Crash of a Convair CV-440-38 Metropolitan off Tortola: 1 killed

Date & Time: Jul 12, 2004 at 0715 LT
Registration:
N4826C
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
San Juan - Sint Maarten
MSN:
391
YOM:
1956
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
27200
Captain / Total hours on type:
924.00
Copilot / Total flying hours:
256
Aircraft flight hours:
45771
Circumstances:
The copilot stated that the pre-flight and run-up before takeoff were performed with no discrepancies noted. After leveling off at 5,500 feet they noticed that the right engine cylinder head temperature and oil temperature was about 10 degrees above the normal parameter for that engine. Shortly after, both pilot's noticed a sharp decrease in the right engine mean effective pressure followed by vibration in the engine. The co-pilot looked at the right engine and informed the pilot that it was on fire around the front lower cylinders. Attempts by the pilot to extinguish the engine fire were unsuccessful. The pilot advised Air Traffic Control of their intention to ditch due to the right engine uncontrolled fire. The co-pilot, handed a life jacket to the pilot and then put his on. The pilot placed his life preserver to the side and did not put it on. While descending the co-pilot opened his side window, but the pilot did not. According to the co-pilot, shortly before ditching the pilot requested 10-degrees of flaps but the flaps did not move. Both pilots were at the controls of the airplane for the ditching. A review of maintenance records revealed that the right engine was installed on the airframe on May 14, 2003 at 45,660.5 hours total airframe time. A complete "C" Check was accomplished on June 15, 2004 at a total time of 45,741.8 hours with no discrepancies noted. The airplane ditched into the Caribbean Ocean 29 miles southeast of Beef Island, Virgin Islands, in an undetermined depth of water, neither the pilot or the airplane wreckage was recovered.
Probable cause:
The in-flight fire on the number two engine, for undetermined reasons.
Final Report:

Crash of an ATR72-212 in San Juan

Date & Time: May 9, 2004 at 1450 LT
Type of aircraft:
Operator:
Registration:
N438AT
Survivors:
Yes
Schedule:
Mayaguez - San Juan
MSN:
438
YOM:
1995
Flight number:
AA5401
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
22
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6071
Captain / Total hours on type:
3814.00
Copilot / Total flying hours:
2000
Copilot / Total hours on type:
20
Aircraft flight hours:
19276
Aircraft flight cycles:
18086
Circumstances:
Flight 5401 departed Mayagüez, Puerto Rico, for San Juan about 14:15. The captain was the nonflying pilot for the flight, and the first officer was the flying pilot. The takeoff, climb, and en route portions of the flight were uneventful. At 14:37, as the flight approached the San Juan traffic area, the ATIS reported that winds were 060 degrees at 17 knots and gusting at 23 knots. Shortly thereafter, the captain briefed a Vref (the minimum approach airspeed in the landing configuration before the airplane reaches the runway threshold) of 95 knots and told the first officer to "stand by for winds." At 14:43 SJU Terminal Radar Approach Control cautioned the pilots of possible wake turbulence from a preceding Boeing. The captain told the first officer to slow down to about 140 kts. At 14:46, the local controller cleared the airplane to land on runway 08. The first officer turned the airplane left toward runway 08 and transitioned to the visual approach slope indicator. At 14:49, the captain stated, "you better keep that nose down or get some power up because you're gonna balloon." The airplane descended below the glideslope, causing a GPWS "glideslope" alert. The airplane was about 45 feet above ground level and traveling at 110 knots indicated airspeed when it crossed the runway 08 threshold. After the airplane crossed the runway threshold, the captain stated, "power in a little bit, don't pull the nose up, don't pull the nose up." At 14:49:39, the captain stated, "you're ballooning," and the first officer replied, "all right." The airplane touched down for the first time about 14:49:41 and about 1,600 feet beyond the runway 08 threshold with vertical and lateral loads of about 1.3 Gs and -0.10 G, respectively. Upon touchdown the captain stated, "get the power," and, 1 second later, "my aircraft." The first officer responded, "your airplane." The airplane had skipped to an altitude of about 4 feet and touched down again two seconds later about 2,200 feet beyond the runway 08 threshold. The airplane then pitched up to an angle of 9° while climbing to an altitude of 37 feet and the engine torque increased from 10 to 43 percent. About 14:49:49, the pitch angle decreased to -3°, and the engine torque started to decrease to 20 percent with the pitch angle decreasing to -10°. The airplane touched down a third time about 14:49:51 at a bank angle of 7° left wing down and about 3,300 feet beyond the runway 08 threshold and with vertical and lateral loads of about 5 Gs and 0.85 G. The ATR pitched up again to 24 feet and landed a fourth time about 14:49:56 (about 15 seconds after the initial touchdown) and about 4,000 feet beyond the runway 08 threshold. This time the airplane pitched down to -7° and that it was banked 29° left wing down. The airplane came to a complete stop on a grassy area about 217 feet left of the runway centerline and about 4,317 feet beyond the runway threshold.
Probable cause:
The captain’s failure to execute proper techniques to recover from the bounced landings and his subsequent failure to execute a go-around.
Final Report:

Crash of a Learjet 25B in Fort Lauderdale

Date & Time: Feb 20, 2004 at 2157 LT
Type of aircraft:
Operator:
Registration:
N24RZ
Flight Type:
Survivors:
Yes
Schedule:
San Juan – Fort Lauderdale
MSN:
25-159
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4500
Aircraft flight hours:
4104
Circumstances:
The captain and first officer were conducting a CFR Part 135 on-demand charter flight, returning two passengers to the accident airplane's base airport. The multi-destination flight originated from the accident airport, about 16 hours before the accident. On the final leg of the flight, the flight encountered stronger than anticipated headwinds, and the first officer voiced his concern several times about the airplane's remaining fuel. As the flight approached the destination airport, the captain became concerned about having to fly an extended downwind leg, and told the ATCT specialist the flight was low on fuel. The ATCT specialist then cleared the accident airplane for a priority landing. According to cockpit voice recorder (CVR) data, while the crew was attempting to lower the airplane's wing flaps in preparation for landing, they discovered that the flaps would not extend beyond 8 degrees. After the landing gear was lowered, the captain told the first officer, in part: "The gear doors are stuck down.... no hydraulics." The captain told the first officer: "Okay, so we're gonna do, this is gonna be a ref and twenty...All right, probably not going to have any brakes..." According to a ATCT specialist in the control tower, the airplane touched down about midway on the 6001-foot long, dry runway. It continued to the end of the runway, entered the overrun area, struck a chain link fence, crossed a road, and struck a building. During a postaccident interview, the captain reported that during the landing roll the first officer was unable to deploy the airplane's emergency drag chute. He said that neither he nor the first officer attempted to activate the nitrogen-charged emergency brake system. The accident airplane was not equipped with thrust reversers. A postaccident examination of the accident airplane's hydraulic pressure relief valve and hydraulic pressure regulator assembly revealed numerous indentations and small gouges on the exterior portions of both components, consistent with being repeatedly struck with a tool. When the hydraulic pressure relief valve was tested and disassembled, it was discovered that the valve piston was stuck open. The emergency drag chute release handle has two safety latches that must be depressed simultaneously before the parachute will activate. An inspection of the emergency drag chute system and release handle disclosed no pre accident mechanical anomalies.
Probable cause:
The pilot in command's misjudged distance/speed while landing, and the flightcrew's failure to follow prescribed emergency procedures, which resulted in a runway overrun and subsequent collision with a building. Factors associated with the accident are the flightcrew's inadequate in-flight planning/decision making, which resulted in a low fuel condition; an open hydraulic relief valve, and inadequate maintenance by company maintenance personnel. Additional factors were an inoperative (normal) brake system, an unactivated emergency drag chute, the flightcrew's failure to engage the emergency brake system, and pressure placed on the flightcrew due to conditions/events.
Final Report:

Crash of a Mitsubishi MU-2B-35 Marquise in San Juan: 2 killed

Date & Time: Apr 15, 2002 at 1500 LT
Type of aircraft:
Operator:
Registration:
N45BS
Flight Type:
Survivors:
No
Site:
Schedule:
Christiansted - San Juan
MSN:
558
YOM:
1972
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
10583
Captain / Total hours on type:
768.00
Aircraft flight hours:
7236
Circumstances:
The flight departed VFR, and when near the destination airport, was advised by air traffic control to hold VFR over the "plaza" and to make left 360 degree orbits. Several witnesses reported light rain was occurring at the time of the accident; there was no lightning or thunder. One witness located where the airplane came to rest reported observing the airplane emerge from the base of the clouds in a 45-degree left wing low and 20 degrees nose low attitude. He momentarily lost sight of the airplane but then noted it rolled to a wings level attitude. He also reported hearing the engine(s) "cutting in an out." Another witness located approximately 1/4 mile north of the accident site observed the airplane flying eastbound beneath the clouds in a right wing and nose low attitude, he also reported hearing the engine(s) sounding like they were "cutting in and out." A pilot-rated witness located an estimated 1,000 feet from where the airplane came to rest estimated that the ceiling was at 300 feet and there was light drizzle. He observed the airplane in a 45-degree angle of bank to the right and in a slight nose low attitude. He stated that the airplane continued in that attitude before he lost sight of the airplane at 250 feet. The airplane impacted trees then a concrete wall while in a nose and right wing low attitude. The airplane then traveled through automobile hoists/lifts which were covered by corrugated metal, and came to rest adjacent to a building of an automobile facility. Impact and a post crash fire destroyed the airplane, along with a building and several vehicles parked at the facility. Examination of the airplane revealed the flaps were symmetrically retracted and landing gears were retracted. No evidence of preimpact failure or malfunction was noted to the flight controls. Examination of the engines revealed no evidence of preimpact failure or malfunction; impact and fire damage precluded testing of several engine accessories from both engines. Examination of the propellers revealed no evidence of preimpact failure or malfunction. Parallel slash marks were noted in several of the corrugated metal panels that covered the hoists/lifts, the slashes were noted 25 and 21 inches between them. According to the airplane manufacturer, the 25 inch distance between the propeller slashes corresponds to an airspeed of 123 knots. Additionally, the power-off stall speed at the airplanes calculated weight with the flaps retracted and 48 degree angle of bank was calculated to be 122 knots. Review of NTSB plotted radar data revealed that the pilot performed one 360-degree orbit to the left with varying angles of left bank and while flying initially at 1,300 feet, climbing to near 1,500 feet, then descending to approximately 800 feet. The airplane continued in the left turn and between 1502:10 and 1502:27, the calibrated airspeed decreased from 160 to 100 knots. At 1502:27, the bank angle was 48 degrees, and the angle of attack was 26 degrees. Between 1502:30 and 1502:35, the true heading changed indicating a bank to the right. The last plotted altitude was 200 feet, which occurred at 1502:35. A NTSB weather study indicated that at the area and altitude the airplane was operating, NWS VIP level 1 to 2 echoes (light to moderate intensity) were noted. Additionally, the terminal aerodrome forecast (TAF) for the destination airport indicated that temporarily between 1400 and 1800 (the flight departed at approximately 1436 and the accident occurred at approximately 1503), visibility 5 miles with moderate rain showers, scattered clouds at 1,500 feet, and a broken ceiling at 3,000 feet.
Probable cause:
The failure of the pilot to maintain airspeed (Vs) while maneuvering following inadvertent encounter with clouds resulting in an inadvertent stall and uncontrolled descent and subsequent in-flight collision with trees, a wall, and a building.
Final Report:

Crash of a Cessna 441 Conquest II near Río Grande: 5 killed

Date & Time: Jan 5, 2002 at 1423 LT
Type of aircraft:
Registration:
N441AW
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Culebra – San Juan
MSN:
441-0199
YOM:
1981
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
3609
Captain / Total hours on type:
1494.00
Aircraft flight hours:
5200
Circumstances:
The pilot was on a visual rules flight from Culebra, Puerto Rico to San Juan, Puerto Rico. No flight plan was filed and a weather briefing was not obtained. The pilot contacted San Juan Radar Approach Control 10 miles east of Fajardo, Puerto Rico and the controller stated the airplane was in radar contact 3 miles east of Fajardo airport. The pilot was instructed to enter a right downwind for runway 10 south of plaza Carolina. The pilot acknowledged the transmission and reported he was at 1,600 feet. Two minutes later the controller stated on the radio frequency, radar contact was lost. The airplane was located by ground personnel on the side of El Yunque Mountain. Review of weather data revealed a weak cold front extended over Puerto Rico. Satellite imagery at the time of the accident revealed a band of low clouds obscuring the accident site. A police helicopter pilot who attempted to reach the crash site reported instrument flight conditions. Examination of the airframe, flight controls, engine assemblies and accessories revealed no anomalies.
Probable cause:
The pilot continued visual flight flight into instrument flight conditions resulting in an in-flight collision with terrain. Low clouds were a factor.
Final Report:

Crash of a Cessna 404 Titan II near Pena Pobre: 1 killed

Date & Time: May 13, 2001 at 1933 LT
Type of aircraft:
Operator:
Registration:
N404BA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Christiansted – San Juan
MSN:
404-0237
YOM:
1978
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1000
Captain / Total hours on type:
103.00
Aircraft flight hours:
12000
Circumstances:
The flight was being handled as a VFR aircraft by air traffic control, was given a discreet transponder code, and was radar contact at an altitude of 4,500 feet. The pilot requested a VFR descent from 4,500 feet, and was cleared to "…descend unrestricted west bound." Radar and radio contact were lost at an altitude of 2,700 feet. The controller tried to re-establish radio contact with the airplane's pilot 10 times before initiating search and rescue efforts. A U.S. Coast Guard helicopter found the wreckage, using the aircraft's emergency locator transmitter. The next day a ground search for the aircraft was halted because of hazardous terrain. Search and rescue personnel had to be airlifted into the crash site to remove the victim. A police helicopter was vectored to the crash site by ATC about an 1 1/2 hours after contact was lost with the flight, and the pilot reported that he could not fly near the crash site because of fog. He reported the ceiling about 2,400 feet. The aircraft impacted in heavily wooded, mountainous terrain at the 2,700-foot level of a 3,524-foot mountain. Toxicology test showed that venlafaxine and desmethylvenlafaxine drugs were found in the pilot's blood, and the levels found were consistent with the recent ingestion of more than 10 times a normal dose of venlafaxine.
Probable cause:
Failure of the pilot-in-command to maintain altitude/clearance, resulting in an in-flight collision with rising terrain.
Final Report:

Crash of a Douglas DC-3A-S1C3G off San Juan

Date & Time: Apr 4, 2001 at 1220 LT
Type of aircraft:
Operator:
Registration:
N19BA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
San Juan - San Juan
MSN:
4986
YOM:
1942
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8795
Captain / Total hours on type:
1200.00
Copilot / Total flying hours:
1300
Aircraft flight hours:
39832
Circumstances:
The flight crew stated that while making a missed approach after a practice instrument landing system approach, the right engine failed. The captain took control of the airplane from the copilot. The captain stated that while he performed the emergency procedures for engine failure, he noticed the left engine was not producing power. He then made a forced landing in water east of the airport. He stated that just before impact, he feathered the left propeller. The copilot stated he observed the captain activate the propeller feathering button for the left engine as he performed the emergency procedures for the right engine failure. The reason for failure of the right engine was not determined.
Probable cause:
The captain's activation of the left propeller feathering button after failure of the right engine for undetermined reasons resulting in loss of all engine power and the airplane making a forced landing in water.
Final Report:

Crash of a Cessna 402C II off Vieques: 1 killed

Date & Time: Jul 8, 2000 at 0455 LT
Type of aircraft:
Registration:
N405MN
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
San Juan - Christiansted
MSN:
402C-0221
YOM:
1979
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2400
Captain / Total hours on type:
235.00
Aircraft flight hours:
13702
Circumstances:
After departure from San Juan, the pilot of N405MN contacted the FAA San Juan Approach Control, was identified on radar by the controller, and told to climb to 7,000 feet. About 1 minute later, the pilot is told to proceed direct to St. Croix. About 4 minutes later, the pilot requested radar vectors to St. Croix, and was told to fly heading 140 degrees. Radar data showed the flight leveled at the cruise altitude of 7,000 feet at about 0444. At about 0453:36, the pilot requested a lower altitude, and was cleared to 2,000 feet. The pilot acknowledged the clearance, and no further transmissions were received from the pilot. The flight began descent from 7,000 feet at about 0454. At 0454:29, the aircraft's transponder reports the flight is at 6,500 feet. At 0454:41, the transponder reports the flight is at 5,600 feet, and at 0454:49, at 4,000 feet. At 0454:53, the transponder reports the flight is at 1,100 feet. The flight is not observed on radar after this. No other aircraft or radar returns are observed near the flight as it began it's descent. One main landing gear tire, wheel, and brake assembly; the left wing lower skin from the area above the wing flap; the left wing baggage compartment door; the right nose baggage compartment door; the cabin floor cover; and some items from the U.S. mail cargo, were recovered floating in the ocean, at points north of the last observed radar contact with the airplane, on the day of the accident and in the days after the accident. The recovered components had damage from being separated from the airplane. None of the recovered components had any fire, heat, or soot damage. The remainder of the airplane was not located and recovered. The depth of the sea in the area of the accident site was reported by the Coast Guard to be about 6,000 feet. U.S. Post Office personnel reported the flight carried 1,517 pounds of U.S. mail. No hazardous materials were in the mail. A 75-pound pouch of mail was recovered from the ocean and identified as having been placed on N405MN. The weather at the time of the accident was reported to scattered clouds with visibility 10 miles.
Probable cause:
The airplanes entry into an uncontrolled descent for undetermined reasons from which it crashed into the ocean.
Final Report:

Crash of a Convair CV-240-13 in San Juan

Date & Time: Sep 24, 1998 at 1319 LT
Type of aircraft:
Registration:
N91237
Flight Type:
Survivors:
Yes
Schedule:
San Juan – Santiago de Cuba
MSN:
140
YOM:
1949
Flight number:
TFA237
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7772
Captain / Total hours on type:
1409.00
Aircraft flight hours:
33835
Circumstances:
During the initial takeoff roll, there was a fluctuation of Brake Mean Engine Pressure (BMEPa measurement of engine output) on #2 engine, and the pilot elected to abort the takeoff. The pilot completed two additional engine run-ups, and no abnormalities were noted. During the second attempted takeoff, and as the airplane climbed through 200 feet MSL, a loud bang or back fire from the #2 engine was heard. BMEP fluctuated and dropped showing about 150 BMEP difference with engine #1. The engine oil temperature started to rise rapidly, the engine oil pressure dropped and the airplane started to vibrate. The first officer reduced the #2 engine to 'dry' power, upon which a second bang or backfire was heard from the #2 engine. The #2 propeller was then feathered by the First Officer. Since altitude could not be maintained, the pilot ditched the airplane in the salt water lagoon. An FAA Inspector who examined the crash site noted that the right engine propeller was not fully feathered, and the wing flaps were extended about three degrees.. The airplane was recovered from the water 70 days after the accident. The flight crew completed the engine out emergency procedure in accordance with the prescribed checklist.
Probable cause:
The loss of power in the No. 2 engine for undetermined reasons, and the inability of the pilot to establish a climb and/or maintain altitude. A factor was the incompletely feathered No. 2 propeller.
Final Report:

Crash of a Convair CV-240-53 in San Juan

Date & Time: Jun 30, 1997 at 0745 LT
Type of aircraft:
Registration:
N344MM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
San Juan - Santo Domingo
MSN:
53-26
YOM:
1954
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9000
Captain / Total hours on type:
6970.00
Aircraft flight hours:
24793
Circumstances:
After departing from runway 08, the airplane climbed to 400 feet above ground level (agl) where the left engine lost power. After confirming a loss of power, the pilot feathered the left propeller, and called for maximum 'dry' thrust on the right engine. Wet power was available which would have provided 450 additional horsepower, however, the pilot elected not to use it. The airplane was unable to maintain altitude, collided with a palm tree, and came to rest on the beach in the surf line. The reason for the left engine malfunction was not determined due to salt water damage. The airplane was 600 pounds over maximum weight.
Probable cause:
A loss of engine power for undetermined reasons, the pilot's improper emergency procedure after the power loss, and the overloading of the airplane, resulting in an inability to maintain altitude and terrain clearance.
Final Report: