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Crash of a Carvair ATL-98 in Nixon Fork Mine

Date & Time: May 30, 2007 at 1200 LT
Operator:
Registration:
N898AT
Flight Type:
Survivors:
Yes
Schedule:
Fairbanks - Nixon Fork Mine
MSN:
42994
YOM:
1946
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
21658
Captain / Total hours on type:
13600.00
Aircraft flight hours:
55753
Circumstances:
The captain was making a VFR landing approach to a remote mining airstrip in a modified Douglas DC-4 airplane at the end of a cross-country nonscheduled cargo flight. The modified airplane had a raised cockpit above the fuselage to accommodate an upward swinging nose door. During the landing flare/touchdown, the airplane undershot the runway threshold, and right main landing gear struck the lip of the runway. The right main landing gear was torn off, which allowed the nose and right wing to collide with the runway surface. The right wing was torn off the fuselage and caught fire. The fuselage, containing the cargo of fuel bladders, slid to a stop and rolled about 90 degrees to the left. The pilot indicated that due to the additional cockpit height of the modified airplane, versus a standard Douglas DC-4 airplane, the airplane was lower than he perceived.
Probable cause:
An undershoot and collision with the runway when the pilot misjudged the distance/altitude during the landing flare/touchdown.
Final Report:

Crash of an Aviation Traders ATL-98 Carvair in Venetie

Date & Time: Jun 28, 1997 at 1618 LT
Registration:
N103
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Venetie - Fairbanks
MSN:
10273/4
YOM:
1943
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
20000
Captain / Total hours on type:
3000.00
Aircraft flight hours:
7145
Circumstances:
The air cargo flight had just off loaded its cargo at a remote site. Shortly after takeoff, the number two engine begin to run rough. The engine was shut down, and the propeller feathered. During the shutdown process, a fire warning light illuminated, and fire became visible near the number 2 engine. The crew activated both banks of engine fire extinguishers, but were unable to extinguish the fire. While on approach to an off-airport emergency landing site, the number two engine fell off and ignited a brush fire. The crew made a successful landing and ran away from the airplane. The airplane continued to burn and was destroyed by fire. The number 2 engine was not recovered or located.
Probable cause:
A fire associated with the number 2 engine for undetermined reasons.
Final Report:

Crash of an Aviation Traders ATL-98 Carvair in Griffin: 2 killed

Date & Time: Apr 4, 1997 at 0016 LT
Registration:
N83FA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Griffin – Americus – Rockford
MSN:
5/10365
YOM:
1944
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
12000
Captain / Total hours on type:
1000.00
Aircraft flight hours:
50558
Circumstances:
During the airplane's takeoff roll, about 3/4 down the 3,700 foot runway, a witness reported that the color of the #1 exhaust flame changed from blue to yellow, accompanied by an audible change in the engine power level. The nose of the airplane yawed left and the left wing dipped. Directional control was regained and the takeoff continued. Skid marks were found about 650 feet before the departure end of the runway that continued about 1360 feet to an abandoned grocery store impacted by the plane. About 315 feet before the building, the left wing contacted a privacy fence, and a utility pole, resulting in a fire at the disrupted left wing main fuel tank. A pilot/mechanic who helped dispatch the airplane observed that the elevator was free as it taxied. Fire damage to all engines precluded a detailed post crash examination of essential fuel and ignition systems. The toxicological report regarding the second pilot indicated that 1.110 mcg/ml (ug/ml, ug/g) of Diphenhydramine, was detected in the blood. According to NTSB medical personnel, Diphenhydramine is a sedating antihistamine often found in over-the-counter allergy medications. A single oral dose of medication containing Diphenhydramine, at twice the recommended maximum of over-the-counter dosage, resulted in maximal blood levels of between 0.08 and 0.16 mcg/ml. The level of Diphenhydramine found during the toxicology examination of the second pilot approximated ten times the levels found following a dosage at twice the recommended strength. Diphenhydramine was also found in the urine. Additional prescription and nonprescription medications were also found during the toxicological examination of the second pilot.
Probable cause:
The flightcrew's inadequate procedures, during a rejected takeoff following a possible engine malfunction at a critical time in the takeoff, and the second pilot's physical impairment.
Final Report:

Crash of a Aviation Traders ATL-98 Carvair in Le Touquet

Date & Time: Mar 18, 1971
Operator:
Registration:
G-APNH
Survivors:
Yes
Schedule:
Southend – Le Touquet
MSN:
11/18333
YOM:
1965
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
11
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The approach to Le Touquet Airport was completed in strong crosswinds. Upon touchdown, the nose gear collapsed and the airplane came to rest 1,550 meters from threshold. All 18 occupants were evacuated safely while the aircraft was considered as damaged beyond repair.

Crash of a Aviation Traders ATL-98 Carvair in Miami: 10 killed

Date & Time: Jun 23, 1969 at 1542 LT
Operator:
Registration:
HI-168
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Miami - Santo Domingo
MSN:
16/10485
YOM:
1944
Flight number:
DO401
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
13736
Captain / Total hours on type:
500.00
Copilot / Total flying hours:
2333
Copilot / Total hours on type:
476
Aircraft flight hours:
41722
Circumstances:
Shortly after takeoff from 12 at Miami-Intl Airport, while climbing to a height of 300 feet, the crew reported engine problems and elected to return. He was cleared for an emergency landing on runway 27 and initiated a circuit when control was lost. The airplane stalled and crashed in a huge explosion onto several buildings located about a mile short of runway 27. Few buildings and cars were destroyed. All four occupants on board the Carvair were killed as well as six people on the ground. 12 other people were injured, some of them seriously. It was later reported that white smoke was coming from the engine number two and black fumes from the engine number four.
Probable cause:
The confused action on the part of the crew while attempting to cope with the catastrophic failure of an engine during takeoff.
Final Report:

Crash of a Aviation Traders ATL-98 Carvair in Twin Falls

Date & Time: Sep 28, 1968
Operator:
Registration:
CF-EPX
Survivors:
Yes
Schedule:
Goose Bay – Twin Falls
MSN:
6/7480
YOM:
1944
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
33
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot, who had limited experience on Carvair aircraft, possibly wanted to touch down as early as possible on the short runway. The main wheels however struck the top of an embankment about 8 feet from the runway threshold. The pilot overshoot and had to feather the no. 2 prop immediately, because the engine was not developing power. The aircraft circled for a while and then touched down on its nosegear. The plane settled on the left wing and swung off the runway.
Probable cause:
The pilot's distraction with the landing hazard led him to attempt a touchdown dangerously close to the runway threshold. The pilot was assigned to perform a landing on a marginal landing area.

Crash of a Aviation Traders ATL-98 Carvair in Karachi: 13 killed

Date & Time: Mar 8, 1967
Operator:
Registration:
F-BMHU
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Karachi - Tokyo
MSN:
4/10338
YOM:
1962
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
13
Circumstances:
Shortly after takeoff, the airplane encountered difficulties to gain height when it struck a bridge over Drig Road and crashed. All six crew members and seven people on the ground were killed.
Probable cause:
Failure of the right engine during initial climb while the left engine did not provide sufficient power.

Crash of a Aviation Traders ATL-98 Carvair in Rotterdam: 1 killed

Date & Time: Dec 28, 1962 at 1055 LT
Operator:
Registration:
G-ARSF
Survivors:
Yes
Schedule:
Southend – Rotterdam
MSN:
3/18339
YOM:
1962
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6534
Captain / Total hours on type:
450.00
Copilot / Total flying hours:
6014
Copilot / Total hours on type:
201
Circumstances:
The crew was completing a visual approach to Rotterdam-Zestienhoven Airport in conditions of snow (visibility 1460 m). During the final approach the landing gear struck a 6 feet high dyke located 800 feet short of the runway threshold. The plane bounced and struck the ground heavily 200 feet further on. The right was sheared off and the aircraft crashed upside down in a snow covered field. The captain was killed and the copilot was seriously injured. Two other crew members were injured while all 14 passengers were unhurt.
Probable cause:
The accident was due to the fact that the commander carried out the final stage of approach below the normal glide path with insufficient engine power, as a result of which the speed of descent was too high in relation to the horizontal distance still to be covered to the beginning of the runway. Consequently, the aircraft, at a high vertical speed, hit a dyke, after facing the direction of approach. The Board was of the opinion that even if there had been no dyke, and it was not an obstruction of any significant height, the aircraft would still have hit the ground a considerable distance short of the runway threshold, although possibly with less fatal consequences than in the present instance.
Final Report: