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Crash of a Piper PA-46-500TP Malibu Meridian in Mendoza: 2 killed

Date & Time: Dec 7, 2009 at 1134 LT
Operator:
Registration:
N600YE
Flight Type:
Survivors:
No
Schedule:
Rockport – Austin
MSN:
46-97250
YOM:
2006
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3513
Circumstances:
The pilot was established on the localizer portion of the instrument landing system approach outside the final approach fix in visual meteorological conditions above clouds. He was then given vectors away from the localizer course by an air traffic controller. The vectors were close together and included a left 90-degree turn, a descent, and a 180-degree right turn back toward the localizer course. During the right turn and descent, the airplane continued turning with increasing bank and subsequently impacted the ground. According to a pilot weather report and flight path data the pilot entered clouds as he was starting the right turn toward the localizer. The combination of descending turns while entering instrument conditions were conducive to spatial disorientation. Further, the heading changes issued by the air traffic controller were rapid, of large magnitude, and, in combination with a descent clearance, likely contributed to the pilot’s disorientation. Diphenhydramine, a drug that may impair mental and/or physical abilities, was found in the pilot’s toxicological test results. While the exact effect of the drug at the time of the accident could not be determined, it may have contributed to the development of spatial disorientation.
Probable cause:
The pilot’s spatial disorientation, which resulted in his loss of airplane control. Contributing to the pilot's spatial disorientation was the sequence and timing of the instructions issued by the air traffic controller. The pilot’s operation of the airplane after using impairing medication may also have contributed.
Final Report:

Crash of a Lockheed L-1329-25 JetStar II in Austin

Date & Time: Nov 27, 1998 at 1405 LT
Type of aircraft:
Operator:
Registration:
N787WB
Survivors:
Yes
Schedule:
Houston - Austin
MSN:
5210
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8350
Captain / Total hours on type:
750.00
Aircraft flight hours:
5938
Circumstances:
During the landing roll, the nose gear settled onto the runway, and the aircraft veered hard to the right. Application of the left brake had no effect. The airplane skidded, exited the runway, struck a runway marker, and collapsed the nose landing gear. The steering actuator had failed, the hydraulic fluid was lost from the steering actuator, and the fuselage received structural damage. The steering actuator assembly, p/n 1501-4, had accumulated 5,938.0 hours since new and had not been repaired or overhauled. Examination of the nose gear steering actuator cylinder by the metallurgist revealed that the cylinder fracture was the result of fatigue cracking initiated by an abrupt machining transition from the 45 degree thread ring chamfer to the straight wall of the cylinder. The engineering drawings appear to depict the radius at the fatigue origin as a continuation of the 0.03 inch to 0.06 inch radius adjacent to the fracture. However, the drawing is not clear on the specific intent of the transition between the nearby radius and the internal threads for the nut.
Probable cause:
The steering actuator fatigue failure resulting from inadequate procedure documentation for the manufacturing process.
Final Report:

Crash of a Piper PA-42-720 Cheyenne III in Horseshoe Bay

Date & Time: Feb 7, 1987 at 0840 LT
Type of aircraft:
Registration:
N81SM
Flight Phase:
Survivors:
Yes
Schedule:
Horseshoe Bay – Austin
MSN:
42-8001007
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3670
Captain / Total hours on type:
12.00
Aircraft flight hours:
2002
Circumstances:
The pilot made a fairly long taxi from the ramp to the end of the runway and then started his takeoff roll with the parking brake still partially set. The brakes became very hot and the component parts expanded. After rolling almost 3,000 feet the brakes tightened up to the extent that both main gear tires started leaving black skid marks which continued until the aircraft ran off the end of the runway without obtaining flying speed, a distance of 3,168 feet. It was noted, through a design feature of the aircraft, that the parking brake handle could be placed in the released position without the brake being released. However, this would give the appearance that it had been released. The main gear tires were worn almost slick during this attempted takeoff. Both main gear brakes had been overheated during this time to the extent that they were destroyed. The aircraft was destroyed by collision with trees, rocks and a fire hydrant at the bottom of a hill off the end of the runway. The pilot escaped with serious injuries.
Probable cause:
Occurrence #1: loss of control - on ground/water
Phase of operation: takeoff - roll/run
Findings
1. (c) airspeed (vlof) - not obtained - pilot in command
2. (c) aircraft preflight - inadequate - pilot in command
3. (f) procedures/directives - not followed - pilot in command
4. (c) emergency procedure - inadequate - pilot in command
----------
Occurrence #2: overrun
Phase of operation: takeoff
Findings
5. (c) aborted takeoff - delayed - pilot in command
6. (c) powerplant controls - improper use of - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: takeoff
Findings
7. (f) terrain condition - downhill
8. (f) object - tree(s)
9. (f) terrain condition - rough/uneven
Final Report:

Crash of a Swearingen SA226TC Metro II in Austin

Date & Time: Aug 13, 1978 at 1643 LT
Type of aircraft:
Operator:
Registration:
N300TL
Survivors:
Yes
Schedule:
San Antonio - Austin
MSN:
TC-238E
YOM:
1977
Crew on board:
2
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4985
Captain / Total hours on type:
815.00
Circumstances:
On final approach to Austin-Robert Mueller Airport, the left engine failed. The crew continued the approach but forgot to lower the landing gear. The airplane belly landed and slid for dozen yards before coming to rest. Two occupants, among them the copilot, were seriously injured while 16 other people escaped with minor injuries. The aircraft was written off.
Probable cause:
Failure of the left engine on final approach due to inadequate preflight preparation on part of the flying crew. The following contributing factors were reported:
- Mismanagement of fuel,
- Fuel starvation,
- Failed to assure the gear was down and locked,
- Improper emergency procedures,
- Failed to follow approved procedures,
- Aircraft refueled in right wing with 125 gallons before 18 minutes flight,
- Crossflow valve found off.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Austin

Date & Time: Aug 15, 1977 at 1521 LT
Operator:
Registration:
N74906
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Austin - Galveston
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
996
Captain / Total hours on type:
280.00
Circumstances:
At liftoff, the twin engine rolled to the right and crashed in flames. The aircraft was destroyed by a post crash fire and the pilot, sole on board, was slightly injured.
Probable cause:
Stall during takeoff run after the pilot attempted operation with known deficiencies in equipment. The following contributing factors were reported:
- Improper maintenance,
- Exhaust system: external supercharger,
- Failed to obtain flying speed,
- Premature liftoff,
- Misused or failed to used flaps,
- Weste gate pivot pin p/n 400460-817 missing on right supercharger,
- Past history of power problems.
Final Report:

Crash of a Cessna 401 in Austin: 3 killed

Date & Time: Aug 19, 1975 at 0801 LT
Type of aircraft:
Operator:
Registration:
N4004Q
Survivors:
No
Schedule:
Dallas - Austin
MSN:
401-0104
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
705
Captain / Total hours on type:
65.00
Circumstances:
While approaching Austin-Robert Mueller Airport runway 12R in a cloud base at 500 feet, the twin engine airplane stalled and crashed in flames onto a house located few miles from the airfield. The aircraft was destroyed and all three occupants were killed. There were no casualties on the ground.
Probable cause:
Stall on final approach because the pilot failed to maintain flying speed. The following contributing factors were reported:
- Attempted operation beyond experience/ability level,
- Improper IFR operation,
- Low ceiling,
- Unqualified person operated aircraft,
- Pilot had no solo time in type of aircraft,
- Two previous approaches completed.

Crash of a Howard Super Ventura in Austin

Date & Time: Aug 3, 1972 at 0923 LT
Operator:
Registration:
N446DD
Survivors:
Yes
Schedule:
Laredo - Dallas
MSN:
5696
YOM:
1943
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
20470
Captain / Total hours on type:
308.00
Circumstances:
En route from Laredo to Dallas, one of the engine lost power due to oil exhaustion. The pilot was cleared to divert to Austin-Robert Mueller Airport but following a wrong approach configuration, the aircraft was not properly aligned. After touchdown on a wet runway, the airplane suffered hydroplaning then veered off runway and came to rest. All three occupants were uninjured while the aircraft was damaged beyond repair.
Probable cause:
In-flight engine failure or malfunction. The following factors were reported:
- Inadequate maintenance and inspection,
- Oil exhaustion, engine lubrication system,
- Improper IFR operation,
- Failed to initiate a go-around,
- Lack of familiarity with aircraft,
- Wet runway,
- Rain,
- Poorly planned approach,
- Not aligned with runway,
- Hydroplaning on wet runway,
- Partial loss of power on one engine,
- Cause of oil exhaustion not determined,
- Annual maintenance check performed the day before the accident,
- Other runway available,
- Wrong switch used for wipers.
Final Report: