Crash of a Beechcraft E18S in Cincinnati: 1 killed

Date & Time: Mar 9, 1989 at 0617 LT
Type of aircraft:
Operator:
Registration:
N3281T
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Cincinnati – Detroit
MSN:
BA-611
YOM:
1962
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10560
Captain / Total hours on type:
15.00
Aircraft flight hours:
13262
Circumstances:
N3281T was attempting an instrument departure when it crashed left of the extended centerline of runway 18. The flight was observed climbing through 200 feet prior to descending to the ground. Prior to taxiing to takeoff the pilot failed to deice the airframe. Airplanes on the parking ramp around N3281T deiced prior to takeoff. Weather reports indicated that temp/dew point were 26 and 23° respectively. The surface observation also reported fog as a restriction to visibility. According to the airplane's handbook that tests prove that a coat of frost on a wing can destroy its lift. The pilot, sole on board, was killed.
Probable cause:
Pilot attempted a takeoff with coating of frost on the airframe which resulted in a loss of lift during climbout.
Final Report:

Crash of a Cessna 414 Chancellor in Pontiac

Date & Time: Dec 19, 1988 at 2010 LT
Type of aircraft:
Operator:
Registration:
N414CM
Flight Type:
Survivors:
Yes
Schedule:
Detroit - Pontiac
MSN:
414-0035
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1023
Captain / Total hours on type:
98.00
Aircraft flight hours:
5916
Circumstances:
While on final approach to land at night, the left engine lost power due to fuel starvation. Attempts to restart the engine were not successful. While the pilot was attempting a restart, the aircraft drifted to the right of the runway centerline and toward the proximity of hangars. The pilot stated that due to the power loss and wind conditions, he elected to land on airport property. Gear extension was delayed until just before landing. The aircraft touched down before the right main landing gear was fully extended and locked. Subsequently, the right main gear collapsed and the aircraft skidded about 500 feet before coming to rest. An examination revealed the nacelle and main fuel tanks were empty, but fuel was still remaining in the auxiliary tanks.
Probable cause:
Occurrence #1: loss of engine power (total) - nonmechanical
Phase of operation: approach
Findings
1. 1 engine
2. (c) fluid, fuel - starvation
3. (c) fuel tank selector position - improper - pilot in command
----------
Occurrence #2: gear not extended
Phase of operation: landing - flare/touchdown
Findings
4. (f) light condition - dark night
5. (f) weather condition - gusts
6. (f) weather condition - crosswind
7. (c) compensation for wind conditions - improper - pilot in command
8. Precautionary landing - initiated - pilot in command
9. (c) gear down and locked - delayed - pilot in command
----------
Occurrence #3: main gear collapsed
Phase of operation: landing
Final Report:

Crash of a McDonnell Douglas MD-82 in Detroit: 156 killed

Date & Time: Aug 16, 1987 at 2045 LT
Type of aircraft:
Operator:
Registration:
N312RC
Flight Phase:
Survivors:
Yes
Schedule:
Saginaw - Detroit - Phoenix - Santa Ana
MSN:
48090
YOM:
1981
Flight number:
NW255
Crew on board:
6
Crew fatalities:
Pax on board:
149
Pax fatalities:
Other fatalities:
Total fatalities:
156
Captain / Total flying hours:
20859
Captain / Total hours on type:
1359.00
Copilot / Total flying hours:
8044
Copilot / Total hours on type:
1604
Aircraft flight hours:
14928
Circumstances:
A McDonnell Douglas DC-9-82 operating Northwest Airlines flight 255 was destroyed when it crashed onto a road during takeoff from Detroit-Metropolitan Wayne County Airport, Michigan, USA. Just one of the 155 occupants survived the accident. Additionally, Two persons on the ground were killed. Flight NW255 was a regularly scheduled passenger flight between Saginaw, Michigan and Santa Ana, California, with en route stops at Detroit and Phoenix, Arizona. About 18:53, flight 255 departed Saginaw and about 19:42 arrived at its gate at Detroit. About 20:32, flight 255 departed the gate with 149 passengers and 6 crewmembers on board. During the pushback, the flightcrew accomplished the BEFORE (engine) START portion of the airplane checklist, and, at 20:33, they began starting the engines. The flight was then cleared to "taxi via the ramp, hold short of (taxiway) delta and expect runway three center [3C] (for takeoff)..." The ground controller amended the clearance, stating that the flight had to exit the ramp at taxiway Charlie. The crew was requested to change radio frequencies. The first officer repeated the taxi clearance, but he did not repeat the new radio frequency nor did he tune the radio to the new frequency. At 20:37, the captain asked the first officer if they could use runway 3C for takeoff as they had initially expected 21L or 21R. After consulting the Runway Takeoff Weight Chart Manual, the first officer told the captain runway 3C could be used for takeoff. During the taxi out, the captain missed the turnoff at taxiway C. When the first officer contacted ground control, the ground controller redirected them to taxi to runway 3C and again requested that they change radio frequencies. The first officer repeated the new frequency, changed over, and contacted the east ground controller. The east ground controller gave the flight a new taxi route to runway 3C, told them that windshear alerts were in effect, and that the altimeter setting was 29.85 inHg. The flightcrew acknowledged receipt of the information. At 20:42, the local controller cleared flight 255 to taxi into position on runway 3C and to hold. He told the flight there would be a 3-minute delay in order to get the required "in-trail separation behind traffic just departing." At 20:44:04, flight 255 was cleared for takeoff. Engine power began increasing at 20:44:21. The flightcrew could not engage the autothrottle system at first, but, at 20:44:38, they did engage the system, and the first officer called 100 knots at 20:44:45. At 20:44:57, the first officer called "Rotate." Eight seconds later, the stall warning stick shaker activated, accompanied by voice warnings of the supplemental stall recognition system (SSRS). The takeoff warning system indicating that the airplane was not configured properly for takeoff, did not sound at any time prior or during takeoff. After flight 255 became airborne it began rolling to the left and right before the left wing hit a light pole in a rental car lot. After impacting the light pole, flight 255 continued to roll to the left, continued across the car lot, struck a light pole in a second rental car lot, and struck the side wall of the roof of the auto rental facility in the second rental car lot. The airplane continued rolling to the left when it impacted the ground on a road outside the airport boundary. The airplane continued to slide along the road, struck a railroad embankment, and disintegrated as it slid along the ground. Fires erupted in airplane components scattered along the wreckage path. Three occupied vehicles on the road and numerous vacant vehicles in the auto rental parking lot along the airplane's path were destroyed by impact forces and or fire. One passenger, a 4-year-old child was injured seriously.
Probable cause:
The flight crew's failure to use the taxi checklist to ensure that the flaps and slats were extended for take-off. Contributing the accident was the absence of electrical power to the airplane take-off warning system which thus did not warn the flight crew that the airplane was not configured properly for take-off. The reason for the absence of electrical power could not be determined.
Final Report:

Crash of a Casa 212 Aviocar 200 in Detroit: 9 killed

Date & Time: Mar 4, 1987 at 1434 LT
Type of aircraft:
Operator:
Registration:
N160FB
Survivors:
Yes
Schedule:
Cleveland - Detroit
MSN:
160
YOM:
1980
Flight number:
NW2268
Crew on board:
3
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
17953
Captain / Total hours on type:
3144.00
Copilot / Total flying hours:
1593
Aircraft flight hours:
12918
Aircraft flight cycles:
24218
Circumstances:
At 14:30 the flight was cleared for a runway 21R visual approach and was cleared to land one minute later, At a height of 60-70 feet the aircraft suddenly yawed violently to the left and banked left 80-90° in a descent. The aircraft then rolled right and struck the ramp area 1,010 feet inside and to the left of the runway 21R threshold. It then skidded 398 feet, struck three ground support vehicles in front of Gate F10 at Concourse F and caught fire. Both pilots and seven passengers were killed, 10 other occupants were injured.
Probable cause:
The captain's inability to control the airplane in an attempt to recover from an asymmetric power condition at low speed following his intentional use of the beta mode of propeller operation to descend and slow the airplane rapidly on final approach for landing. Factors that contributed to the accident were an unstabilized visual approach, the presence of a departing DC-9 on the runway, the desire to make a short field landing, and the higher-than-normal flight idle fuel flow settings of both engines. The lack of fire-blocking material in passenger seat cushions contributed to the severity of the injuries.
Final Report:

Crash of a Piper PA-46-310P Malibu in Boyne Falls: 2 killed

Date & Time: Mar 23, 1986 at 1643 LT
Registration:
N43769
Flight Type:
Survivors:
No
Schedule:
Detroit – Boyne Falls
MSN:
46-8508007
YOM:
1985
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1168
Circumstances:
After the pilot was cleared for an RNAV-B approach, the aircraft crashed on hilly terrain approximately 3 miles southeast of the airport at an elevation of 750 feet msl. Impact occurred after the aircraft had turned to the south-southeast and was descending. Minimum descent altitude (MDA) for the approach was 1,680 feet. No preimpact mechanical problems were found. Approximately 4 hours before takeoff, FSS personnel provided a weather briefing. There was no weather reporting station at the destination, but the area forecast was for marginal VMC with isolated visibilities of 3 to 5 miles in light snow showers. Pellston (approximately 25 miles away) was forecast for a chance of 1,200 feet overcast and 3 miles visibility with light snow showers, but this info was not given to the pilot. Later, when the pilot filed an IFR flight plan, he did not update his weather briefing. While en route, he checked the Pellston and Traverse City weather and was advised they had indefinite or obscured ceilings of 1,500 feet or less with gusty winds and light snow squalls. According to witnesses, there were snow showers or squalls in the accident area with 1/4 to 3/4 miles visibility. The missed approach procedure called for: right climbing turn to 3,000 feet, proceed to the IAF (8 miles south of airport) and hold. Both occupants were killed.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: approach - faf/outer marker to threshold (ifr)
Findings
1. (f) preflight planning/preparation - inadequate - pilot in command
2. (f) preflight briefing service - inadequate - atc personnel (fss)
3. (f) weather condition - low ceiling
4. (f) weather condition - snow
5. (f) weather condition - high wind
6. (f) weather condition - gusts
7. (f) weather condition - obscuration
8. (f) weather condition - below approach/landing minimums
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: approach
Findings
9. (c) ifr procedure - not followed - pilot in command
10. (c) minimum descent altitude - not maintained - pilot in command
11. (c) descent - not corrected - pilot in command
Final Report:

Crash of an Embraer EMB-110P1 Bandeirante in Alpena: 3 killed

Date & Time: Mar 13, 1986 at 2200 LT
Operator:
Registration:
N1356P
Survivors:
Yes
Schedule:
Detroit - Alpena - Saulte Sainte Marie
MSN:
110-370
YOM:
1981
Flight number:
MQ1746
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3384
Captain / Total hours on type:
574.00
Copilot / Total flying hours:
6271
Copilot / Total hours on type:
21
Aircraft flight hours:
9698
Aircraft flight cycles:
16767
Circumstances:
About 2050 on March 13, 1986, Simmons Airlines flight 1746, an Embraer Bandeirante, EMB-110P1, operating as a regularly scheduled flight, departed the Detroit Metropolitan Airport en route to Sault Ste Marie, Michigan, with a stop in Alpena, Michigan. The en route portion of the flight to Alpena was uneventful. However, due to the prevailing instrument meteorological conditions, the crew was unable to complete the instrument landing system (ILS) approach and land and they declared a missed approach at 2142. At 2153, the flight was cleared for a second ILS approach to Alpena. At 2156, the crew acknowledged that radar services were being terminated. This was the last transmission from the airplane. About 2215, a motorist reported that the airplane had
crashed. The airplane was found in a wooded area about 300 feet to the left of the extended centerline, and 1 1/2 miles short of the threshold of runway 01 at Alpena. The airplane was destroyed and two of the seven passengers and one of the two crewmembers onboard were killed.
Probable cause:
The National Transportation Safety Board determines that the probable cause of this accident was the flightcrew’s continued descent of the airplane below the glideslope and through the published decision height without obtaining visual reference of the runway for undetermined reasons. Contributing to the accident was the inefficient system used to disseminate weather-related information to the crew.
Final Report:

Crash of a Cessna 402C in Detroit: 1 killed

Date & Time: Nov 12, 1985 at 0208 LT
Type of aircraft:
Registration:
N6788Y
Flight Type:
Survivors:
No
Schedule:
Teterboro - Detroit - Chicago
MSN:
402C-0433
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4900
Captain / Total hours on type:
350.00
Aircraft flight hours:
2607
Circumstances:
A 100-feet ceiling with 3,000 feet RVR existed at Detroit. The pilot attempted an ILS approach with a 200 feet dh when he struck trees one mile from the runway. He flew the aircraft to the airfield but crashed near the threshold. The only approach plates found onboard were for Detroit and Midway in Chicago. Midway was his final destination after Detroit. He did not have enough fuel to get to Midway. The rest of his approach plates were later found in his personal vehicle back in Pennsylvania. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: approach - faf/outer marker to threshold (ifr)
Findings
1. (f) object - tree(s)
2. (c) ifr procedure - improper use of - pilot in command
3. (f) information unavailable - pilot in command
4. (f) weather condition - low ceiling
5. (c) preflight planning/preparation - inattentive - pilot in command
6. (f) self-induced pressure - pilot in command
7. (c) not performed - pilot in command
8. (c) visual lookout - reduced - pilot in command
9. (c) minimum descent altitude - not followed - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
10. (f) flt control syst, aileron control - loss, partial
11. (f) directional control - not possible - pilot in command
12. (f) flight control, aileron surface - loss, partial
13. (f) wing,wingtip - loss, total
Final Report:

Crash of a Convair VT-29B in Trenton

Date & Time: Jun 19, 1985 at 0702 LT
Type of aircraft:
Operator:
Registration:
N155PA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Trenton - Detroit
MSN:
322
YOM:
1953
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7000
Captain / Total hours on type:
2500.00
Aircraft flight hours:
16900
Circumstances:
The copilot begun takeoff with 2,700 rpm and 52 to 53.5' of manifold pressure (mp). Water injection was not used although 12 gallons was available. At 150 to 250 feet agl, the left engine lost power and the left propeller auto feathered. The captain took control and took action to verify left engine feathering. Neither pilot moved any of the other engine controls. A turn was initiated to return to the airport, but the aircraft began losing speed and altitude. Subsequently, it crash landed in a partly wooded area short of an open field and burned until firefighting personnel arrived. The impeller was demolished by fire, but evidence of debris from the impeller was found in the left engine intake and on top of its #3 and # 11 piston. The company's stated policy was to use water (wet takeoff), except when precluded by mechanical malfunction or lack of additional fluid; however, 4 dissimilar power charts were found in the aircraft. Takeoff weight was 38,670 lbs. Performance manual showed aircraft capable of 420 fpm climb with 12° of flaps, one prop feathered, landing gear up, dry power (no water). Max power setting was 2,700 rpm and 56' mp for dry takeoff; 2,800 rpm and 59.5' mp for wet takeoff. Both pilots were seriously injured.
Probable cause:
Occurrence #1: loss of engine power (partial) - mech failure/malf
Phase of operation: takeoff - initial climb
Findings
1. (c) eng assembly, blower/impeller/integral supercharger - failure, total
2. Propeller feathering - performed
----------
Occurrence #2: forced landing
Phase of operation: maneuvering - turn to landing area (emergency)
Findings
3. (c) throttle/power control - improper use of - pilot in command
4. (f) information unclear - company/operator management
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: maneuvering - turn to landing area (emergency)
Findings
5. (f) object - tree(s)
6. (f) terrain condition - rough/uneven
Final Report: