Crash of a Cessna T303 Crusader in San Diego

Date & Time: May 7, 1999 at 2230 LT
Type of aircraft:
Registration:
N3303S
Flight Type:
Survivors:
Yes
Schedule:
Houston – San Diego
MSN:
303-00018
YOM:
1981
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
25000
Captain / Total hours on type:
200.00
Aircraft flight hours:
1832
Circumstances:
The airplane departed Houston, Texas, for a VFR flight to San Diego, California. The pilot in the left seat said that they originally planned to purchase fuel at Gila Bend, Arizona, but were told that the fueling was closed. The left seat pilot said they elected to land at a private airstrip and made arrangements to have an individual drive to Casa Grande airport to purchase fuel for them. The left seat pilot said they were worried about adequate runway length, so they elected to only purchase 65 gallons of fuel for the remainder of the flight to San Diego. En route to San Diego, the right seat pilot obtained weather for the destination from FSS and was advised of 1,000-foot overcast ceiling. The right seat pilot then requested and received an instrument clearance. The TRACON controller advised the pilot of the accident airplane that he would have to keep speed up due to jet traffic or be given delay vectors for traffic spacing. The pilot told ATC that they were fuel critical and later said they had about 45 minutes to 1 hour of fuel. The right seat pilot was cleared for the localizer runway 27 approach. Approximately 18 minutes later, the pilot elected to do a missed approach because he was too high to land and moments later told San Diego radar that he was fuel critical and only had about 5 minutes of fuel left. San Diego radar began to give the pilot vectors to the closest airport and told the pilot not to descend any further. The right seat pilot replied that they were a glider and later told San Diego police that they had run out of fuel. There were no discrepancies noted with either the airframe or the engines during the postaccident aircraft examination.
Probable cause:
The pilot-in-command's inaccurate fuel consumption calculations that resulted in fuel exhaustion and the subsequent ditching.
Final Report:

Crash of a Cessna T303 Crusader near Nottingham

Date & Time: Jul 16, 1998 at 1833 LT
Type of aircraft:
Registration:
G-BSPF
Flight Type:
Survivors:
Yes
Schedule:
Sheffield – Nottingham
MSN:
303-00100
YOM:
1982
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
290
Captain / Total hours on type:
68.00
Circumstances:
The aircraft was en route from Sheffield City Airport to Nottingham where it was based. The pilot joined the traffic zone at Burton Joyce, an unofficial but well used Visual Reporting Point, at a height of about 1,000 feet. The weather was fine with good visibility and the pilot took the opportunity to view the house of the aircraft's co-owner located in the vicinity of Burton Joyce. While orbiting the house, the pilot felt a moderate 'bumping' sensation which he attributed to thermal activity rather than pre-stall buffet. The left wing suddenly dropped and the aircraft rolled through the vertical. The pilot applied corrective rudder and moved the control column forward which rolled the aircraft erect but he was unable to arrest the rate of descent because the engines did not appear to be developing full power. He therefore elected to carry out a forced landing with the landing gear retracted. On approaching the field, the aircraft struck a telegraph pole, yawed to the left and landed with a very high rate of descent before coming to a halt after a short ground slide. The pilot was unable to evacuate the aircraft because of his injuries but was rescued by local people who were quickly on the scene. There was no fire. The pilot stated that at the time the aircraft departed from normal flight, he was flying at about 100 kt with 60° of bank. The basic stalling speed of the aircraft in the configuration at the time was about 70 kt. Application of the correction for load factor in the turn would have given a stalling speed of 100 kt. The majority of eye witnesses stated that the aircraft was very low at the point at which it departed from normal flight, probably in the region of 300 feet above ground level.
Final Report:

Crash of a Cessna T303 Crusader in Midvale: 6 killed

Date & Time: Mar 2, 1998 at 1805 LT
Type of aircraft:
Registration:
N727RT
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Boise - Boise
MSN:
303-00090
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
7743
Captain / Total hours on type:
319.00
Aircraft flight hours:
1675
Circumstances:
Radar data indicated that the aircraft completed a figure-eight maneuver at about 3,000 feet AGL, with an estimated airspeed of 140 knots and approximate 40 degree bank angle before leveling out at the completion of the maneuver. The radar data then indicated level flight before a rapid descent. A witness reported observing the aircraft in visual conditions and flying at a high altitude and that it 'appeared fast.' The witness stated that he observed the aircraft make a wide, shallow left turn, then turn back the other way. The nose of the aircraft then started to gradually lower, and the airplane eventually came straight down and started to spin. The witness lost sight of the airplane behind hilly terrain and he did not see the impact. Postaccident examination of the wreckage indicated that the aircraft collided with the terrain in a slight nose-down attitude, located in a gully with approximate 30 degree bank angle. The aircraft then slid downhill to the right and came to rest with the fuselage upright and the empennage was twisted to the right and inverted. No evidence was found to indicate a mechanical failure or malfunction.
Probable cause:
The pilot's failure to maintain aircraft control.
Final Report:

Crash of a Cessna T303 Crusader in Rogers: 2 killed

Date & Time: Nov 25, 1993 at 1804 LT
Type of aircraft:
Registration:
N2297C
Flight Type:
Survivors:
No
Schedule:
Arlington - Rogers
MSN:
303-00093
YOM:
1982
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1786
Captain / Total hours on type:
907.00
Aircraft flight hours:
1450
Circumstances:
The instrument rated private pilot departed on a night ifr cross country flight into forecasted icing conditions. During the approach at his destination airport, the pilot requested lower altitude to attempt to breakout from the weather. After being assigned 3,100 feet and obtaining a clearance for the ILS approach, the pilot cancelled ifr during descent and proceeded visually for the airport. The aircraft operated in an area of reported freezing rain and ice pellets, with fog and drizzle. Control was lost during the turn from base to final approach. Both occupants were killed.
Probable cause:
The pilot's continued flight into known adverse weather conditions, and the ensuing inadvertent stall. Factors were the icing conditions, the fog, the drizzle, the dark night light conditions, and the pilot's disregard for the forecasted weather conditions.
Final Report:

Crash of a Cessna T303 Crusader in Prescott: 5 killed

Date & Time: Jul 4, 1993 at 0320 LT
Type of aircraft:
Operator:
Registration:
N9667C
Flight Type:
Survivors:
No
Schedule:
Prescott - Prescott
MSN:
303-00200
YOM:
1982
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
550
Captain / Total hours on type:
40.00
Aircraft flight hours:
3123
Circumstances:
On July 4, 1993, about 0320 hours mountain standard time, a Cessna T303, N9667C, collided with terrain about 2,000 feet short of the approach end of runway 21 at Ernest A. Love Field in
Prescott, Arizona. The airplane was destroyed. The commercial pilot and four passengers were fatally injured. The airplane was being operated as a personal flight. The local flight departed Love Field about two minutes before the accident. Night visual meteorological conditions prevailed at the time. The accident airplane arrived at Love Field about 2300 hours on July 3, 1994. An airport operations specialist employed by the City of Prescott greeted the airplane to see if the pilot needed fuel. Three males got out of the airplane, one of which was carrying a can of beer. One occupant of the airplane replied to the operations specialist fuel inquiry and stated, "Not right now, maybe later or in the morning." The operations specialist asked the three men if they had a place to stay and they indicated they were meeting friends. The night manager of the Airport Centre Motel, located off the west boundary of Love Field, noticed the three men walking from the airport 2330 hours on July 3, 1994. The motel manager stated all three men were drinking beverages from cans. The manager was unable to state the type of beverages they were drinking. At 2300 hours, July 3, 1994, the girl friend of one of the airplane's passengers received a call from her boy friend requesting a ride from Love Field to "downtown" Prescott. The girlfriend met her boy friend with two other friends. According to the girl friend, all three men were holding beer cans. The girl friend dropped the men off in the downtown area with plans to meet later. Approximately 0100 hours July 4, 1993, three females were leaving the Palace Saloon in downtown Prescott. The women were approached by three men on the sidewalk. One of the men identified himself as a pilot to the women. One of the women did not believe him and being associated with pilots in the past she asked him, "How many hours do you need [from] bottle to throttle?" The pilot responded, "Eight, but I guess I will have to break that rule tonight." The six walked on the sidewalk continuing the conversations. The woman who previously challenged the pilot walked along side him. She described him as quiet, friendly, not intoxicated, and at one point apologetic for being quiet. The pilot expounded on his quietness by stating he was very tired, and that he had been in Laughlin, Nevada, the night before, worked all day, rented the airplane, and then flew to Prescott. As the evening progressed, the group went to a restaurant, ate, and walked to the women's hotel. The men solicited a ride to the airport and the women agreed. During the ride to the airport, two of the men were talkative but the pilot remained quiet. The pilot was observed closing his eyes with his head back. The group arrived at the airport about 0245 hours. The men offered to show the women the airplane. The pilot opened the airplane and moved into the cockpit. The woman, who earlier challenged the pilot, asked one of the other men, "Why is the pilot so quiet, is he drunk?" The other man said, "No, he only had a few drinks." The woman then heard the pilot and the other man talking in the cockpit. The pilot was trying to turn on the pilot-controlled airport lighting. The woman heard the other man tell the pilot to "stop clicking the button so many times, and that it was supposed to be three clicks and then stop." The men then offered the women a 10-minute ride in the airplane. The woman who earlier challenged the pilot refused. Her two friends accepted and got into the airplane and she went back to their vehicle and waited. At 0254 hours, the pilot contacted the Prescott Flight Service Station (FSS) on frequency 122.4 Mhz and asked about the pilot- controlled lighting system. The pilot indicated that he tried to activate the lights but was unsuccessful. After consulting the Airport/Facility Directory, the air traffic control (ATC) specialist informed the pilot the lights were pilot activated on frequency 125.3 Mhz. The ATC specialist then heard seven "clicks" on 122.4 Mhz. He advised the pilot that he was still on 122.4 Mhz. The pilot replied, "Thank you, sir, we got 'em." At 0259 hours, the ATC specialist asked the pilot if he needed any further assistance. The pilot indicated that further assistance was not needed. The ATC specialist then issued the Prescott altimeter setting, 29.92 inHg, and asked the pilot if he had the flight precaution for turbulence. The pilot responded he did not. The ATC specialist issued AIRMET Tango for occasional moderate turbulence below 20,000 feet. The pilot then acknowledged he had received it. There were no further communications between the pilot and the Federal Aviation Administration ATC specialist. FAA radar data from Albuquerque Center tracked a single aircraft in the Love Field traffic pattern at 0319 hours. The radar data listed ten positions corresponding to right traffic off runway 21. The radar data indicates the tracked airplane reached an altitude of 6,500 feet mean sea level (msl), or about 1,500 feet above the ground.
Probable cause:
The pilot misjudging distance and altitude during a night approach. Factors which contributed to the accident were: the pilot's impairment due to fatigue exacerbated by alcohol consumption, the dark night, and the high density altitude and turbulent weather condition.
Final Report:

Crash of a Cessna T303 Crusader on Mt Piz Ault: 5 killed

Date & Time: Feb 21, 1993 at 1037 LT
Type of aircraft:
Operator:
Registration:
D-IBCT
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Lugano - Bielefeld
MSN:
303-00207
YOM:
1983
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
3296
Captain / Total hours on type:
650.00
Aircraft flight hours:
1361
Circumstances:
The twin engine aircraft departed Lugano-Agno Airport at 1037LT on a private flight to Bielefeld, carrying four passengers and one pilot. The aircraft continued to the north and climbed to the assigned altitude of 15,000 feet that was maintained until over Ambri. Then, the aircraft lost 500 feet and its speed varied between 150 and 95 knots. ATC instructed the pilot to climb to FL150 when three minutes later, the aircraft lost 800 feet then disappeared from radar screens. The wreckage was found two days later on the southern slope of Mt Piz Ault, Graubünden. The aircraft was totally destroyed by impact forces and all five occupants were killed. At the time of the accident, weather conditions were poor with a northerly wind gusting to 50 knots and a visibility reduced to 200 metres due to snow falls. Severe icing conditions were reported with significant atmospheric turbulences on airway A9.
Probable cause:
The accident was the consequence of the following:
- Wrong estimation of weather conditions on part of the pilot actualized in the Alps area,
- The pilot decided to continue the flight into weather conditions that exceeded the aircraft's power and the pilot's capabilities,
- The total weight of the aircraft was 210 lbs above the maximal permissible weight,
- It is possible that the pilot's attention was diverted because a non fixed GPS system was turning around in the cockpit due to turbulences.
Final Report:

Crash of a Cessna T303 Crusader in The Channel

Date & Time: May 1, 1992 at 1754 LT
Type of aircraft:
Operator:
Registration:
G-BPZV
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Exeter - Guernsey
MSN:
303-00006
YOM:
1981
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
756
Captain / Total hours on type:
77.00
Circumstances:
The aircraft had departed Exeter on a flight to Guernsey when, during the climb to FL35, a slight smell of fumed was noticed in the cockpit. By the time the aircraft had passed SKERRY, by some four to five nm, smoke was seen coming from under the right hand instrument panel. The pilot asked the passenger to investigate the source, but he reported that he could see no burning. The pilot then informed Jersey control of their situation and advised that he was returning direct to Start Point, the nearest land on the coast. After changing to Exeter Radar, the pilot initiated a descent in case an immediate ditching should prove necessary, and briefed his passenger to don a life-jacket. He also directed the passenger to sit at the rear of the cabin, adjacent to the door, so that he would be ready to deploy the life-raft through the upper half of the door if they had to ditch. As the density of the smoke and fumes increased, the pilot elected to carry out a controlled ditching, fearing that if he tried to reach the coast he would be overcome by the fumes. However, he stated that he was reluctant to open the cabin air vents in case this escalated any hidden fire, and he did not turn off the master switch since he required the radios to maintain contact with Exeter Radar. The pilot transmitted a Mayday call, giving a full position report, and at 200 feet amsl he shut down both engines and feathered the propellers. He estimated the sea-well was between eight and ten feet but, since a strong wind was blowing (20 knots), he decided to land into-wind. The aircraft contacted the water at approximately 70 knots, plunging into a swell which generated an impact which the pilot later described as 'tremendous'.The aircraft, however, floated for some one and a half minutes before sinking, enabling both occupants to safely escape from the rear door. The pilot reported that, once in the water, it took them an estimated 20 minutes to get the life-raft inflated, but their life-jackets provided adequate support during this period. Although the pilot advised that flares and a handheld radio were being carried on board the aircraft, these were lost during the ditching. After approximately 45 minutes, an SAR helicopter from RAF Chivenor arrived on scene, recovered both survivors, and took them to hospital in Exeter. The pilot, who was wearing a lap and diagonal restraint, and the passenger, who was wearing only a lap strap, were largely uninjured.
Probable cause:
Since the aircraft was not recovered, it was not possible to establish the source of the smoke which issued from below the right instrument panel.
Final Report:

Crash of a Cessna T303 Crusader in DeLand

Date & Time: May 28, 1990 at 0803 LT
Type of aircraft:
Registration:
N4973V
Flight Type:
Survivors:
Yes
Schedule:
Daytona Beach - DeLand
MSN:
303-00285
YOM:
1984
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1520
Captain / Total hours on type:
100.00
Aircraft flight hours:
2542
Circumstances:
During an NDB approach in instrument conditions with the landing gear extended, the fire warning light for the right engine illuminated. The right engine was shut down and a missed approach was initiated; however, the landing gear would not retract and the aircraft would not maintain altitude. As it descended into the top of an overcast at an altitude of about 600 feet, the pilots tried to restart the engine, but to no avail. Subsequently, the aircraft descended below the clouds at an altitude of about 150 feet to 170 feet. As the instructor (cfi) landed the aircraft in an open field, the nose gear encountered soft dirt and the aircraft nosed over. An exam revealed that an electrical power jumper wire between 2 bus bars had become chafed and shorted. The left and right isolation circuit breakers and the bus tie circuit breaker were found in the tripped (open) position. This resulted in a false fire warning light and prevented the landing gear from being retracted.
Probable cause:
The chafed and shorted electrical wiring between bus bars, which caused a partial electrical failure, resulted in a false fire warning indication, and prevented the restart of the right engine.
Final Report:

Crash of a Cessna T303 Crusader near Englewood: 2 killed

Date & Time: Jan 11, 1988 at 2010 LT
Type of aircraft:
Registration:
N9565T
Flight Phase:
Survivors:
No
Site:
Schedule:
Englewood - El Paso
MSN:
303-00027
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4550
Captain / Total hours on type:
42.00
Aircraft flight hours:
1070
Circumstances:
The pilot obtained two weather briefings and filed an IFR flight plan to El Paso, TX. He was not instrument rated. The aircraft departed Englewood at 1959 and disappeared from radar at 2010. The crash site was 11- 1/2 miles southeast of the Kiowa vortac and 36 miles southeast of Englewood. Radar showed a 15-miles wide band of snow showers southeast of the Kiowa vortac. Ground witnesses reported blizzard conditions. Pilot medical certificate stated, 'not valid for night flight or by color control.' Pilot autopsy also disclosed 'myxomatous alteration of the mitral valve, consistent with mitral valve prolapse (floppy mitral valve).' Both occupants were killed.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: cruise - normal
Findings
1. (f) light condition - dark night
2. (c) flight into known adverse weather - initiated - pilot in command
3. (f) self-induced pressure - pilot in command
4. (f) lack of total instrument time - pilot in command
5. (f) weather condition - high wind
6. (f) weather condition - gusts
7. (f) weather condition - snow
8. (f) weather condition - obscuration
9. (f) weather condition - turbulence
----------
Occurrence #2: loss of control - in flight
Phase of operation: maneuvering
Findings
10. (c) spatial disorientation - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
11. Terrain condition - snow covered
Final Report: