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Crash of a Lockheed WC-130H Hercules in Savannah: 9 killed

Date & Time: May 2, 2018 at 1127 LT
Type of aircraft:
Operator:
Registration:
65-0968
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Savannah – Davis-Monthan
MSN:
4110
YOM:
1965
Crew on board:
5
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total hours on type:
2070.00
Copilot / Total hours on type:
9
Circumstances:
On 2 May 2018, at approximately 1127 hours local time (L), the Mishap Aircraft (MA), a WC-130H, tail number 65-0968, assigned to the Puerto Rico Air National Guard, 156th Airlift Wing (156 AW), located at Muñiz Air National Guard Base, Puerto Rico, crashed approximately 1.5 miles northeast of Savannah/Hilton Head International Airport (KSAV), Georgia. All nine members aboard the MA—Mishap Pilot 1 (MP1), Mishap Pilot 2, Mishap Navigator, Mishap Flight Engineer, and Mishap Loadmaster (collectively the “Mishap Crew (MC)”), and four mission essential personnel, Mishap Airman 1, 2, 3, and 4—perished during the accident. The MC’s mission was to fly the MA to the 309th Aerospace Maintenance and Regeneration Group at Davis-Monthan Air Force Base, Arizona (commonly referred to as the “Boneyard”), for removal from service. The MA had been at KSAV for almost a month, since 9 April 2018, to undergo prescheduled fuel cell maintenance and unscheduled work on engine number one by 156 AW maintenance personnel using the facilities of the 165th Airlift Wing. During takeoff roll, engine one revolutions per minute (RPM) fluctuated and did not provide normal RPM when MP1 advanced the throttle lever into the flight range for takeoff. Approximately eight seconds prior to aircraft rotation, engine one RPM and torque significantly decayed, which substantially lowered thrust. The fluctuation on roll and significant performance decay went unrecognized by the MC until rotation, when MP1 commented on aircraft control challenges and the MA veered left and nearly departed the runway into the grass before it achieved flight. The MA departed KSAV at approximately 1125L. As the MC retracted the landing gear, they identified the engine one RPM and torque malfunction and MP1 called for engine shutdown. However, the MC failed to complete the Takeoff Continued After Engine Failure procedure, the Engine Shutdown procedure, and the After Takeoff checklist as directed by the Flight Manual, and the MA’s flaps remained at 50 percent. Additionally, MP1 banked left into the inoperative engine, continued to climb, and varied left and right rudder inputs. At an altitude of approximately 900 feet mean sea level and 131 knots indicated air speed, MP1 input over nine degrees of left rudder, the MA skidded left, the left wing stalled, and the MA departed controlled flight and impacted the terrain on Georgia State Highway 21.
Probable cause:
The board president found, by a preponderance of the evidence, the cause of the mishap was MP1’s improper application of left rudder, which resulted in a subsequent skid below three-engine minimum controllable airspeed, a left-wing stall, and the MA’s departure from controlled flight. Additionally, the board president found, by a preponderance of the evidence, the MC’s failure to adequately prepare for emergency actions, the MC’s failure to reject the takeoff, the MC’s failure to properly execute appropriate after takeoff and engine shutdown checklists and procedures, and the Mishap Maintainers’ failure to properly diagnose and repair engine number one substantially contributed to the mishap.
Final Report:

Ground accident of a Pilatus PC-12/47E in Savannah

Date & Time: Jan 6, 2016 at 0835 LT
Type of aircraft:
Operator:
Registration:
N978AF
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Savannah - Lexington
MSN:
1078
YOM:
2008
Flight number:
Cobalt Air 727
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
23141
Captain / Total hours on type:
534.00
Copilot / Total flying hours:
7900
Copilot / Total hours on type:
5100
Aircraft flight hours:
4209
Circumstances:
The aircraft collided with a ditch during a precautionary landing after takeoff from Savannah/Hilton Head International Airport (SAV), Savannah, Georgia. The pilot and copilot sustained minor injuries, and the airplane was substantially damaged. The airplane was registered to Upper Deck Holdings, Inc. and was being operated by PlaneSense, Inc,. as a Title 14 Code of Federal Regulations Part 91 positioning flight. Visual meteorological conditions prevailed, and an instrument flight rules flight plan was filed for the flight to Blue Grass Airport (LEX), Lexington, Kentucky. The pilot in the left seat was the pilot monitoring and the copilot in the right seat was the pilot flying. The crew had the full length of the runway 1 available (7,002 ft) for takeoff. The pilots reported that the acceleration and takeoff was normal and after establishing a positive rate of climb, the crew received an auditory annunciation and a red crew alerting system (CAS) torque warning. The engine torque indicated 5.3 pounds per square inch (psi); the nominal torque value for the conditions that day was reported by the crew to be 43.3 psi. With about 2,700 ft of runway remaining while at an altitude of 200 ft msl, the copilot elected to land immediately; the copilot pushed the nose down and executed a 90° left descending turn and subsequently landed in the grass. Although he applied "hard" braking in an attempt to stop, the airplane impacted a drainage ditch, resulting in substantial impact damage and a postimpact fire. The pilot reported that, after takeoff, he observed a low torque CAS message and the copilot told him to "declare an emergency and run the checklist." The pilot confirmed that the landing gear were extended and the copilot turned the airplane to the left toward open ground between the runways and the terminal. About 60 seconds elapsed from the start of the takeoff roll until the accident. The airport was equipped with security cameras that captured the airplane from its initial climb through the landing and collision. One camera, pointed toward the west-southwest, recorded the airplane's left descending turn and its landing in the grass, followed by impact and smoke. A second camera, mounted on the control tower, pointed toward the southeast and showed the airplane during the initial climb before it leveled off and entered a descending left turn; it also showed the airplane land and roll through the grass before colliding with the ditch.
Probable cause:
The pilots' failure to follow proper procedures in response to a crew alerting system warning for high engine torque values, which necessitated an off-runway emergency landing during which the airplane sustained substantial damage due to postimpact fire. Contributing to the accident was the erroneous engine torque indication for reasons that could not be determined.
Final Report:

Crash of an Embraer EMB-110P1 Bandeirante in Orangeburg

Date & Time: Dec 9, 2005 at 2240 LT
Operator:
Registration:
N790RA
Flight Type:
Survivors:
Yes
Schedule:
Savannah - Columbia
MSN:
110-278
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2250
Captain / Total hours on type:
195.00
Aircraft flight hours:
14837
Circumstances:
The pilot had flown the airplane the day before the accident and after landing on the morning of the accident; she ordered fuel for the airplane. While exiting the airplane another pilot informed her that he had heard a "popping noise" coming from one of the engines. The pilot of the accident airplane elected to taxi to a run up area to conduct an engine run up. The fuel truck arrived at the run up area and the pilot elected not to refuel the airplane at that time and continued the run up. No anomalies were noted during the run up and the airplane was taxied back to the ramp and parked. The pilot arrived back at the airport later on the day of the accident and did not re-order fuel for the airplane nor did she recall checking the fuel tanks during the preflight inspection of the airplane. The pilot departed and was in cruise flight when she noticed the fuel light on the annunciator panel flickering. The pilot checked the fuel gauges and observed less than 100 pounds of fuel per-side indicated. The pilot declared low fuel with Columbia Approach Control controllers and requested to divert to the nearest airport, Orangeburg Municipal. The controller cleared the pilot for a visual approach to the airport and as she turned the airplane for final, the left engine lost power followed by the right engine. The pilot made a forced landing into the trees about 1/4 mile from the approach end of runway 36. The pilot exited the airplane and telephoned 911 emergency operators on her cell phone. The pilot stated she did not experience any mechanical problems with the airplane before the accident. Examination of the airplane by an FAA inspector revealed the fuel tanks were not ruptured and no fuel was present in the fuel tanks.
Probable cause:
The pilot's inadequate preflight inspection and her failure to refuel the airplane which resulted in total loss of engine power due to fuel exhaustion, and subsequent in-flight collision with trees.
Final Report:

Crash of a Mitsubishi MU-2B-35 Marquise in Hilton Head: 1 killed

Date & Time: Aug 1, 2001 at 0751 LT
Type of aircraft:
Operator:
Registration:
N1VY
Flight Type:
Survivors:
No
Schedule:
Columbia – Savannah – Hilton Head
MSN:
567
YOM:
1972
Flight number:
BKA170
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4184
Captain / Total hours on type:
483.00
Aircraft flight hours:
11612
Circumstances:
The airplane was on final approach to land at Hilton Head Airport, when according to witnesses, it suddenly rolled to the right, and descended, initially impacting trees at about the 70-foot level, and then impacting the ground. A fire then ensued upon ground impact, and the debris field spanned about 370 feet along an azimuth of about 082 degrees. Examination of the airplane wreckage revealed that left wing flap actuator and jack nut measurements were consistent with the wing flaps being extended to 40 degrees, and on the right wing the flap jack nut and actuator measurements were consistent with the right flap being extended to about a 20-degrees. In addition, the right flap torque tube assembly between the flap motor and the flap stop assembly had disconnected, and the flap torque tube assembly's female coupler which attaches to the male spline end of the flap motor and flap stop assembly was found with a cotter pin installed through the female coupler of the flap stop assembly. The cotter pin, had not been placed through the spline and the coupler consistent with normal installation as per Mitsubishi's maintenance manual, or as specified in Airworthiness Directive 88-23-01. Instead, the cotter pin had missed the male spline on the flap motor. In addition, the flap coupler on the opposite side of the flap motor was found to also found to not have a cotter pin installed. Company maintenance records showed that on April 3, 2001, about 87 flight hours before the accident, the airplane was inspected per Airworthiness Directive (AD) 88-23-01, which required the disassembly, inspection, and reassembly of the flap torque tube joints. In addition, on July 9, 2001, the airplane was given a phase 1 inspection, and Bankair records showed that a company authorized maintenance person performed the applicable maintenance items, and certified the airplane for return to service.
Probable cause:
Improper maintenance/installation and and inadequate inspection of the airplane's flap torque tube joints during routine maintenance by company maintenance personnel, which resulted in the right flap torque tube assembly coupler becoming detached and the flaps developing asymmetrical lift when extended, which resulted in an uncontrolled roll, a descent, and an impact with a tree during approach to land.
Final Report:

Crash of a Cessna 208B Grand Caravan in Gainesville: 2 killed

Date & Time: Mar 3, 1995 at 1943 LT
Type of aircraft:
Registration:
N227DM
Survivors:
No
Schedule:
Savannah - Gainesville
MSN:
208B-0364
YOM:
1993
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2005
Captain / Total hours on type:
201.00
Circumstances:
The flight was executing the non-precision NDB runway 04 approach, had reported procedure turn inbound, and was cleared to change to advisory frequency. Witnesses observed the airplane descend out of the base of the overcast clouds in a 10° nose down, 45° left wing down attitude. The airplane impacted terrain about 3/4 mile south-southeast of the airport. Witnesses in the area reported that the weather was ceilings of about 100 feet and visibility of about 500 feet in light rain and fog. The minimum descent altitude for the approach is 465 feet agl. Both pilots were killed.
Probable cause:
The pilots failure to maintain the minimum descent altitude during the approach. The weather and dark night light condition were factors.
Final Report:

Crash of a Cessna 421C Golden Eagle III off Savannah: 5 killed

Date & Time: Jan 13, 1992 at 1606 LT
Registration:
N40JK
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Milville - Sebastian
MSN:
421C-0441
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
3064
Captain / Total hours on type:
500.00
Circumstances:
At 0716, the pilot received a weather brief for a proposed takeoff of 1130. The FSS briefer provided info on thunderstorms forecast in GA and FL. No info was provided about forecast lines and clusters of thunderstorms in SC coastal plains and sern GA. En route, the pilot was given info about level III thunderstorms across the projected flight path by Beaufort and Savannah approach control. ATC radar data revealed that the aircraft flew the route contained in the flight plan clearance. Radio transmissions from the aircraft indicated that onboard weather radar was being used. ATC radar data and radio communications indicated that the aircraft entered a thunderstorm, then made a 180° turn to exit the storm. Examination of the wreckage revealed plastic deformation of the wings inboard of the engines in an upward direction. Also, both wings broke off outboard of the engines in a downward direction. The horizontal stab and elevator were not recovered. There was fuselage damage which indicated that the horizontal stab separated aft and down. All five occupants were killed.
Probable cause:
The pilot's inadequate weather evaluation, and his continued flight into known adverse weather conditions. Factors were: the improper weather briefing by a flight service station specialist, and level iii thunderstorms.
Final Report:

Crash of a BAe 125-3A in Houston

Date & Time: Aug 13, 1989 at 1750 LT
Type of aircraft:
Operator:
Registration:
N66HA
Flight Type:
Survivors:
Yes
Schedule:
Savannah - Houston
MSN:
25126
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5180
Captain / Total hours on type:
10.00
Aircraft flight hours:
3966
Circumstances:
During landing, upon nose wheel contact with the runway, directional control was lost and the aircraft exited the runway hard surface and crossed a ditch collapsing the nose gear. The crew stated that full left rudder and differential braking would not stop the right drift, and that the aircraft was in grass uncontrollable by the time the steering tiller was reached. The nose wheel steering system was extensively damaged by the impact sequence when the nose wheel well aft bulkhead was forced into the steering assembly. The pilot stated that if he had been 'spring loaded to the tiller' that he could have possibly kept the aircraft off the grass.
Probable cause:
Failure of the nose wheel steering system for undetermined reasons, and the pilot-in-command's hesitation reaching for the nose wheel steering tiller. A contributing factor was his lack of experience in a DH-125.
Final Report:

Crash of a Beechcraft C90 King Air in Beaufort: 2 killed

Date & Time: Nov 30, 1987 at 0946 LT
Type of aircraft:
Operator:
Registration:
N4463W
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Savannah - Philadelphia
MSN:
LJ-633
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
14000
Aircraft flight hours:
2092
Circumstances:
At 0938, while climbing thru 9,000 feet, the pilot was cleared to climb to FL210. Approximately 10 minutes later, the ATC controller noted the aircraft's mode C return wasn't being displayed on his scope. He tried to advise the pilot, but couldn't establish radio contact. The aircraft broke up in flight and the wreckage was found submerged in a creek and on marshland. A large piece of the right outboard wing panel was found about 2 miles east of the main wreckage. The right engine was found approximately 800 feet to 1,200 feet northeast of the main wreckage in 4 feet of water. There was evidence the right outboard wing had failed from upward and aft overload. No pre-accident mechanical failure or malfunction was found that would have resulted in an in-flight break-up. Radar data showed the aircraft was climbing at 115 knots and 1,100 feet/minute; at approximately 16,000 feet msl, rate of climb slowed to approximately 750 feet/minute, then increased to 1,200 feet/minute. Peak altitude was approximately 18,200 feet. Aircraft then entered a steep descent and crashed. At the approximately time and place of peak altitude, primary targets appeared on radar and remained for several minutes. Organic material was found on left engine inlet screen, but source was not determined. Accident occurred along bird flyway. Both occupants were killed.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: climb
Findings
1. (c) reason for occurrence undetermined
2. Design stress limits of aircraft - exceeded
3. Wing - overload
4. Wing - separation
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
5. Terrain condition - water
Final Report:

Crash of a Cessna 441 Conquest II in West Columbia

Date & Time: Jan 15, 1986 at 0950 LT
Type of aircraft:
Operator:
Registration:
N441CD
Survivors:
Yes
Schedule:
Savannah - West Columbia
MSN:
441-0131
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3053
Captain / Total hours on type:
873.00
Aircraft flight hours:
1069
Circumstances:
During final approach the pilot noticed aircraft flying 'unusual' and elected go-around. During power-up, the aircraft lost power and a forced landing was made on a residential street near the airport. The pilot stated that he had inadvertently placed the fuel selector in crossfeed and had exhausted the fuel supply in the right wing by feeding both engines. There were no reported mechanical problems prior to the accident.
Probable cause:
Occurrence #1: loss of engine power (total) - nonmechanical
Phase of operation: go-around (vfr)
Findings
1. Fluid, fuel - starvation
2. (c) fuel tank selector position - improper - pilot in command
3. (c) in-flight planning/decision - poor - pilot in command
4. (f) checklist - not followed - pilot in command
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
----------
Occurrence #3: hard landing
Phase of operation: landing - flare/touchdown
Final Report:

Crash of a Cessna 340A near Orangeville: 1 killed

Date & Time: Nov 20, 1983 at 1255 LT
Type of aircraft:
Registration:
N85JK
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Savannah – Fort Lauderdale
MSN:
340A-0700
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The aircraft disappeared from radar coverage while in cruise flight at 10,000 feet msl near Orangeville, FL. The ATC transcript revealed that the pilot had been inquiring about the weather ahead of him and was cleared to descend to 6,000 feet in order to get below strong headwinds. One minute later he transmitted that he was going to stay at 10,000 feet because he did not have any choice (strong turbulence). His last transmission stated the weather was getting worse. The aircraft has not been located.
Probable cause:
Occurrence #1: missing aircraft
Phase of operation: unknown
Findings
1. Reason for occurrence undetermined
Final Report: