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Crash of a Lockheed WC-130H Hercules in Savannah: 9 killed

Date & Time: May 2, 2018 at 1127 LT
Type of aircraft:
Operator:
Registration:
65-0968
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Savannah – Davis-Monthan
MSN:
4110
YOM:
1965
Crew on board:
5
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total hours on type:
2070.00
Copilot / Total hours on type:
9
Circumstances:
On 2 May 2018, at approximately 1127 hours local time (L), the Mishap Aircraft (MA), a WC-130H, tail number 65-0968, assigned to the Puerto Rico Air National Guard, 156th Airlift Wing (156 AW), located at Muñiz Air National Guard Base, Puerto Rico, crashed approximately 1.5 miles northeast of Savannah/Hilton Head International Airport (KSAV), Georgia. All nine members aboard the MA—Mishap Pilot 1 (MP1), Mishap Pilot 2, Mishap Navigator, Mishap Flight Engineer, and Mishap Loadmaster (collectively the “Mishap Crew (MC)”), and four mission essential personnel, Mishap Airman 1, 2, 3, and 4—perished during the accident. The MC’s mission was to fly the MA to the 309th Aerospace Maintenance and Regeneration Group at Davis-Monthan Air Force Base, Arizona (commonly referred to as the “Boneyard”), for removal from service. The MA had been at KSAV for almost a month, since 9 April 2018, to undergo prescheduled fuel cell maintenance and unscheduled work on engine number one by 156 AW maintenance personnel using the facilities of the 165th Airlift Wing. During takeoff roll, engine one revolutions per minute (RPM) fluctuated and did not provide normal RPM when MP1 advanced the throttle lever into the flight range for takeoff. Approximately eight seconds prior to aircraft rotation, engine one RPM and torque significantly decayed, which substantially lowered thrust. The fluctuation on roll and significant performance decay went unrecognized by the MC until rotation, when MP1 commented on aircraft control challenges and the MA veered left and nearly departed the runway into the grass before it achieved flight. The MA departed KSAV at approximately 1125L. As the MC retracted the landing gear, they identified the engine one RPM and torque malfunction and MP1 called for engine shutdown. However, the MC failed to complete the Takeoff Continued After Engine Failure procedure, the Engine Shutdown procedure, and the After Takeoff checklist as directed by the Flight Manual, and the MA’s flaps remained at 50 percent. Additionally, MP1 banked left into the inoperative engine, continued to climb, and varied left and right rudder inputs. At an altitude of approximately 900 feet mean sea level and 131 knots indicated air speed, MP1 input over nine degrees of left rudder, the MA skidded left, the left wing stalled, and the MA departed controlled flight and impacted the terrain on Georgia State Highway 21.
Probable cause:
The board president found, by a preponderance of the evidence, the cause of the mishap was MP1’s improper application of left rudder, which resulted in a subsequent skid below three-engine minimum controllable airspeed, a left-wing stall, and the MA’s departure from controlled flight. Additionally, the board president found, by a preponderance of the evidence, the MC’s failure to adequately prepare for emergency actions, the MC’s failure to reject the takeoff, the MC’s failure to properly execute appropriate after takeoff and engine shutdown checklists and procedures, and the Mishap Maintainers’ failure to properly diagnose and repair engine number one substantially contributed to the mishap.
Final Report:

Crash of a Cessna 404 Titan at Davis Monthan AFB

Date & Time: Nov 26, 1992 at 1915 LT
Type of aircraft:
Operator:
Registration:
N5429J
Flight Type:
Survivors:
Yes
Schedule:
Davis Monthan - Davis Monthan
MSN:
404-0107
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4981
Captain / Total hours on type:
685.00
Aircraft flight hours:
4011
Circumstances:
During a 2 hour and 40 minute training mission, the pilot maintained a low power setting with the fuel mix at full rich. After the mission, the pilot climbed the airplane to 9,000 feet agl to clear obstacles between his location and his destination. During the descent, the pilot said he reduced power more rapidly than usual and descended faster than normal at about 180 kias. About 800 to 1,000 feet agl, in the traffic pattern, the pilot applied power. Both engines lost total power. He set up an 85 kias glide; competed emergency procedures; and retracted the landing gear. The engines did not restart. He did not feather the propellers. He extended the landing gear prior to touchdown. The pilot said he did not flare the airplane during landing which resulted in the airplane colliding with the ground. The engine manual and the poh recommend adjusting the fuel mixture for cruise. An engine manual note states long descents at low power should be avoided because the engines may cool excessively and may not accelerate satisfactorily when power is reapplied. The poh recommends feathering propellers and gliding at 120 kias for dual engine failure. Soot was noted on all spark plugs during engine exam. Both engines started and ran normally from idle to full acceleration during the exam.
Probable cause:
The pilot's inflight decision to deviate from the airplane's engine manual and the pilot's operating handbook by maintaining the fuel mixture at full rich throughout the mission and rapidly descending the airplane which resulted in both engine's losing total power. Factors in this accident were:
1) the pilot not following the emergency procedure for both engines failing as outlined in the pilot's operating handbook, and
2) the pilot not performing a flare during the landing sequence which resulted in the airplane colliding with the terrain.
Final Report:

Crash of a Boeing 707-321B in Marana: 1 killed

Date & Time: Sep 20, 1990 at 0707 LT
Type of aircraft:
Operator:
Registration:
N320MJ
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Marana - Davis Monthan
MSN:
20028
YOM:
1968
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
13192
Captain / Total hours on type:
4000.00
Aircraft flight hours:
34965
Circumstances:
Witnesses reported 1st attempt to takeoff was aborted after aircraft swerved left and right. On 2nd try, aircraft lifted off about halfway down runway. After lift-off, it rolled right, right wing hit ground and aircraft crashed. Investigations revealed rudder trim was 7.9 to 8.3 units (79% to 83%) nose right. Simulator tests with that setting resulted in consistent right wing collisions with ground after liftoff. Crew's checklist referred to mech checklist for critical items to check before takeoff. Mech checklist and 50 of 54 flight instruments had been removed from aircraft, leaving 2 airspeed indicators, altimeter and standby gyro horizon. In 60 simulated takeoffs in this configuration, there was evidence of insufficient attitudinal ref to recognize rolling of aircraft before sufficient altitude was attained. FAA's designated airworthiness rep (dar) had inspected aircraft three days before and issued ferry permit. He lacked FAA mechanical certification and experience with large aircraft. FAA order 8000.62 and ac 183.33 lacked specific guidance for selection, training and oversight of dar activity. Also, lack of guidance concerning minimum equipment list. Pilot not current or medical qualified to fly aircraft.
Probable cause:
Improper preflight planning/preparation by the pilot, and his failure to use a checklist. Factors related to the accident were: the faa's inadequate surveillance of the operation, the FAA's insufficient standards/requirements, the pilot's operation of the aircraft with known deficiencies, and his lack of recent experience in the type of aircraft.
Final Report:

Crash of a Douglas C-54P Skymaster at Davis Monthan AFB

Date & Time: Jan 2, 1975 at 1358 LT
Type of aircraft:
Registration:
N39AP
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Davis-Monthan - Barstow-Daggett
MSN:
10430
YOM:
1944
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6409
Captain / Total hours on type:
20.00
Circumstances:
After takeoff from Davis Monthan AFB, the four engine airplane encountered difficulties to gain height. It struck power cables, stalled and crashed in flames. All three occupants were injured while the aircraft was destroyed.
Probable cause:
Inadequate preflight preparation on part of the crew. The following contributing factors were reported:
- Collision with wires,
- Lack of familiarity with aircraft,
- Failed to abort takeoff,
- Gust locks engaged,
- Operational supervisory personnel: inadequate supervision of flight crew,
- Unqualified person operated aircraft,
- Airport conditions,
- Checklist: failed to use,
- Downwind,
- Mechanic acting as copilot,
- 3,060 feet soft dirt strip.
Final Report:

Crash of a Boeing B-50A-35-BO Superfortress on Picacho Peak: 2 killed

Date & Time: Aug 20, 1953 at 0205 LT
Type of aircraft:
Operator:
Registration:
47-116
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Davis-Monthan - Davis-Monthan
MSN:
15800
YOM:
1947
Location:
Crew on board:
12
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
Few minutes after takeoff from Davis-Monthan AFB, while cruising at an altitude of 15,000 feet, the crew encountered an unexpected situation. Immediately, the captain ordered his crew to bail out and all 12 occupants abandoned the aircraft that dove into the ground and crashed in a huge explosion on the slope of the Picacho Peak, southeast of Picacho. The airplane disintegrated on impact and debris were found on a wide area. Ten crew members were injured while two others were killed.
Crew:
Cpt John D. Winters, pilot,
1st Lt William H. Montgomery, copilot,
William Reale, flight engineer,
Cpt John A. Barnes, navigator,
S/Sgt David Fry, radio operator,
William P. Cooke, gunner,
A1c Richard W. Dickey, gunner
A3c Charles R. Stewart, gunner,
Cpt Charles D. Bostick, †
S/Sgt Herbert G. Emberton, †
Cpt Lee F. Aubechon 1.
Probable cause:
It was reported that a sudden and heavy fire erupted on the right wing, maybe from an engine.

Crash of a Boeing B-50A-25-BO Superfortress near Comobabi: 7 killed

Date & Time: Nov 16, 1950
Type of aircraft:
Operator:
Registration:
46-047
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Davis-Monthan - Davis-Monthan
MSN:
15767
YOM:
1947
Crew on board:
13
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
The Boeing B-50 was completing a training mission out of Davis-Monthan AFB and was carrying a crew of 13. While cruising at an assigned altitude of 9,000 feet, the aircraft collided with a USAF Boeing B-50 that was engaged in a refueling mission out of Davis-Monthan with 10 crew members on board. Both aircraft went into a dive and crashed in a desert area located in the region of Comobabi, about 50 miles west of Tucson. On board the B-29, six crew members were killed while four others were injured. On board the B-50, seven crew members were killed while six others were injured. The exact circumstances of the collision remains unclear.

Crash of a Boeing KB-29M Superfortress near Comobabi: 6 killed

Date & Time: Nov 16, 1950
Type of aircraft:
Operator:
Registration:
44-70024
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Davis-Monthan - Davis-Monthan
MSN:
10856
YOM:
1944
Crew on board:
10
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The KB-29M aircraft was engaged in a refueling mission out of Davis-Monthan and was carrying a crew of 10. While cruising at an assigned altitude of 9,000 feet, the aircraft collided with a USAF Boeing B-50 that was completing a training sortie from Davis-Monthan with a crew of 13 on board. Both aircraft went into a dive and crashed in a desert area located in the region of Comobabi, about 50 miles west of Tucson. On board the B-29, six crew members were killed while four others were injured. On board the B-50, seven crew members were killed while six others were injured. The exact circumstances of the collision remains unclear.

Crash of a Boeing B-50A-30-BO Superfortress near Goose Bay

Date & Time: Sep 22, 1950
Type of aircraft:
Operator:
Registration:
47-105
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Goose Bay – Davis-Monthan
MSN:
15789
YOM:
1947
Country:
Crew on board:
16
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
One hour after departure from Goose Bay bound for Davis-Monthan AFB, the carburetor of the engine number 2 suffered icing and the engine failed. The captain decided to return to Goose Bay for a safe landing when the same engine caught fire shortly later. As the crew was trying to extinguish the fire, the engine number four caught fire as well. In such conditions, the captain ordered his crew to abandon the aircraft. After all 16 crew members bailed out, the aircraft continued a while to the east and eventually crashed in a wooded area located about 94 miles east of Goose Bay. The aircraft disintegrated on impact and all 16 occupants were later rescued and evacuated.
Probable cause:
Carburetor icing, engine failure and engine fire.

Crash of a Boeing B-50A-5-BO Superfortress in Davis-Monthan AFB

Date & Time: Aug 13, 1950
Type of aircraft:
Operator:
Registration:
46-010
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Davis-Monthan - Davis-Monthan
MSN:
15730
YOM:
1947
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was performing a local training flight in the vicinity of the Davis-Monthan AFB when one (or more?) engine failed. The crew decided to make an emergency landing in a desert area located two miles southeast of the airbase. The aircraft belly landed and slid for several yards before coming to rest. There were no injuries but the aircraft christened 'Lucky Lady II' was damaged beyond repair. It completed the first nonstop world tour from February 26 till March 6, 1949.
Probable cause:
Engine failure.

Crash of a Boeing B-50A-20-BO Superfortress near Davis Monthan AFB: 4 killed

Date & Time: Jul 13, 1950
Type of aircraft:
Operator:
Registration:
46-040
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Davis-Monthan - Davis-Monthan
MSN:
15760
YOM:
1947
Crew on board:
10
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew was engaged in a navigational exercice from Davis-Monthan AFB. About 19 minutes after takeoff, while cruising at the assigned altitude of 12,700 feet, a propeller blade failed on the engine number three. The engine vibrated and detached from its mount. It then struck the right wing and the fuselage, causing a fire. Out of control, the aircraft dove into the ground and six of the ten crew members were able to bail out before the aircraft crashed in a desert area located about 44 miles northeast of Davis-Monthan AFB.
Crew (43rd BW):
Cpt Vaughn S. Lautenschlager, pilot,
Lt Jerome McCarville, copilot,
Cpt Patrick Montoya, navigator,
Cpt Alvin Tonne, bombardier,
Sgt Earl Hornbuckle, flight engineer,
Lt Arthur Weisberg, observer,
Sgt Robert Jones, radio operator, †
Sgt Harold Martin, gunner, †
Sgt Robert O'Daniel, gunner, †
Cpl James Adcock, gunner. †
Probable cause:
Loss of a propeller blade on the engine number three.