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Crash of a Socata TBM-700 in the Ridgway Reservoir: 5 killed

Date & Time: Mar 22, 2014 at 1400 LT
Type of aircraft:
Operator:
Registration:
N702H
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bartlesville – Montrose
MSN:
112
YOM:
1996
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
908
Captain / Total hours on type:
9.00
Aircraft flight hours:
4848
Circumstances:
About 3 months before the accident, the pilot received about 9 hours of flight instruction, including completion of an instrument proficiency check, in the airplane. The accident flight was a personal cross-country flight operated under instrument flight rules (IFR). Radar track data depicted the flight proceeding on a west-southwest course at 15,800 ft mean sea level (msl) as it approached the destination airport. The flight was cleared by the air traffic controller for a GPS approach, passed the initial approach fix, and, shortly afterward, began a descent as permitted by the approach procedure. The track data indicated that the flight became established on the initial approach segment and remained above the designated minimum altitude of 12,000 ft msl. Average descent rates based on the available altitude data ranged from 500 feet per minute (fpm) to 1,000 fpm during this portion of the flight. At the intermediate navigation fix, the approach procedure required pilots to turn right and track a north-northwest course toward the airport. The track data indicated that the flight entered a right turn about 1 mile before reaching the intermediate fix. As the airplane entered the right turn, its average descent rate reached 4,000 fpm. The flight subsequently tracked northbound for nearly 1-1/2 miles. During this portion of the flight, the airplane initially descended at an average rate of 3,500 fpm then climbed at a rate of 1,800 fpm. The airplane subsequently entered a second right turn. The final three radar data points were each located within 505 ft laterally of each other and near the approximate accident site location. The average descent rate between the final two data points (altitudes of 10,100 ft msl and 8,700 ft msl) was 7,000 fpm. About the time that the final data point was recorded, the pilot informed the air traffic controller that the airplane was in a spin and that he was attempting to recover. No further communications were received from the pilot. The airplane subsequently impacted the surface of a reservoir at an elevation of about 6,780 ft and came to rest in 60 ft of water. A detailed postaccident examination of the airframe, engine and propeller assembly did not reveal any anomalies consistent with a preimpact failure or malfunction. The available meteorological data suggested that the airplane encountered clouds (tops about 16,000 ft msl or higher and bases about 10,000 ft msl) and was likely operating in IFR conditions during the final 15 minutes of the flight; however, no determination could be made regarding whether the clouds that the airplane descended through were solid or layered. In addition, the data suggested the possibility of both light icing and light turbulence between 12,000 ft msl and 16,000 ft msl along the flight path. Although the pilot appeared to be managing the flight appropriately during the initial descent, it could not be determined why he was unable to navigate to the approach fixes and maintain control of the airplane as he turned toward the airport and continued the descent.
Probable cause:
The pilot's loss of airplane control during an instrument approach procedure, which resulted in the airplane exceeding its critical angle of attack and entering an inadvertent aerodynamic stall and spin.
Final Report:

Crash of a Rockwell Aero Commander 500B in Bartlesville

Date & Time: Jan 13, 2012 at 1930 LT
Operator:
Registration:
N524HW
Flight Type:
Survivors:
Yes
Schedule:
Kansas City - Cushing
MSN:
500-1533-191
YOM:
1965
Flight number:
CTL327
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8487
Captain / Total hours on type:
3477.00
Circumstances:
The pilot was en route on a positioning flight when the airplane’s right engine surged and experienced a partial loss of power. He adjusted the power and fuel mixture controls; however, a few seconds later, the engine surged again. The pilot noted that the fuel flow gauge was below 90 pounds, so he turned the right fuel pump on. The pilot then felt a surge on the left engine, so he performed the same actions he as did for the right engine. He believed that he had some sort of fuel starvation problem. The pilot then turned to an alternate airport, at which time both engines lost total power. The airplane impacted trees and terrain about 1.5 miles from the airport. The left side fuel tank was breached during the accident; however, there was no indication of a fuel leak, and about a gallon of fuel was recovered from the airplane during the wreckage retrieval. The company’s route coordinator reported that prior to the accident flight, the pilot checked the fuel gauge and said the airplane had 120 gallons of fuel. A review of the airplane’s flight history revealed that, following the flight immediately before the accident flight, the airplane was left with approximately 50 gallons of fuel on board; there was no record of the airplane having been refueled after that flight. Another company pilot reported the airplane fuel gauge had a unique trait in that, after the airplane’s electrical power has been turned off, the gauge will rise 40 to 60 gallons before returning to zero. When the master switch was turned to the battery position during an examination of another airplane belonging to the operator, the fuel gauge indicated approximately 100 gallons of fuel; however, when the master switch was turned to the off position, the fuel quantity on the gauge rose to 120 gallons, before dropping off scale, past empty. Additionally, the fuel cap was removed and fuel could be seen in the tank, but there was no way to visually verify the quantity of fuel in the tank.
Probable cause:
The total loss of engine power due to fuel exhaustion and the pilot’s inadequate preflight inspection, which did not correctly identify the airplane’s fuel quantity before departure.
Final Report:

Crash of a Convair CV-640 in Bartlesville

Date & Time: Oct 28, 1987 at 0734 LT
Type of aircraft:
Operator:
Registration:
N3411
Flight Type:
Survivors:
Yes
Schedule:
Chicago - Oklahoma City
MSN:
31
YOM:
1966
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5389
Captain / Total hours on type:
2480.00
Aircraft flight hours:
44764
Circumstances:
The captain was cross-feeding both engines from the right tank while the first officer (f/o) was flying, without informing the f/o. The captain then left the cockpit while cross-feeding. Both tank valves and the right boost pump were on. The right tank ran dry, the right engine failed, and the prop autofeathered while the captain was absent. The captain returned, turned on the left boost pump, but left the right boost pump and the valves open, and attempted to restart the right engine. The left engine then failed but this was not recognized by the crew. The electrical system failed due to the attempted restarts and the fact that nonessential equipment was not turned off. The captain did not apply sufficient pull to the emergency gear handle to lower the gear manually. The aircraft was landed on a short wet sod runway, with the gear and flaps up, at a high rate of speed. The aircraft ran off the end of the runway, through a ditch, across a road, and into trees. Both pilots escaped uninjured.
Probable cause:
Occurrence #1: loss of engine power (total) - nonmechanical
Phase of operation: cruise - normal
Findings
1. (c) 1 engine
2. Fluid, fuel - starvation
3. (c) fuel tank selector position - inattentive - pilot in command
4. (c) crew/group coordination - improper - pilot in command
5. (f) in-flight planning/decision - improper - pilot in command
----------
Occurrence #2: loss of engine power (total) - nonmechanical
Phase of operation: cruise - normal
Findings
6. (c) all engines
7. (c) fluid, fuel - starvation
8. (c) emergency procedure - improper - pilot in command
9. (f) checklist - inadequate - company/operator management
----------
Occurrence #3: forced landing
Phase of operation: descent - emergency
Findings
10. Airspeed - excessive - copilot/second pilot
----------
Occurrence #4: gear not extended
Phase of operation: landing
Findings
11. (c) gear extension - improper use of - pilot in command
12. (f) electrical system - deteriorated
----------
Occurrence #5: on ground/water collision with object
Phase of operation: landing
Findings
13. (f) terrain condition - ditch
Final Report:

Crash of a Cessna 421C Golden Eagle III in Altus: 8 killed

Date & Time: Sep 4, 1983 at 1607 LT
Registration:
N111FN
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Altus - Bartlesville
MSN:
421C-0321
YOM:
1977
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
7620
Captain / Total hours on type:
269.00
Aircraft flight hours:
1505
Circumstances:
The pilot initiated a takeoff on a hot afternoon with 7 passengers on board. Shortly after liftoff, two witnesses observed what they described as a puff of black smoke from the right engine. According to witnesses, the aircraft turned to the left before crossing the departure end of the runway at low altitude and low speed. Subsequently, the aircraft rolled rapidly to the left and impacted the ground in a near flat attitude, with a high rate of sink, and sufficient forward velocity to slide or bounce about 70 feet before coming to rest and burning. An exam of the wreckage, including teardowns of both engines, revealed no pre-impact/mechanical malfunction or failure. The aircraft was estimated to be 80 lbs below its max design gross weight. Its center of gravity was computed to be 1.45 inches aft of its rear limit. The temperature was 101° and the density altitude was about 4,000 feet. All eight occupants were killed.
Probable cause:
Occurrence #1: loss of engine power
Phase of operation: takeoff - initial climb
Findings
1. (c) reason for occurrence undetermined
----------
Occurrence #2: loss of control - in flight
Phase of operation: maneuvering - turn to landing area (emergency)
Findings
2. (c) airspeed (VMC) - not maintained - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
3. (c) aircraft handling - not maintained - pilot in command
Final Report:

Crash of a Hawker-Siddeley HS.125-1A-522 in Taos

Date & Time: Jan 26, 1979 at 1200 LT
Type of aircraft:
Registration:
N3MF
Flight Type:
Survivors:
Yes
Schedule:
Bartlesville – Taos
MSN:
25093
YOM:
1966
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8335
Captain / Total hours on type:
60.00
Circumstances:
After touchdown on runway 04 at Taos Airport, the airplane went out of control and crashed on a snowbank. All 10 occupants escaped with minor injuries while the aircraft was damaged beyond repair.
Probable cause:
Hard landing and subsequent collision with a snowbank upon touchdown following an improper level off. The following contributing factors were reported:
- Failed to maintain directional control,
- Overload failure.
Final Report:

Crash of a Lockheed 18-14 LodeStar near Bartlesville: 8 killed

Date & Time: Dec 12, 1956 at 0850 LT
Type of aircraft:
Operator:
Registration:
N28366
Flight Phase:
Survivors:
No
Schedule:
Bartlesville – Salt Lake City
MSN:
2043
YOM:
1940
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
8837
Captain / Total hours on type:
700.00
Copilot / Total flying hours:
3000
Copilot / Total hours on type:
500
Circumstances:
The purpose of this flight was to take six passengers, all Phillips' employees. from Bartlesville, Oklahoma, to Salt Lake City, Utah. Company Pilot Joe Mark Bower and company Copilot-Mechanic Robert Ellwood Ulrich were assigned to the flight by the Aviation Department of Phillips. When the aircraft was loaded and prior to leaving the ramp Copilot Ulrich called the company radio station, located on the airport, requested taxiing instructions, and asked for an IFR clearance to Salt Lake City, nonstop. The company radio operator obtained the desired clearance from ARTC through Tulsa, and immediately relayed it to the aircraft. A flight plan previously prepared contained the following information: Proposed time of departure 0805; estimated elapsed time 5 hours, 15 minutes; fuel on board 6 hours. Departure was at 0826. At that time the gross weight of the aircraft was 19,284 pounds (maximum allowable was 19.500 pounds), and the load was properly distributed with respect to allowable center of gravity limitations. About 14 minutes after takeoff, at approximately 0840, Copilot Ulrich called Bartlesville Radio and stated that the flight was having engine trouble, with an oil temperature over 100 degrees, and requested that the IFR flight plan be canceled as they might return. The Bartlesville operator complied and notified Tulsa. At the next contact, about 0845, the copilot again called Bartlesville Radio stating that they could not unfeather the propeller. At that time he asked the Bartlesville operator to determine the condition of the runways at Tulsa (about 40 miles to the south). This information was obtained and immediately relayed to the copilot, whereupon he said. "Going to Tulsa, changing over." Bartlesville's single 4,600-foot runway had patches of snow and ice while all runways at Tulsa Airport were clear. This was the last radio contact with the flight. None of the messages had mentioned which engine was giving trouble; none indicated any anxiety or stress. There is no known record of N 28366 having made radio contact with any ground station or aircraft other than Bartlesville Radio. About the same time as the last radio contact, the Bartlesville radio operator and Phillips' chief pilot saw the aircraft passing south of the Bartlesville Airport heading easterly. They estimated its altitude to be 3,000 feet above the ground. The aircraft continued east for about 4-1/2 miles, until beyond the more congested part of Bartlesville, and then turned to the right about 90 degrees toward Tulsa. A number of persons saw the flight after it turned toward Tulsa. When it had been on this southerly heading for about four miles the aircraft was seen to plunge to earth in a manner described by several witnesses as a spin. Impact with the rolling terrain was on a heading of about 240 degrees, while the wings were about level, and while the nose-down angle was close to vertical. An explosion and intense fire ensued, largely destroying the general structure of the aircraft.
Probable cause:
The Board determines that the probable cause of this accident was loss of flying speed during single-engine flight for reasons undetermined. resulting in a spin to the ground. The following findings were reported:
- There was no indication of unairworthiness in the airframe or its controls, as far as could be learned,
- The No. 2 (right) engine, although not subject to complete examination due to ground fire, exhibited no sins of malfunctioning,
- Neither propeller nor their feathering mechanism showed any evidence of malfunctioning,
- The left engine developed a bearing failure and its propeller was feathered,
- The reason for the bearing failure cannot be isolated,
- Single-engine flight was started for a distance of 40 Miles,
- Early in this flight altitude, speed, and then control were lost, and the aircraft spun to the ground.
Final Report: