Crash of a Cessna 650 Citation VII in Guarda-Mor: 4 killed

Date & Time: Nov 10, 2015 at 1904 LT
Type of aircraft:
Operator:
Registration:
PT-WQH
Flight Phase:
Survivors:
No
Schedule:
Brasília – São Paulo
MSN:
650-7083
YOM:
1998
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
13143
Copilot / Total flying hours:
2527
Copilot / Total hours on type:
1633
Circumstances:
The aircraft took off from the Presidente Juscelino Kubitschek (SBBR) Aerodrome, Brasília - DF, to the Congonhas Aerodrome (SBSP), São Paulo - SP, at 2039 (UTC), to carry out a personnel transportation flight with two crewmembers and two passengers on board. During the cockpit preparation procedure, the crew members commented about the operation of the Pitch Trim System. The first flight of the day, that occurred in the morning, was from São Paulo to Brasilia and with no abnormalities. About thirty minutes after take-off from Brasília, still during the climb, near the FL370, the cabin voice recorder recorded a characteristic sound of the aircraft’s horizontal stabilizer moving. Then, the aircraft made a downward trajectory with high speed and a big rate of descent until the impact against the ground. The aircraft was destroyed. All occupants perished at the site, among them Lúcio Flávio de Oliveira and Marco Antonio Rossi, two Directors of Banco Brasdesco.
Probable cause:
Contributing factors:
- Control skills – undetermined
It is possible that, after inadvertent movement of the horizontal stabilizer, the crewmembers did not operate on the control switches of the secondary pitch trim system, since no other warning sound (Clacker) was recorded on the CVR recordings. The action prevised in the emergency procedures Pitch Trim Runaway or Failure, item 3, regarding trimming of the aircraft through the secondary system, possibly, was not performed. The performance of the crew may have been restricted only to the elevator control on the aircraft controls or to the control of the stabilizer associated with the primary trimming mode.
- Attitude – undetermined
The decision to make the flight without the proper functioning of the primary pitch trim and autopilot system may have been the result of the pilot's self-confidence because of the successful previous flight under similar operating conditions. Considering the hypothesis that the updated Shutdown Checklist, which should incorporate the Stabilizer Trim Backdrive Monitor - TEST, was not performed after the precrash flight, one could consider that there was a lack of adhesion to the aircraft operating procedures. Such an attitude could be associated with the pilot's self-confidence about the aircraft's operating routine, whose acquired experience could have given him the habit of ignoring some of the procedures deemed less important during the flight completion phase.
- Crew Resource Management – a contributor
Throughout the flight, there was an absence of verbalization and communication of the actions on the checklist. Similarly, in the face of the emergency situation of the horizontal stabilizer (Pitch Trim Runaway or Failure), no statements were identified regarding the actions required to manage this situation among the crew. These characteristics denote inefficiency in the use of human resources available for the aircraft operation.
- Training – undetermined
It is possible that the absence of a periodic training in simulator, especially the emergency Pitch Trim Runway or Failure, has affected the performance of the crew, as far as the CVR did not record statements related to the actions required by the abnormal condition experienced.
- Organizational culture – undetermined
The operator did not usually properly fill out the PT-WQH flight logbook. This condition evidenced the existence of informal rules regarding the monitoring of the operational conditions of the aircraft. In this context, it is possible that the history of failures related to the pitch trim system has not been registered.
- Piloting judgment – undetermined
Moments prior to takeoff, it was recorded in the CVR speeches related to the flight without the autopilot, possibly related to a failure or inoperativeness of the primary pitch trim system. The takeoff with a possible failure in the pitch trim system of the aircraft, showed an inadequate assessment of the risks involved in the operation under those conditions.
- Aircraft maintenance – undetermined
It was not possible to establish a link between the maintenance services performed on the aircraft in September 2015 and the events that resulted in the accident occurred on 10NOV2015. However, it was not ruled out that an incomplete crash survey was carried out in the pitch trim system of the aircraft, due to the lack of detail of the service orders.
- Decision-making process – a contributor
The sounds related to the test positions of the Rotary Test Switch have not been recorded in the CVR recording, so it is possible to conclude that the Warning Systems - Check item of the Cockpit Preparation Checklist has not been performed. The decision to perform the flight without the complete execution of all items of the Cockpit Preparation Checklist, prevented the correct verification of the primary longitudinal Trim system of the aircraft and reflected an inadequate judgment about the risks involved in that operation.
- Interpersonal relationship – undetermined
According to the CVR data, there was a possible rush of the crew to take-off, even though it was verified that the aircraft's pitch trim system did not work properly. It was not possible to determine if this rush was motivated by passengers’ pressure or self-imposed by the pilot.
- Support systems – undetermined
It is possible that the Pilots' Abbreviated Checklist - NORMAL PROCEDURES, aboard the aircraft, was outdated, without the incorporation of the Stabilizer Trim Backdrive Monitor - TEST procedure in the Shutdown Checklist. The possible completion of Shutdown Checklist with outdated procedures would have hampered the manufacturer's suggested verification for identification of abnormalities in the aircraft's pitch trim system.
- Managerial oversight – undetermined
The records and control of the operational check flights, both by the maintenance shop and by the operator, prevised in documentation issued by the manufacturer (SB650- 27-53 and ASL650-55-04) were not performed in an adequate manner, indicating possible weaknesses in the supervision of the maintenance activities.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Weston

Date & Time: Oct 26, 2015 at 1233 LT
Operator:
Registration:
N55GK
Survivors:
Yes
Schedule:
Jacksonville – Fort Lauderdale
MSN:
31-7852013
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11000
Captain / Total hours on type:
105.00
Aircraft flight hours:
6003
Circumstances:
The airline transport pilot of the multiengine airplane had fueled the main (inboard) fuel tanks to capacity before the cross-county flight. As the flight approached the destination airport, an air traffic controller instructed the pilot to turn right for a visual approach, and the pilot acknowledged. Subsequently, the pilot reported that he might have to land on a highway. The airplane impacted a marsh area about 15 miles from the destination airport. Review of data downloaded from an onboard engine monitor revealed that the right engine momentarily lost and regained power before experiencing a total loss of power. Examination of the wreckage revealed that the left propeller was feathered and that the right propeller was in the normal operating range. Sufficient fuel to complete the flight was drained from the left wing fuel tanks. Although the right wing fuel tanks were compromised during the impact, sufficient fuel was likely present in the right main fuel tanks to complete the flight before impact because both the left and right main fuel tanks were fueled to capacity concurrently before the flight, but it likely was in a low fuel state due to fuel used during the flight. The right wing main fuel tank was not equipped with a flapper valve, which should have been located on the baffle nearest the wing root where the fuel pickup was located. The flapper valve is used to trap fuel near the fuel pickup and prevent it from flowing outboard away from the pickup. The maintenance records did not indicate that the right main fuel tank bladder had been replaced; however, the manufacture year printed on the bladder was about 20 years before the accident and 16 years after the manufacture of the airplane, indicating that the bladder had been replaced at some point. When the right main fuel tank bladder was replaced, the flapper valve would have been removed. Based on the evidence, it is likely that maintenance personnel failed to reinstall the flapper valve after installing the new fuel bladder. This missing valve would not affect operation of the fuel system unless the right main fuel tank was in a low fuel state, when fuel could flow outboard away from the fuel pickup (such as in a right turn, which the pilot was making when the engine lost power), and result in fuel starvation to the engine.Toxicology testing of the pilot revealed that his blood alcohol level during the flight was likely between 0.077 gm/dl and 0.177 gm/dl, which is above the level generally considered impairing. Therefore, it is likely that, during the right turn, the fuel in the right main fuel tank moved outboard, which resulted in fuel starvation to the right engine. When the right engine lost power, the pilot should have secured the right engine by feathering the propeller to reduce drag and increase single-engine performance; however, given the position of the propellers at the accident site, the pilot likely incorrectly feathered the operating (left) engine, which rendered the airplane incapable of maintaining altitude. It is very likely that the pilot's impairment due to his ingestion of alcohol led to his errors and contributed to the accident.
Probable cause:
The pilot's feathering of the incorrect propeller following a total loss of right engine power due to fuel starvation, which resulted from maintenance personnel's failure to reinstall the flapper valve in the right main fuel tank. Contributing to the accident was the pilot's impairment due to alcohol consumption.
Final Report:

Crash of a Learjet 31A in Apaseo el Alto: 4 killed

Date & Time: Oct 22, 2015 at 1528 LT
Type of aircraft:
Operator:
Registration:
XB-GYB
Flight Phase:
Survivors:
No
Schedule:
Toluca - Zacatecas
MSN:
31-166
YOM:
1998
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Copilot / Total flying hours:
2693
Aircraft flight hours:
3237
Aircraft flight cycles:
2368
Circumstances:
The aircraft departed Toluca Airport at 1528LT on an executive flight to Zacatecas, carrying two passengers and two pilots. Four minutes later, the crew was cleared to climb to FL380 and later reported moderate but continue turbulences. Then the aircraft entered an uncontrolled descent and disintegrated in the air before crashing near Apaseo el Alto. Debris were found on a large area and all four occupants were killed.
Probable cause:
Due to lack of evidences, the exact cause of the loss of control could not be determined.
Final Report:

Crash of a Comp Air CA-8 in Ray

Date & Time: Oct 15, 2015 at 1810 LT
Type of aircraft:
Operator:
Registration:
N224MS
Survivors:
Yes
Schedule:
Anniston - Ray
MSN:
0652843
YOM:
2006
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
948
Captain / Total hours on type:
49.00
Circumstances:
The private pilot reported that, while on a left downwind in the airport traffic pattern after conducting a cross-country business flight, he extended the flaps 10 degrees. While on short final, he fully extended the flaps, and shortly after, the left wing dropped. The pilot attempted to correct the left wing drop by applying right aileron and rudder; however, the airplane did not respond. The pilot chose to conduct a go-around and increased engine power. The airplane subsequently pitched up, and the left turn steepened. The pilot subsequently reduced engine power, and the airplane began to descend. The airplane struck the ground short of the runway, and the left wing separated from the fuselage. The examination of the airframe, flight controls, and engine revealed no preimpact mechanical anomalies that would have precluded normal operation. Examination of the trim system revealed that the right aileron trim and the left rudder trim were in positions that would have resulted in a right turn and a left yaw. Further, a witness reported that the airplane appeared to be in a cross-controlled attitude while on final approach to the airport. It is likely that the pilot’s improper use of the trim led to a cross-controlled situation and resulted in the subsequent stall during the attempted go-around.
Probable cause:
The pilot's improper use of the trim, which created a cross-controlled situation and resulted in an aerodynamic stall during the attempted go-around.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Hammond: 2 killed

Date & Time: Oct 14, 2015 at 1548 LT
Operator:
Registration:
N33FA
Flight Phase:
Survivors:
No
Schedule:
Hammond - Atlanta
MSN:
421B-0502
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The twin-engine airplane, flown by a commercial pilot, was departing on a business flight from runway 31 when the right engine lost power. According to a pilot-rated witness, the airplane was about halfway down the 6,500 ft runway at an altitude of about 100 ft above ground level when he heard a "loud pop" and then saw the airplane's right propeller slow. The witness reported that the airplane yawed to the right and then began a right turn toward runway 18 with the right engine's propeller windmilling. The witness further reported that the airplane cleared a tree line by about 150 ft, rolled right, descended straight down to ground impact, and burst into flames. Postaccident examination of the airplane's right engine revealed that the crankshaft was fractured adjacent to the No. 2 main bearing, which had rotated. The crankcase halves adjacent to the No. 2 main bearing were fretted where the case through-studs were located. The fretting of the mating surfaces was consistent with insufficient clamping force due to insufficient torque of the through-stud nuts. Records indicated that all six cylinders on the right engine had been replaced at the airplane's most recent annual inspection 8 months before the accident. In order to replace the cylinders, the through-stud nuts had to be removed as they also served to hold down the cylinders. It is likely that when the cylinders were replaced, the through-stud nuts were not properly torqued, which, over time, allowed the case halves to move and led to the bearing spinning and the crankshaft fracturing. During the accident sequence, the pilot made a right turn in an attempt to return to the airport and did not feather the failed (right) engine's propeller, allowing it to windmill, thereby creating excessive drag. It is likely that the pilot allowed the airspeed to decay below the minimum required for the airplane to remain controllable, which combined with his failure to feather the failed engine's propeller and the turn in the direction of the failed engine resulted in a loss of airplane control.
Probable cause:
The loss of right engine power on takeoff due to maintenance personnel's failure to properly tighten the crankcase through-studs during cylinder replacement, which resulted in crankshaft fracture. Also causal were the pilot's failure to feather the propeller on the right engine and his failure to maintain control of the twin-engine airplane while maneuvering to return to the airport.
Final Report:

Crash of a Hawker 800XP in Port Harcourt

Date & Time: Jun 8, 2015 at 1916 LT
Type of aircraft:
Registration:
N497AG
Survivors:
Yes
Schedule:
Abuja – Port Harcourt
MSN:
258439
YOM:
1999
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4180
Captain / Total hours on type:
2752.00
Copilot / Total flying hours:
16744
Copilot / Total hours on type:
147
Aircraft flight hours:
8447
Aircraft flight cycles:
6831
Circumstances:
On 11th June, 2015, at about 18:25 h, an HS-125-800XP aircraft with nationality and registration marks N497AG, operated by SWAT Technology Limited departed Nnamdi Azikiwe International Airport, Abuja (DNAA) for Port Harcourt International Airport (DNPO) as a charter flight on an Instrument Flight Rule (IFR) flight plan. There were five persons on board inclusive of three flight crew and two passengers. The Captain was the Pilot Flying while the Co-pilot was the Pilot Monitoring. At 18:48 h, N497AG established contact with Lagos and Port Harcourt Air Traffic Control (ATC) units cruising at Flight Level (FL) 280. At 18:55 h, the aircraft was released by Lagos to continue with Port Harcourt. Port Harcourt cleared N497AG for descent to FL210. At 19:13 h, the crew reported field in sight at 6 nautical miles to touch down to the Tower Controller (TC). TC then cleared the aircraft to land with caution “runway surface wet”. The crew experienced light rain at about 1.3 nautical miles to touch down with runway lights ON for the ILS approach. At about 1,000 ft after the extension of landing gears, the PM remarked ‘Okay...I got a little rain on the windshield’ and the PF responded, ‘We don’t have wipers sir... (Laugh) Na wa o (Na wa o – local parlance, - pidgin, for expression of surprise). From the CVR, at Decision Height, the PM called out ‘minimums’ while the PF called back ‘landing’ as his intention. The PM reported that the runway edge lights were visible on the left side. On the right side, it was missing to a large extent and only appeared for about a quarter of the way from the runway 03 end. The PM observed that the aircraft was slightly to the left of the “centreline” and pointed out “right, right, more right.” The PM further stated that at 50 ft, the PF retarded power and turned to the left. At 40 ft, the PM cautioned the PF to ‘keep light in sight don’t go to the left’. At 20 ft, the PM again said, ‘keep on the right’. PF replied, ‘Are you sure that’s not the centre line?’. At 19:16 h, the aircraft touched down with left main wheel in the grass and the right main wheel on the runway but was steered back onto the runway. The PF stated, “...but just on touchdown the right-hand lights were out, and in a bid to line up with the lights we veered off the runway to the left”. The nose wheel landing gear collapsed, and the aircraft stopped on the runway. The engines were shut down and all persons on board disembarked without any injury. From the CVR recordings, the PF told the PM that he mistook the brightly illuminated left runway edge lights for the runway centreline and apologized for the error of judgement for which the PM responded ‘I told you’. The aircraft was towed out of the runway and parked at GAT Apron at 21:50 h. The accident occurred at night in light rain.
Probable cause:
The accident was the consequence of a black hole effect disorientation causing low-level manoeuvre into grass verge.
The following contributing factors were identified:
- Most of the runway 21 right edge lights were unserviceable at landing time.
- Inadequate Crew Resource Management during approach.
Final Report:

Crash of a Cessna 421A Golden Eagle I in Monterrey

Date & Time: May 21, 2015
Type of aircraft:
Operator:
Registration:
XB-MTC
Flight Phase:
Survivors:
Yes
Schedule:
Monterrey – Piedras Negras
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after take off from Monterrey-Del Norte Airport, while climbing, the pilot encountered unknown technical problems and attempted an emergency landing in the Seventh Military Zone of the Secretary of the National Defense located west of the airport. The aircraft crashed in a pasture and came to rest upside down, bursting into flames. All five occupants were quickly rescued by military personal while the aircraft was partially destroyed by fire.

Crash of a Canadair CL-601-3A Challenger in Marco Island

Date & Time: Mar 1, 2015 at 1615 LT
Type of aircraft:
Operator:
Registration:
N600NP
Survivors:
Yes
Schedule:
Marathon – Marco Island
MSN:
3002
YOM:
1983
Crew on board:
3
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8988
Captain / Total hours on type:
844.00
Copilot / Total flying hours:
18500
Copilot / Total hours on type:
1500
Aircraft flight hours:
15771
Circumstances:
Earlier on the day of the accident, the pilot-in-command (PIC) and second-in-command (SIC) had landed the airplane on a 5,008-ft-long, asphalt-grooved runway. After touchdown with the flaps fully extended, the ground spoilers and thrust reversers were deployed, and normal braking occurred. The PIC, who was the flying pilot, and the SIC subsequently departed on an executive/corporate flight with a flight attendant, the airplane owner, and five passengers onboard. The PIC reported that he flew a visual approach to the dry, 5,000-ft-long runway while maintaining a normal glidepath at Vref plus 4 or 5 knots at the runway threshold with the flaps fully extended. He added that the touchdown was "firm" and between about 300 to 500 ft beyond the aiming point marking. After touchdown, the PIC tried unsuccessfully to deploy the ground spoilers. He applied "moderate" brake pressure when the nose landing gear (NLG) contacted the runway, but felt no deceleration. He also attempted to deploy the thrust reversers without success. The PIC then informed the SIC that there was no braking energy, released the brakes, and turned off the antiskid system. He then reapplied heavy braking but did not feel any deceleration, and he again tried to deploy the thrust reversers without success. He maintained directional control using the nosewheel steering and manually modulated the brakes. However, the airplane did not slow as expected. While approaching the runway end and realizing that he was not going to be able to stop the airplane on the runway, the PIC intentionally veered the airplane right to avoid water ahead. However, the airplane exited the runway end into sand, and the NLG collapsed. The airplane then came to rest about 250 ft past the departure end of the runway. The passengers exited the airplane, and shortly after, airport personnel arrived and rendered assistance. The airplane owner, who was a passenger in the cabin, stated that he left his seat and moved toward the cabin door when he realized that the airplane would not stop on the runway, and he sustained serious injuries. Examination of the airplane revealed that there was minimal pressure at the No. 2 (left inboard) brake due to failure of a spring in the upper brake control valve (BCV), and the coupling subassembly of the No. 1 wheel speed sensor (WSS) was fractured. A representative from the airplane manufacturer reported that, during certification of the brake system, the failure of the BCV spring was considered acceptably low and would be evident to flight crewmembers within five landings of the failure. Because the airplane did not pull while braking during the previous landing earlier that day to a similar length runway, the spring likely failed during the accident landing. Although the PIC was unable to manually deploy the ground spoilers and thrust reversers during the landing roll, they functioned normally during the landing earlier that day and during postaccident operational testing and examination, with no systems failures or malfunctions noted. Additionally, there were no malfunctions or failures with the weight-onwheels system found during postaccident examinations that would have precluded normal operation. Therefore, the PIC's unsuccessful attempts to deploy the ground spoilers and thrust reversers were likely due to errors made while multitasking when presented with an unexpected situation (inadequate deceleration) with little runway remaining. Airplane stopping distance calculations based on the airplane's reported weight, weather conditions, calculated and PIC-reported Vref speed, flap extension, and estimated touchdown point (300 to 500 ft beyond the aiming point marking as reported by the PIC and SIC and corroborated by security camera footage) and assuming the nonuse of the ground spoilers and thrust reversers, operational antiskid and steering systems, and the loss of one brake per side (symmetric half braking) showed that the airplane would have required 690 ft of additional runway; under the same conditions but with thrust reversers used, the airplane still would have required 27 ft of additional runway. Even though there were no antiskid failure annunciations, the PIC switched off the antiskid system, which led to the rupture of the Nos. 1, 3, and 4 tires and likely fractured the No. 1 WSS's coupling subassembly, both of which would have further contributed to the loss of braking action. Therefore, the combination of the failure of a spring in the No. 2 brake's upper BCV and the fracture of the coupling subassembly of the No. 1 WSS, the pilot's failure to attain the proper touchdown point, the slightly excess speed, and the subsequent failure of three of the tires resulted in there being insufficient runway remaining to avoid a runway overrun. Although the BCV manufacturer reported that there was 1 previous case involving a failed BCV spring and 43 instances of units with relaxed springs within the BCVs, none of these failed or relaxed springs would have been detected by maintenance personnel because a focused inspection of the BCV was not required.
Probable cause:
The failure of a spring inside the No. 2 brake's upper brake control valve and the fracture of the coupling subassembly of the No. 1 wheel speed sensor during landing, which resulted in the loss of braking action, and the pilot-in-command's (PIC) deactivation of the antiskid system even though there were no antiskid failure annunciations, which resulted in the rupture of the Nos. 1, 3, and 4 tires, further loss of braking action, and subsequent landing overrun. Contributing to accident were the PIC's improper landing flare, which resulted in landing several hundred feet beyond the aiming point marking, and his unsuccessful attempts to deploy the thrust reversers for reasons that could not be determined because postaccident operational testing did not reveal any anomalies that would have precluded normal operation. Contributing to the passenger's injury was his leaving his seat intentionally while the airplane was in motion.
Final Report:

Crash of a Cessna 401A in Fulton

Date & Time: Nov 17, 2014 at 1720 LT
Type of aircraft:
Operator:
Registration:
N401ME
Flight Phase:
Survivors:
Yes
Schedule:
Fulton – Little Rock
MSN:
401A-0085
YOM:
1969
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2949
Captain / Total hours on type:
304.00
Copilot / Total flying hours:
8675
Copilot / Total hours on type:
1850
Aircraft flight hours:
6434
Circumstances:
The private pilot reported that, immediately after takeoff in the multi-engine airplane, the right engine experienced a total loss of power. The pilot aborted the takeoff; the airplane exited the end of the runway surface, impacted rough terrain, and came to rest upright. Examination of the right engine showed that the magneto distributor drive gears were not turning. Both damaged magnetos were removed and replaced with a slave set of magnetos. The right engine was installed in an engine test cell, and subsequently started and performed normally throughout the test cell procedure. The damaged magnetos from the right engine were disassembled. Both nylon magneto distributor gears exhibited missing gear teeth and brown discoloration. A review of maintenance records showed that the right engine had been operated for about 8 years and an estimated 697 hours since the most recent magneto overhauls had been completed. According to maintenance instructions from the engine manufacturer, the magnetos should be inspected every 500 hours and should be overhauled or replaced at the expiration of five years since the last overhaul. Guidance also indicated that discoloration of the drive gear is an indication that the gear had been exposed to extreme heat and should be replaced.
Probable cause:
A failure of the right engine magneto distributor drive gears, which resulted in a total loss of engine power during takeoff. Contributing to the accident was the operator's failure to inspect and maintain the magnetos in accordance with the engine manufacturer's specifications.
Final Report:

Crash of a Cessna 560XLS Citation Excel in Santos: 7 killed

Date & Time: Aug 13, 2014 at 1003 LT
Operator:
Registration:
PR-AFA
Survivors:
No
Site:
Schedule:
Rio de Janeiro – Santos
MSN:
560-6066
YOM:
2011
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
6235
Captain / Total hours on type:
130.00
Copilot / Total flying hours:
5279
Copilot / Total hours on type:
95
Aircraft flight hours:
434
Aircraft flight cycles:
392
Circumstances:
The aircraft took off from Santos Dumont Airport (SBRJ) at 12:21 UTC, on a transport flight bound for Santos Aerodrome (SBST), with two pilots and five passengers on board. During the enroute phase of the flight, the aircraft was under radar coverage of the approach control units of Rio de Janeiro and São Paulo (APP-RJ and APP-SP, respectively), and no abnormalities were observed. Upon being released by APP-SP for descent and approach toward SBST, the aircraft crew, already in radio contact with Santos Aerodrome Flight Information Service (Santos Radio), reported their intention to perform the IFR ECHO 1 RWY 35 NDB approach chart profile. After reporting final approach, the crew informed that they would make a go-around followed by a holding procedure, and call Santos Radio again. According to an observer that was on the ground awaiting the arrival of the aircraft at Santos Air Base (BAST) and to another observer at the Port of Santos, the aircraft was sighted flying over the aerodrome runway at low height, and then making a turn to the left after passing over the departure end of the runway, at which point the observers lost visual contact with the aircraft on account of the weather conditions. Moments later, the aircraft crashed into the ground. All seven occupants were killed.
Probable cause:
The following factors were identified:
- Considering the pronounced angle formed between the trajectory of the aircraft and the terrain, as well as the calculated speed (which by far exceeded the aircraft operating limit) moments before the impact, it is possible to infer that, from the moment the aircraft disappeared in the clouds, it could only have reached such speed and flown that trajectory if it had climbed considerably, to the point of being detected by the radar. Such condition presented by the aircraft may have been the result of an exaggerated application of controls.
- The making of an approach with a profile different from the one prescribed shows lack of adherence to procedures, which, in this case, may have been influenced by the self-confidence of the pilot on his piloting ability, given his prior experiences.
- Despite the lack of pressure on the part of the passengers to force compliance with the agenda, it is a known fact that this type of routine creates in the crew a self-pressure, most of the time unconscious, for accomplishing the flight schedule on account of the commitments undertaken by the candidate in campaign, and, therefore, the specific characteristics of this type of flight pose demands in terms of performance that may have influenced the pilots to operate with reduced safety margins.
- The meteorological conditions were close to the safety minimums for the approach and below the minimums for the circle-to-land procedure prescribed in the ECHO 1 approach. However, such conditions, by themselves, would not represent risk for the operation, if the profile of the ECHO 1 procedure was performed in accordance with the parameters established in the aeronautical publications and the flight parameters defined by the aircraft manufacturer. Upon verifying that the above mentioned parameters were not complied with, one observes that the meteorological conditions became a complicating factor for flying the aircraft, rendering it difficult to be stabilized on the final approach, and a go-around became necessary, as a result.
- In the scenario of the aircraft collision with the ground, there were aspects favorable to the occurrence of spatial disorientation, such as: reduction of the visibility on account of meteorological conditions, stress and workload increase due to the missed approach procedure, maneuvers with a G-load above 1.15G, and a possible loss of situational awareness. The large pitch-down angle, the high speed, and the power developed by the engines at the moment of impact are also evidence compatible with incapacitating disorientation, and point towards a contribution of this factor.
- The integration between the pilots may have been hindered by their little experience working together as one crew, and also by their different training background. In addition, the personal characteristics of the captain, as a more impositive and confident person, in contrast with the more passive posture of the copilot, may also have hampered the crew dynamics in the management of the flight.
- In the seven days preceding the day of the accident, the crew was in conformity with the Law 7183 of 5 April 1984 in relation to both duty time and rest periods. However, the analysis of copilot’s voice, speech, and language indicated compatibility with fatigue and somnolence, something that may have contributed to the degradation of the crew’s performance.
- Their lack of training of missed approach procedures in CE 560XLS+ aircraft may have demanded from the crew a higher cognitive effort in relation to the conditions required for the aircraft model, since they possibly did not have conditioned behaviors for controlling the flight and that could otherwise provide them with more agility with regard to the cockpit actions. Thus, they probably missed the skills, knowledge, and attitudes that would allow them to more adequately perform their activities in that operational context.
- Even though Santos Radio reported, in the first contact with the aircraft, that the aerodrome was operating IFR, the messages transmitted to the aircraft did not include the conditions of ceiling, visibility, and SIGMET information (ICA 100-37). This may have contributed to reducing the crew’s situational awareness, since the last information accessed by them was probably the 11:00 UTC SBST METAR, which reported VMC conditions for operation in the aerodrome. Thus, the pilots may have built a mental model of unreal SBST meteorological conditions more favorable to the operation.
- After coordination of the descent, the PR-AFA aircraft made a left turn and, for an unknown reason, deviated from the W6-airway profile, reporting six positions that were not compatible with the real flight path until the moment it started a final approach. This approach was different from the trajectory of the final approach defined for the ECHO 1 procedure, and was flown with speed parameters different from those recommended by the aircraft manufacturer. These aspects reduced the chances of the aircraft to align with the final approach in a stabilized manner. The fact that the aircraft made a low pass over the runway and then a left turn at low altitude in weather conditions below the minimum established in the circle-to-land procedure instead of performing the profile prescribed in the ECHO 1 approach chart also resulted in risks to the operation, and created conditions which were conducive to spatial disorientation.
- Since the captain had already conducted FMS visual approaches on other occasions, his acquired work-memory may have strengthened his confidence in performing the procedure again, even though in another scenario, on account of the human being tendency to rely on previous successful experiences.
- A poor perception on the part of the pilots relative to the real meteorological conditions on the approach may have compromised their level of situational awareness, thus leading the aircraft to a condition of operation below the safe minimums.
- The TAF/GAMET weather prognostics with validity up to 12:00 UTC, and available to the crew at the time the flight plan was filed at the AIS-RJ, indicated a possibility of degradation of the ceiling and visibility parameters on account of rain associated with mist, encompassing the duration of the aforementioned flight, especially in the area of SBST. The 11:00 UTC satellite image and the SIGMET valid from 10:30 UTC to 13:30 UTC, also showed an active cold front in the Southeast with stratiform cloud layers over SBST and a forecast of convective cells with northeasterly movement at an average speed of 12kt. Despite the availability of such information, the crew may not have made a more accurate analysis showing the swift deterioration of the weather conditions in the period between their takeoff from SBRJ and the approach to SBST, and thus may have failed to plan their conduct of the flight in accordance with the weather conditions forecast by the meteorological services.
- Despite having the C560 qualification required to operate the CE 560XLS+aircraft, the pilots were not checked by the employers as to their previous experience on this kind of equipment, or as to the need of transition training and/or specific formation to fly the PRAFA aircraft. The adoption of a formal process for the recruitment, selection, monitoring and evaluation of the performance of the professionals could have identified their training needs for that type of aircraft.
- Although the RBAC 61 requires pilots to undergo flight instruction and proficiency checks to switch between models of the CE 560XL family, the need of specific training was only clarified on 4 July 2014, with the publication of the ANAC Supplementary Instruction (IS 61-004, Revision A). Until that date, this need could only be determined by means of consultation of the FSB Report, made available only on the FAA website. In this context, the PR-AFA pilots would only be evaluated on the CE 560XLS+ aircraft on the occasion of their type revalidation, which would take place shortly before the expiration date of their C560 qualifications, which were valid until October 2014 (captain), and May 2015 (copilot). The fact that there was a qualification (C560) that was shared for the operation of C560 Citation V, C560 Encore, C560 Encore+, CE 560XL, CE 560XLS, or CE 560XLS + aircraft was not enough to make the DCERTA system refuse flight plans filed by pilots who lacked proper training to operate one of the aforementioned aircraft models. The RBAC 67 contained physical and mental health requirements which were not clear, inducing physicians to resort to other publications for guidance and support of their decisions and judgments relative to the civil aviation personnel. The absence of clear requirements to be adopted as the acceptable minimum for the exercise of the air activity, led the physicians responsible for judging the pilots’ health inspections’ to use their own discretion on the subject, opening gaps that could allow professionals not fully qualified to perform functions in flight below the minimum acceptable safety levels.
- Considering the possibility that the captain accumulated tasks as a result of a possible difficulty of the copilot in assisting him at the beginning of the missed approach procedure, such accumulation may have exceeded his ability to deal with the tasks, leading him to committing piloting errors and/or experiencing spatial disorientation.
Final Report: