Crash of a Convair CV-580 in Santa Barbara

Date & Time: Nov 12, 1968 at 1728 LT
Type of aircraft:
Registration:
N73135
Flight Type:
Survivors:
Yes
Schedule:
Santa Barbara - Santa Barbara
MSN:
85
YOM:
1968
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4741
Captain / Total hours on type:
866.00
Circumstances:
Following an uneventful training flight in the region of Santa Barbara Airport, the aircraft belly landed, slid for few dozen yards and came to rest on the runway. All four occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
The accident was caused by the combination of the following factors:
- The student pilot failed to extend the landing gear on approach,
- Inadequate supervision of flight on part of the pilot-in-command,
- The crew failed to use the approach checklist,
- The landing gear warning horn was inoperative for undetermined reason.
Final Report:

Crash of a Grumman G-21A Goose off Avalon: 1 killed

Date & Time: Sep 29, 1968 at 1400 LT
Type of aircraft:
Registration:
N325
Flight Phase:
Flight Type:
Survivors:
No
MSN:
B127
YOM:
1945
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
14000
Captain / Total hours on type:
3000.00
Circumstances:
While flying at low height, the pilot lost control of the seaplane that crashed into the sea few dozen yards off Avalon. Few debris were found floating on water but the pilot's body was never found.
Probable cause:
Due to lack of evidences, the cause of the accident could not be determined.
Final Report:

Crash of a Lockheed L-1649A Starliner in Stockton

Date & Time: Sep 28, 1968 at 1613 LT
Type of aircraft:
Registration:
N8081H
Flight Type:
Survivors:
Yes
Schedule:
Stockton - Stockton
MSN:
1026
YOM:
1958
Crew on board:
3
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local training flight at Stockton Airport, California. Following several uneventful circuits, the crew initiated a new approach. On final, the crew failed to realize his altitude was too low when the right main gear struck a blast pad located 102 feet short of the runway threshold and was torn off. The airplane partially belly landed and slid for dozen yards before coming to rest. While all 11 occupants escaped uninjured, the aircraft was damaged beyond repair.
Probable cause:
The student pilot misjudged the distance and altitude on final and the pilot-in-command failed to supervise the flight adequately.
Final Report:

Crash of a Rockwell 1121A Jet Commander in Hollywood: 3 killed

Date & Time: Sep 13, 1968 at 0723 LT
Operator:
Registration:
N148E
Flight Type:
Survivors:
No
Schedule:
Santa Monica - Hollywood
MSN:
1121-022
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
11164
Captain / Total hours on type:
6121.00
Circumstances:
While on final approach to Hollywood-Burbank Airport on a positioning flight from Santa Monica, the airplane adopted a nose-down attitude, struck power cables, hit a house and crashed in a wasteland located few miles short of runway. Both pilots and one people on the ground were killed. The aircraft was destroyed as well as several cars. A house was also damaged.
Probable cause:
Uncontrolled descent caused by vortex turbulences from a preceding aircraft with separation of approximately 3 minutes and 15 seconds.
Final Report:

Crash of a Boeing KC-135A-BN Stratotanker on Mt Lassen: 9 killed

Date & Time: Jul 30, 1968
Type of aircraft:
Operator:
Registration:
56-3655
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Castle - Castle
MSN:
17404
YOM:
1958
Crew on board:
9
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
9
Aircraft flight hours:
6089
Circumstances:
The crew departed Castle AFB on a training mission. After completing a simulated emergency descent from FL390 to FL230, the pilot-in-command initiated a sharp turn when control was lost. The airplane crashed on Mt Lassen and was totally destroyed. All nine crew members were killed.
Probable cause:
It was determined that the loss of control was the consequence of the physical loss of the stabilizer which detached during the sharp turn, maybe due to overload.

Crash of a De Havilland DH.104 Dove 1 in Colusa County

Date & Time: Jul 9, 1968 at 0954 LT
Type of aircraft:
Registration:
N4914V
Survivors:
Yes
MSN:
04273
YOM:
1949
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2200
Captain / Total hours on type:
250.00
Circumstances:
While completing a regional executive flight, one of the engine failed in flight. The pilot decided to divert to Colusa County but on approach, his position was wrong so he decided to make a go-around when the airplane struck power cables, stalled and crashed in a field. All four occupants were injured and the aircraft was damaged beyond repair.
Probable cause:
The accident was the consequence of the following factors:
- Engine failure,
- Mismanagement of fuel,
- Fuel starvation,
- Improper in-flight decision,
- Improper decision to abort landing while on single engine.
Final Report:

Crash of a Waco UIC in San Luis Obispo: 4 killed

Date & Time: Apr 27, 1968 at 1314 LT
Type of aircraft:
Operator:
Registration:
N13066
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
San Luis Obispo - San Luis Obispo
MSN:
3716
YOM:
1933
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
After completing touch-and-go, the pilot increased engine power and elected to takeoff. While climbing, the airplane stalled and crashed, killing all four occupants.
Probable cause:
The pilot failed to obtain/maintain flying speed and the aircraft entered an abnormally steep climb after touch-and-go and crashed.
Final Report:

Crash of a Lockheed P-3B-95-LO Orion at Moffett AFB

Date & Time: Apr 11, 1968
Type of aircraft:
Operator:
Registration:
A9-296
Flight Type:
Survivors:
Yes
Schedule:
Moffett - Moffett
MSN:
5406
YOM:
1968
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local test flight on this new aircraft which should be delivered to the Royal Australian Air Force. Upon landing, one of the main landing gear collapsed and the airplane came to rest in flames. While all four crew members escaped uninjured, the aircraft was destroyed by fire.
Probable cause:
Undercarriage collapsed upon landing.

Crash of a Rockwell Commander 680E near Lake Hughes: 1 killed

Date & Time: Mar 7, 1968 at 1723 LT
Operator:
Registration:
N6243B
Flight Phase:
Survivors:
No
Site:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
While completing a regional executive flight, the pilot encountered technical problems en route and elected to make an emergency landing. While flying over mountainous terrain, he attempted a wheels-up landing on a hillside when the airplane crashed. The burned wreckage was found a day later and the pilote, sole on board, was killed.
Probable cause:
Improper operation of powerplant on part of the pilot. Conditions conducive to carburetor/induction systems icing.
Final Report:

Crash of a Beechcraft E18S in San Diego: 3 killed

Date & Time: Jan 8, 1968 at 1040 LT
Type of aircraft:
Registration:
N82B
Flight Phase:
Survivors:
Yes
MSN:
BA-149
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
7224
Captain / Total hours on type:
477.00
Circumstances:
Shortly after takeoff from Lindbergh Field, while climbing at a height of 50 feet, the pilot made a sharp turn when the aircraft stalled and crashed ion flames. A passenger was seriously injured while three other occupants were killed.
Probable cause:
Engine failure after rotation caused by a cracked shroud on the third stage stator assembly due to fatigue fracture. The pilot used minimum runway length for takeoff and minimum takeoff speed.
Final Report: