Crash of a Cessna 421B Golden Eagle II in Cherokee County: 1 killed

Date & Time: Mar 4, 2017 at 0023 LT
Registration:
N421KL
Flight Type:
Survivors:
No
Schedule:
Tulsa - Cherokee County
MSN:
421B-0015
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4000
Aircraft flight hours:
7522
Circumstances:
The 69-year-old commercial pilot was making a personal cross-country flight in the newly purchased airplane. When the airplane was on final approach to the destination airport in night visual meteorological conditions, airport surveillance video showed it pitch up and roll to the right. The airplane then descended in a nose-down attitude to impact in a ravine on the right side of the runway. During the descent over the ravine the right wing came in contact with a powerline that briefly cut power to the airport. Postaccident examination of the airframe, engines, and their components revealed no evidence of mechanical anomalies or malfunctions that would have precluded normal operation. The pilot's toxicology findings identified five different impairing medications: clonazepam, temazepam, hydrocodone, nortriptyline, and diphenhydramine. Although the results were from cavity blood and may not accurately reflect antemortem levels, the hydrocodone, temazepam, and diphenhydramine levels were high enough to likely have had some psychoactive effects. While the exact effects of these drugs in combination are not known, it is likely that the pilot was impaired to some degree by his use of this combination of medications, which likely contributed to his failure to maintain control of the airplane.
Probable cause:
The pilot's failure to maintain control of the airplane during a night visual landing approach. Contributing to the accident was the pilot's impairment due to his use of a combination of medications.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Foley

Date & Time: Apr 26, 2016 at 1424 LT
Registration:
N3372Q
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Foley - Carrollton
MSN:
421B-0256
YOM:
1972
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5450
Circumstances:
The private pilot of the twin-engine airplane departed on the personal flight. During the takeoff roll, all indications were normal. When the airplane accelerated to between 75 and 80 knots, the pilot pulled back on the yoke slowly, and the airplane began to climb. After he raised the landing gear, the pilot noticed that the airplane was not continuing to climb and that the airspeed was 80 knots; he then heard the stall warning horn. The airplane impacted trees about 1/4 mile from the runway, caught fire, and was destroyed; the pilot egressed with minor injuries. The airplane's published minimum control speed was 86 knots and the break ground and climb speed was 106 knots. Given that information, it is likely that the pilot's attempt to rotate and climb the airplane below 80 knots resulted in the airplane being unable to gain altitude and climb above trees at the end of the runway.
Probable cause:
The pilot's failure to obtain proper takeoff speed before breaking ground, which resulted in the airplane's failure to gain altitude and a collision with trees and terrain.
Final Report:

Crash of a Cessna 421B Golden Eagle II off Sabaneta de Palmas

Date & Time: Apr 1, 2016 at 2200 LT
Operator:
Registration:
HI938
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
421B-0129
YOM:
1971
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While flying by night, the twin engine airplane crashed under unknown circumstances in the lake of Maracaibo and came to rest few dozen metres off Sabaneta de Palmas. There were no casualties but the aircraft was damaged beyond repair.

Crash of a Cessna 421B Golden Eagle II in Hammond: 2 killed

Date & Time: Oct 14, 2015 at 1548 LT
Operator:
Registration:
N33FA
Flight Phase:
Survivors:
No
Schedule:
Hammond - Atlanta
MSN:
421B-0502
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The twin-engine airplane, flown by a commercial pilot, was departing on a business flight from runway 31 when the right engine lost power. According to a pilot-rated witness, the airplane was about halfway down the 6,500 ft runway at an altitude of about 100 ft above ground level when he heard a "loud pop" and then saw the airplane's right propeller slow. The witness reported that the airplane yawed to the right and then began a right turn toward runway 18 with the right engine's propeller windmilling. The witness further reported that the airplane cleared a tree line by about 150 ft, rolled right, descended straight down to ground impact, and burst into flames. Postaccident examination of the airplane's right engine revealed that the crankshaft was fractured adjacent to the No. 2 main bearing, which had rotated. The crankcase halves adjacent to the No. 2 main bearing were fretted where the case through-studs were located. The fretting of the mating surfaces was consistent with insufficient clamping force due to insufficient torque of the through-stud nuts. Records indicated that all six cylinders on the right engine had been replaced at the airplane's most recent annual inspection 8 months before the accident. In order to replace the cylinders, the through-stud nuts had to be removed as they also served to hold down the cylinders. It is likely that when the cylinders were replaced, the through-stud nuts were not properly torqued, which, over time, allowed the case halves to move and led to the bearing spinning and the crankshaft fracturing. During the accident sequence, the pilot made a right turn in an attempt to return to the airport and did not feather the failed (right) engine's propeller, allowing it to windmill, thereby creating excessive drag. It is likely that the pilot allowed the airspeed to decay below the minimum required for the airplane to remain controllable, which combined with his failure to feather the failed engine's propeller and the turn in the direction of the failed engine resulted in a loss of airplane control.
Probable cause:
The loss of right engine power on takeoff due to maintenance personnel's failure to properly tighten the crankcase through-studs during cylinder replacement, which resulted in crankshaft fracture. Also causal were the pilot's failure to feather the propeller on the right engine and his failure to maintain control of the twin-engine airplane while maneuvering to return to the airport.
Final Report: