Crash of a Lockheed 18-56-24 LodeStar in Lake Milton: 13 killed

Date & Time: Sep 4, 1962 at 2100 LT
Type of aircraft:
Operator:
Registration:
N1000F
Flight Phase:
Survivors:
No
Schedule:
Buffalo – Ashland
MSN:
2463
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
11
Pax fatalities:
Other fatalities:
Total fatalities:
13
Captain / Total flying hours:
13250
Copilot / Total flying hours:
1000
Aircraft flight hours:
6557
Circumstances:
After takeoff from Buffalo Airport, the crew was cleared to climb to 8,000 feet. About an hour into the flight, the airplane went out of control, entered a dive and crashed near Lake Milton, Ohio. The crew was unable to send any distress call. The aircraft disintegrated on impact and all 13 occupants were killed.
Probable cause:
The Board determines that the probable cause of this accident was a malfunction of the electric elevator trim tab unit which resulted in aircraft uncontrollability and subsequent structural failure of the wing.
Final Report:

Crash of a Lockheed C-121G Super Constellation in Oakland

Date & Time: Aug 31, 1962
Operator:
Registration:
54-4057
Flight Type:
Survivors:
Yes
MSN:
4138
YOM:
1953
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Suffered a ground accident at Oakland Airport. There were no casualties but the aircraft was written off.

Crash of a Martin 404 in Wilmington

Date & Time: Aug 22, 1962 at 0748 LT
Type of aircraft:
Operator:
Registration:
N40401
Flight Type:
Survivors:
Yes
Schedule:
Wilmington - Wilmington
MSN:
14101
YOM:
1952
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4492
Captain / Total hours on type:
125.00
Aircraft flight hours:
20260
Circumstances:
The crew was completing a local training flight at Wilmington-New Hanover County Airport. After touchdown, the airplane went out of control, veered off runway and came to rest. While all three crew members were uninjured, the aircraft was damaged beyond repair.
Probable cause:
The accident was the consequence of an unwanted propeller reversal during a critical phase of landing caused by malfunction of the propeller low pitch stop lever assembly, resulting from foreign matter in the servo valve control.

Crash of a Howard Super Ventura off Chicago: 2 killed

Date & Time: Aug 17, 1962 at 1654 LT
Operator:
Registration:
N18A
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Chicago - Chicago
MSN:
5271
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
Shortly after takeoff from Chicago-Merrill C. Meigs Airport, while in initial climb, the airplane stalled and crashed into Michigan Lake. The aircraft was lost and both crew members were killed. They were performing a positioning flight to Chicago-Palwaukee Airport when the accident occurred.
Probable cause:
Loss of control during initial climb caused by an engine failure.

Crash of a Lockheed WV-2 Super Constellation at Patuxent River NAS: 5 killed

Date & Time: Aug 9, 1962
Operator:
Registration:
141324
Flight Type:
Survivors:
Yes
Schedule:
Corpus Christi - Patuxent
MSN:
4448
YOM:
1956
Crew on board:
4
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
On approach to Patuxent River NAS, the crew encountered poor weather conditions with heavy rain falls. In low visibility, the aircraft was too low and struck the ground before coming to rest in flames few hundred yards short of runway threshold. Five occupants were killed while 14 others were injured. The aircraft was destroyed.

Crash of a Boeing KC-135A-BN Stratotanker in Hanscom Field: 3 killed

Date & Time: Aug 8, 1962
Type of aircraft:
Operator:
Registration:
55-3144
Flight Type:
Survivors:
No
Schedule:
Wright-Patterson - Hanscom Field
MSN:
17260
YOM:
1957
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
On final approach to Bedford-Hanscom Field Airport, the pilot-in-command did not realize his altitude was insufficient. The four engine aircraft struck telephone poles, stalled and crashed in a boulder located 2,657 feet short of runway threshold. The aircraft was destroyed and all three crew members were killed.

Crash of a Lockheed L-188A Electra in Knoxville

Date & Time: Aug 6, 1962 at 1731 LT
Type of aircraft:
Operator:
Registration:
N6102A
Survivors:
Yes
Schedule:
Dallas – Little Rock – Memphis – Knoxville – Washington DC – New York
MSN:
1019
YOM:
1958
Flight number:
AA414
Crew on board:
5
Crew fatalities:
Pax on board:
67
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
20634
Captain / Total hours on type:
878.00
Copilot / Total flying hours:
11000
Copilot / Total hours on type:
423
Aircraft flight hours:
6947
Circumstances:
On August 6, 1962, at 1731 e.s.t., Flight 414, an American Airlines, Inc., Lockhead Electra, N 6102A, crashed during a landing on runway 4L at McGhee-Tyson Airport, Knoxville, Tennessee. Sixty-seven passengers and five crew members were on board the aircraft. All escaped injury except one passenger who suffered a minor injury. The aircraft was substantially damaged. During the landing made by the captain in an area of thunderstorm activity and heavy rain showers, the aircraft skidded to the right off the runway. It struck a newly constructed taxiway the surface of which was approximately 17 inches above ground level, causing failure of the right main landing gear. The right wing became separated front the aircraft. The remainder of the aircraft continued to deviate to the right off the side of the runway for a short distance and came to rest 3,010 feet from the approach end of the runway on a heading of 200 degrees magnetic.
Probable cause:
The Board determines that the probable cause of this accident was the loss of directional control as a result of the improper technique employed in a crosswind landing in adverse weather conditions.
Final Report:

Crash of a Rockwell T-39A-1-NA Sabreliner in Everett: 2 killed

Date & Time: Jul 29, 1962
Type of aircraft:
Operator:
Registration:
61-0661
Flight Type:
Survivors:
No
Schedule:
Everett - Everett
MSN:
265-64
YOM:
1962
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
While completing a training mission over the Washington State, the crew informed ATC about hydraulic problems and was cleared to land at Everett-Paine Field. After touchdown, the aircraft was unable to stop within the remaining distance, overran, went through a fence and came to rest on an embankment. Both pilots were killed.
Probable cause:
Failure of the hydraulic system.

Crash of a Lockheed P2V-5 Neptune at Glynco NAS: 6 killed

Date & Time: Jul 23, 1962
Type of aircraft:
Operator:
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Jacksonville - Glynco
Crew on board:
10
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The crew was completing a training mission from Jacksonville, Florida. While flying in the vicinity of the Glynco NAS (now Brunswick), the airplane crashed in unknown circumstances in a field. Six crew members were killed while four others were injured.

Crash of a Bristol 175 Britannia 314 in Honolulu: 27 killed

Date & Time: Jul 22, 1962 at 2319 LT
Type of aircraft:
Operator:
Registration:
CF-CZB
Survivors:
Yes
Schedule:
Vancouver – Honolulu – Nadi – Auckland – Sydney
MSN:
13394
YOM:
1958
Flight number:
CP301
Location:
Crew on board:
11
Crew fatalities:
Pax on board:
29
Pax fatalities:
Other fatalities:
Total fatalities:
27
Captain / Total flying hours:
13250
Captain / Total hours on type:
920.00
Copilot / Total flying hours:
16073
Copilot / Total hours on type:
1628
Circumstances:
The aircraft had arrived in Honolulu at 0507 hours Hawaiian standard time on 21 July as CPA Flight 323 from Vancouver, British Columbia, Canada. It was departing, the evening of 22 July, as Empress Flight 301 on a scheduled international flight for Nadi (Fiji Islands), Auckland (New Zealand) and Sydney (Australia). The night takeoff was commenced at 22:38 hours local time and approximately two minutes after becoming airborne and during the climbout a fire warning indication for No 1 engine was received in the cockpit. The No. 1 propeller was feathered and the tower controller was advised that the aircraft was returning to Honolulu. As an over-gross landing weight condition existed, fuel jettisoning in the amount of 35000 lb was carried out The jettisoning operation was completed at 23:06 hours following which the flight was vectored west of the outer marker to Intercept the ILS final approach course for runway 08. The three-engine landing approach appeared normal until the aircraft had proceeded beyond the runway threshold and had commenced its landing flare at an altitude of approximately 20 feet above the runway centreline. A go-around was attempted from this position, and the aircraft banked and veered sharply to the left. Initial ground contact was made by the left wing tip approximately 550 feet to the left of the runway centreline and approximately 700 feet beyond the threshold of the runway. The aircraft progressively disintegrated as it moved across the ground, then struck heavy earth-moving equipment parked approximately 970 feet from the runway centreline.
Probable cause:
The attempted three-engine go-around, when the aircraft was in a full landing configuration, at insufficient airspeed and altitude to maintain control.
Final Report: