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Crash of a Cessna 441 Conquest II in Lakeland

Date & Time: Jan 2, 1997 at 1121 LT
Type of aircraft:
Registration:
N441MS
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lakeland - Lakeland
MSN:
441-0056
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6511
Captain / Total hours on type:
533.00
Aircraft flight hours:
4697
Circumstances:
During the takeoff roll the pilot stated the right engine had an over torque condition and he was unable to control the aircraft. The aircraft went off the runway to the left and crashed coming to rest upright. A post crash fire erupted and destroyed the aircraft. The mechanic rated passenger stated he was observing the right engine gauges during this maintenance test flight and did not observe any over torque indications. When he looked up from the instruments at about the time the aircraft should lift off, the aircraft was drifting to the left. The pilot, who was looking at the engine instruments, looked up, saw the aircraft was about to drift off the runway, and retarded both power levers. The passenger/mechanic (who was also a pilot) reported that the pilot placed the propellers in reverse. Six thousand feet of runway remained at the abort point. The aircraft pitched up and then crashed on the left wing and nose. Cessna Service Newsletter SLN99-15 and AlliedSignal Operating Information Letter OI 331-17 report an abnormality that may affect the model engine in which an uncommanded engine fuel flow increase or fluctuation may occur, resulting in an unexpected high torque and asymmetric thrust. The condition is associated with an open torque motor circuit within the engine fuel control. A system malfunction resulting in engine acceleration to maximum power would produce an overtorque of about 2,288 foot-pounds (ft-lb). This power output is restricted by a fuel flow stop in the engine fuel control. Normal takeoff power is 1,669 ft-lbs; therefore, one engine accelerating to the stop limit while one engine continued to operate normally would cause a torque differential of 619 ft-lbs. The total loss of power in one engine during takeoff while one engine continued to operate normally would result in a torque differential of 1,669 ft-lbs. The Cessna 441 Flight Manual states that at 91 knots indicated airspeed, the airplane is controllable with one engine inoperative (that is, with a torque differential between engines of up to 1,669 ft-lbs). However, if an electronic engine control failure occurs on one engine and the other engine is retarded to idle, the fuel flow to the failed engine will not be reduced, and a torque differential of about 2,288 ft-lbs will occur, at which point the airplane is uncontrollable by the pilot.
Probable cause:
Failure of the electronic engine control, which caused an overtorque condition in the right engine that made directional control of the airplane not possible by the pilot when the power to the left engine was retarded to idle during the takeoff roll.
Final Report:

Crash of a Rockwell Grand Commander 680E in Lakeland: 1 killed

Date & Time: Sep 9, 1996 at 2010 LT
Registration:
N262X
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Lakeland - Winter Haven
MSN:
680-745-38
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6893
Captain / Total hours on type:
22.00
Aircraft flight hours:
5284
Circumstances:
After takeoff, the pilot transmitted to ATC controllers that he had lost power in an engine. He made a steep turn to the left back toward the airport, then a right turn toward the runway. The aircraft's nose dropped in the right turn, and the aircraft crashed nose first on a taxiway. Post crash examination of the aircraft structure and flight control systems revealed no preimpact failure or malfunction. The left propeller was found in the feathered position, and the right propeller was found in a high blade angle. The right propeller had damage consistent with the engine operating. Teardown examination of the engines and propellers showed no findings that would have resulted in engine or propeller malfunction or failure. At the time the aircraft was purchased by the pilot in March 1996, he had not flown for about 10 years. Since purchasing the aircraft, he had logged 2.5 hours of transition/checkout in the airplane and had flown it for a total of about 22 hours, mostly on 'sightseeing flights.'
Probable cause:
Failure of the pilot to maintain minimum control speed, while returning to the airport for a precautionary landing, following a reported loss of power in one engine, which resulted in a loss of aircraft control and an uncontrolled collision with the terrain. Factors relating to the accident were: loss of power in the left engine for undetermined reason(s), and the pilot's apparent lack of familiarity with single engine operation in the make and model of aircraft.
Final Report:

Crash of a Cessna 425 Conquest in Lakeland: 1 killed

Date & Time: Feb 11, 1992 at 0602 LT
Type of aircraft:
Operator:
Registration:
N66LM
Flight Type:
Survivors:
No
Schedule:
Bartow - Lakeland
MSN:
425-0137
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10850
Circumstances:
The pilot departed VFR and flew to his destination and found it fogged in. He then requested and was given an IFR clearance for an ILS approach to another airport. He was observed to break out of the clouds at about 100 feet agl in a left bank and yaw. He then crashed short of the runway and to the left of the centerline. Examination of the airplane, engines and propellers revealed no preexisting failures. After the crash a fire partially consumed the wreckage. The pilot, sole on board, was killed.
Probable cause:
Loss of control in flight by the pilot for undetermined reasons.
Final Report:

Crash of a Beechcraft 60 Duke in Lakeland

Date & Time: Dec 1, 1985 at 0840 LT
Type of aircraft:
Operator:
Registration:
N7080D
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Bartow – Saint Petersburg
MSN:
P-30
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3381
Captain / Total hours on type:
1458.00
Aircraft flight hours:
1461
Circumstances:
The pilot stated that he experienced a loss of power in both engines, made an emergency landing in a cow pasture, and struck a cow on landing rollout. Due to the extent of post crash fire no determination could be made as to the nature of the malfunction of the engines described by the pilot.
Probable cause:
Occurrence #1: loss of engine power
Phase of operation: cruise - normal
Findings
1. (c) reason for occurrence undetermined
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
----------
Occurrence #3: on ground/water collision with object
Phase of operation: landing - roll
Findings
2. Object - animal(s)
3. Fluid, fuel - fire
Final Report:

Crash of a Piper PA-60 Aerostar (Ted Smith 600) in Eva: 6 killed

Date & Time: Sep 13, 1985 at 1111 LT
Registration:
N680CC
Flight Type:
Survivors:
No
Schedule:
Lakeland - Huntsville
MSN:
60-0031
YOM:
1970
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
1993
Captain / Total hours on type:
97.00
Circumstances:
During an IFR arrival/descent, the pilot stated he 'had to feather one engine, I have an oil leak and I'm just trying to descend . . .' he then said he was descending thru 5,300 feet. As he continued the approach, he informed the controller he would be unable to go around since the hydraulic system was powered by the affected right engine. Subsequently, the pilot said he was at 1,500 feet and was having a hard time holding altitude. A witness heard and saw the aircraft in a level attitude at low altitude, then saw the aircraft dive toward the ground. It impacted in a steep descent just short of a long field and burned. The right propeller was feathered, but there was no evidence of oil starvation in either engine. The pilot's neighbor said he (the pilot) was aware of a hydraulic leak, but he was awaiting the annual inspection (due in September) to repair it. An exam revealed the flaps were partially extended, the landing gear control was in the 'up' position, and the gear was down. The flight manual stated that with a hydraulic failure downstream of the accumulator, the flap handle should be in 'neutral' to prevent gear and flap extension. The flap control could not be found. All six occupants were killed.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: descent - normal
Findings
1. (c) reason for occurrence undetermined
2. (f) fluid - leak
----------
Occurrence #2: loss of engine power (partial) - nonmechanical
Phase of operation: descent - normal
Findings
3. Miscellaneous - intentional
----------
Occurrence #3: forced landing
Phase of operation: descent - emergency
Findings
4. (f) maintenance - inadequate - company/operator management
5. (f) operation with known deficiencies in equipment - performed - pilot in command
6. (c) emergency procedure - improper - pilot in command
7. Hydraulic system - pressure too low
8. (f) gear extension - inadvertent
9. (f) lowering of flaps - inadvertent
10. Level off - not possible
----------
Occurrence #4: loss of control - in flight
Phase of operation: descent - emergency
Findings
11. (c) airspeed (vmc) - not maintained - pilot in command
----------
Occurrence #5: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Lakeland: 2 killed

Date & Time: Dec 4, 1983 at 1446 LT
Operator:
Registration:
N4115K
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Lakeland - Lakeland
MSN:
31-8452006
YOM:
1984
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3550
Captain / Total hours on type:
600.00
Aircraft flight hours:
0
Aircraft flight cycles:
0
Circumstances:
The aircraft was on its first production flight test. Shortly after lift-off it was observed to enter an abrupt right bank, followed by a steep left bank before crashing. Examination of the left wing revealed that its aileron cables were connected to their respective bellcrank attach points backwards. Both pilots were killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
1. (c) flt control syst, aileron control - improper
2. (c) acft/equip, inadequate compliance determination - manufacturer
3. (c) aircraft preflight - inadequate - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: takeoff - initial climb
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Lakeland: 2 killed

Date & Time: Sep 2, 1982 at 1516 LT
Operator:
Registration:
N62957
Flight Type:
Survivors:
No
Schedule:
Lakeland - Lakeland
MSN:
31-7752005
YOM:
1977
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3327
Captain / Total hours on type:
179.00
Aircraft flight hours:
1255
Circumstances:
The flight was conducting single-engine flight tests with the inboard gear doors removed and was being photographed by a chase aircraft. At the end of the tests the pilot was unable to restart the left engine and returned for a single-engine landing. The pilot overshot the landing attempt and executed a single-engine go-around. The pilot then reported he had a gear problem. An occupant of the chase aircraft reported that the main gear were hanging 75 to 80 degrees from the horizontal. A company employee at the airport reported that the nose gear was about 10° aft of the normal down and locked position. The aircraft continued on a wsw heading away from the airport, passing over several suitable emergency landing sites while in a slow descent until colliding with the guy/grounding wire atop a powerline pole located 4 miles wsw of the arpt. The aircraft was destroyed and both occupants were killed.
Probable cause:
Occurrence #1: loss of engine power
Phase of operation: maneuvering
Findings
1. (c) propeller system/accessories,feathering system - undetermined
----------
Occurrence #2: in flight collision with object
Phase of operation: go-around (VFR)
Findings
2. (c) planned approach - poor - pilot in command
3. (f) go-around - initiated - pilot in command
4. (f) aborted landing - performed - pilot in command
5. (f) door,landing gear - other
6. (f) landing gear,normal retraction/extension assembly - undetermined
7. (f) gear retraction - not possible - pilot in command
8. (f) aircraft performance,engine out capability - deteriorated
9. (c) in-flight planning/decision - improper - pilot in command
10. (f) object - guy wire
Final Report: