the left, and flew into the ground nose first. All three persons aboard the aircraft were killed and the aircraft was destroyed.
Probable cause:
The probable cause of the accident was the loss of aircraft control due to an encounter with wake turbulence from the preceding aircraft at an altitude too low for recovery and the pilot's failure to follow established separation and flight path selection procedures for wake turbulence avoidance.
Final Report: