Crash of a Beechcraft 65-80 Queen Air off New Orleans: 2 killed

Date & Time: Mar 11, 1979 at 1610 LT
Type of aircraft:
Operator:
Registration:
N10QH
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Oklahoma City - Oklahoma City
MSN:
LD-110
YOM:
1963
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
5204
Circumstances:
The twin engine airplane departed Oklahoma City Airport in the late morning on a local check-out flight. En route, the pilot became lost and disoriented, causing the aircraft to fly to the south for few hours until it went low on fuel. The pilot ditched the airplane off New Orleans. A passenger was slightly injured while two other occupants were killed.
Probable cause:
Ditching after the pilot became lost and disoriented. The following contributing factors were reported:
- Improper in-flight decisions,
- Fuel exhaustion,
- Ditching site 835 SM from departure point.
Final Report:

Crash of a Mitsubishi MU-2B-35 Marquise in Searcy

Date & Time: Jan 23, 1979 at 0855 LT
Type of aircraft:
Operator:
Registration:
N5NW
Survivors:
Yes
Schedule:
Oklahoma City – Searcy
MSN:
597
YOM:
1973
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3300
Captain / Total hours on type:
1031.00
Circumstances:
During the last segment on approach to Searcy Municipal Airport, the twin engine airplane stalled and crashed. All three occupants escaped with minor injuries while the aircraft was damaged beyond repair.
Probable cause:
Stall on level off/touchdown after the pilot failed to maintain flying speed. The following contributing factors were reported:
- Failed to initiate go-around,
- Not aligned with runway.
Final Report:

Crash of a Piper PA-31-325 Navajo C/R in Dallas

Date & Time: Dec 20, 1978 at 0711 LT
Type of aircraft:
Operator:
Registration:
N27604
Flight Phase:
Survivors:
Yes
Site:
Schedule:
Dallas - Oklahoma City
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5310
Captain / Total hours on type:
429.00
Circumstances:
After takeoff from Dallas-Love Field Airport, while climbing, one of the engine failed. The pilot elected to return for a safe landing when the aircraft lost height and crashed into residences by the airport. All seven occupants were seriously injured while no one on the ground was injured. The aircraft was destroyed.
Probable cause:
Engine malfunction during initial climb and subsequent collision with residences due to improperly serviced aircraft by ground crew. The following contributing factors were reported:
- Improper fuel grade,
- Operational supervisory personnel: deficiency, company maintained equipment, services, regulation,
- High obstructions,
- Partial loss of power on one engine,
- Complete engine failure one engine,
- Forced landing off airport on land,
- The truck use to refuel the airplane was supposed to be 100LL fuel but contained Jet A fuel,
- The fuel farm tank vent covers were improperly marked.
Final Report:

Crash of a Rockwell Grand Commander 690A in Calumet: 2 killed

Date & Time: May 27, 1978 at 1010 LT
Registration:
N299F
Flight Phase:
Survivors:
No
Schedule:
Oklahoma City - Colorado Springs
MSN:
690-11112
YOM:
1973
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
7000
Captain / Total hours on type:
500.00
Circumstances:
Few minutes after takeoff from Oklahoma City Airport, from climb to cruise, the crew encountered bad weather condition with thunderstorm activity. In severe turbulences, the airplane suffered a general disintegration and crashed in Calumet. The aircraft was totally destroyed and both occupants were killed.
Probable cause:
In-flight airframe failure during climb to cruise due to inadequate preflight preparation. The following contributing factors were reported:
- Initiated flight in adverse weather conditions,
- Exceeded designed stress limits of aircraft,
- Airframe failure of wings spars,
- Airframe failure of flight control surfaces: horizontal stabilizer, attachments,
- Overload failure,
- Separation in flight,
- Low ceiling,
- Thunderstorm activity,
- General disintegration,
- Embedded thunderstorms.
Final Report:

Crash of a Rockwell Grand Commander 690A near Independence: 1 killed

Date & Time: Nov 17, 1976 at 1950 LT
Registration:
N57186
Flight Phase:
Survivors:
No
Schedule:
Kansas City - Oklahoma City
MSN:
690-11186
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10000
Captain / Total hours on type:
980.00
Circumstances:
En route from Kansas City to Oklahoma City, the twin engine airplane was in normal cruise when control was lost. It entered a dive, suffered an overload failure then crashed in an open field. The pilot, sole on board, was killed.
Probable cause:
Airframe failure and fire or explosion in flight for undetermined reasons. The following findings were reported:
- Overload failure,
- Fire in wing,
- Separation in flight,
- Altitude varied between 14,500 and 15,300 feet during last 4 minutes of flight.
Final Report:

Crash of a Rockwell Sabreliner 75 in Watertown

Date & Time: Jun 14, 1975 at 1632 LT
Type of aircraft:
Operator:
Registration:
N67KM
Flight Phase:
Survivors:
Yes
Schedule:
Watertown - Oklahoma City
MSN:
380-7
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
22000
Captain / Total hours on type:
130.00
Circumstances:
Just after liftoff, while climbing, the airplane struck a flock of birds (13 inland seagulls). Both engines flamed out and the airplane lost speed and height. The right wing stalled and struck an installation approach light on T-bar before the airplane crashed in flames 150 meters further. All six occupants were injured and the aircraft was destroyed.
Probable cause:
Engine failure during initial climb due to bird ingestion. The following contributing factors were reported:
- Collision with runway approach lights,
- Hit flock of inland seagulls.
Final Report:

Crash of a Rockwell 1121 Jet Commander in Tullahoma

Date & Time: Mar 13, 1975 at 1440 LT
Operator:
Registration:
N711JT
Survivors:
Yes
Schedule:
Oklahoma City - Tullahoma
MSN:
1121-091
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4300
Captain / Total hours on type:
70.00
Circumstances:
Following an uneventful flight from Oklahoma City, the twin engine airplane landed on runway 36 at Tullahoma-Northern Regional Airport. After touchdown, it was unable to stop within the remaining distance and overran the wet runway before colliding with trees. All seven occupants escaped with various injuries and the aircraft was damaged beyond repair.
Probable cause:
Overshoot runway and collided with trees after the crew delayed in initiating go-around. The following contributing factors were reported:
- Wet runway,
- Hydroplaning on wet runway,
- Touchdown on runway 36 near intersection with runway 24, approximately 2,000 feet remaining.
Final Report:

Crash of a Rockwell Aero Commander 680V in Olathe: 1 killed

Date & Time: Jan 31, 1975 at 1336 LT
Operator:
Registration:
N399T
Survivors:
No
Schedule:
Oklahoma City - Olathe
MSN:
680-1532-2
YOM:
1965
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
18843
Captain / Total hours on type:
800.00
Circumstances:
The approach to Olathe-Johnson County Airport was completed in poor weather conditions due to fog and low clouds. When the pilot passed below the clouds, the airplane was at an altitude of 400 feet just over the runway end. control was lost and the airplane crashed by the runway and was destroyed. The pilot, sole on board, was killed.
Probable cause:
The pilot failed to maintain flying speed on final approach. The following contributing factors were reported:
- Improper IFR operation,
- Failed to initiate a go-around,
- Low ceiling,
- Icing conditions including sleet and freezing rain,
- Fog,
- Moderate airframe icing in area,
- Aircraft observed to break out of overcast about 400 feet over end of runway.
Final Report:

Crash of a Rockwell Sabreliner 40R in Oklahoma City: 2 killed

Date & Time: Jan 15, 1974 at 0600 LT
Type of aircraft:
Operator:
Registration:
N5565
Survivors:
No
Schedule:
Corpus Christi - Oklahoma City
MSN:
282-119
YOM:
1973
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
21500
Captain / Total hours on type:
2000.00
Circumstances:
The approach to Oklahoma City was started in limited visibility due to foggy conditions. On final, the crew descended below the MDA when the airplane struck the ground and crashed in flames few miles short of runway threshold. The aircraft was destroyed by impact forces and a post crash fire and both pilots were killed.
Probable cause:
Controlled flight into terrain following an improper IFR operation on final approach. The following factors were reported:
- Instruments misread or failed to read,
- Poor crew coordination,
- Low ceiling and fog,
- Pilot fatigue,
- ILS approach below minimums,
- Descended below MDA,
- Crew had a little rest before flight,
- ATC did not monitor altitude on radar.
Final Report:

Crash of a Beechcraft 65-B80 Queen Air in Milo: 3 killed

Date & Time: Oct 21, 1971 at 2000 LT
Type of aircraft:
Operator:
Registration:
N317K
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Dallas - Oklahoma City
MSN:
LD-342
YOM:
1967
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
4000
Circumstances:
While cruising by night over State of Oklahoma, the pilot lost control of the airplane that entered a dive. During the descent, the airplane disintegrated and eventually crashed in an open field located near Milo. All three occupants were killed.
Probable cause:
Uncontrolled descent following physical impairment of the pilot. The following factors were reported:
- Spatial disorientation,
- Alcoholic impairment of efficiency and judgment,
- Overload failure,
- Pilot blood alcohol level 1,77 ‰
- Area near total darkness.
Final Report: