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Crash of a Piper PA-31-350 Navajo Chieftain in Easton: 1 killed

Date & Time: Jul 11, 2006 at 1735 LT
Operator:
Registration:
N40ST
Flight Type:
Survivors:
No
Schedule:
Spokane - Seattle
MSN:
31-7405183
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1430
Captain / Total hours on type:
102.00
Aircraft flight hours:
3646
Circumstances:
While cruising en route in VFR conditions, the aircraft lost power on both engines. The pilot attempted an emergency forced landing at a nearby unpaved State airport, but after encountering a 20 mph tailwind on downwind and a 20 mph headwind on final, the aircraft impacted a tall conifer tree while about one-half mile from the approach end of the runway. The reason for the dual engine power loss was not determined.
Probable cause:
The loss of power in both engines for undetermined reasons while in cruise flight, leading to an attempted forced landing. Factors include unfavorable winds at the site of the forced landing, and trees off the approach end of the grass runway the pilot was attempting to land on.
Final Report:

Crash of a Cessna 401A in Spokane: 3 killed

Date & Time: Jan 8, 1996 at 1907 LT
Type of aircraft:
Registration:
N117AC
Flight Type:
Survivors:
Yes
Schedule:
Pasco - Spokane
MSN:
401A-0040
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3500
Captain / Total hours on type:
70.00
Aircraft flight hours:
5800
Circumstances:
The pilot received abbreviated weather briefing for emergency medical service (EMS)/air ambulance flight. Before flight, he expressed anxiety about possible low visibility for landing and timely transport of dying patient. During ILS runway 03 approach (rwy 03 approach), the aircraft remained well above the glide slope until close to the middle marker; aircraft's speed decreased from 153 to 100 kts, while vertical speed increased from 711 feet/min to about 1,250 feet/min descent. About 1 mile from runway and 500 feet agl (in fog), the aircraft abruptly turned left of localizer course and gradually descended with no distress call from pilot. The aircraft hit a pole, then flew into a building and burned. Low ceiling, fog and dark night conditions prevailed. Pilot (recent ex military helicopter pilot) had logged/reported 3,500 hours of flight time and about 150 hours in multiengine airplanes, but there was evidence he lacked experience with actual instrument approaches in fixed wing aircraft; he had difficulty with instrument flying during recent training and FAA check flights. No preimpact mechanical problem was found with aircraft/engines. No ILS anomalies were found. Flight nurse was using cellular phone, but no evidence was found of interference with aircraft's navigational system. Visibility and ceiling at destination were less than forecast at time of pilot's preflight weather briefing. Paramedic was only survivor.
Probable cause:
Failure of the pilot to follow proper IFR procedures, by failing to maintain proper alignment with the localizer course during the ILS approach and/or by failing to follow the proper missed approach procedure. Factors relating to the accident were: darkness; adverse weather conditions; and pressure on the pilot to complete the EMS flight, due to the circumstances and conditions that prevailed.
Final Report:

Crash of a Convair CV-440F Metropolitan in Spokane

Date & Time: Jan 4, 1996 at 1853 LT
Operator:
Registration:
N358SA
Flight Type:
Survivors:
Yes
Schedule:
Phoenix - Spokane
MSN:
153
YOM:
1954
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5194
Captain / Total hours on type:
817.00
Aircraft flight hours:
8642
Circumstances:
Before the ferry flight, the pilot (PIC) & inexperienced copilot noted the left & right, float-type, underwing, fuel gauges indicated about 3,900 & 4,050 lbs of fuel, respectively. After takeoff, they noted that the cockpit gauges showed an opposite fuel imbalance of 4,100 & 3,600 lbs in the left & right tanks. Due to this indication, the PIC crossfed fuel from the left tank to both engines for about 30 min to rectify the perceived fuel imbalance. Later as they approached the destination, the left tank was exhausted of fuel, & the left engine lost power, although the left gauge indicated about 500 lbs of fuel remaining in that tank. The PIC then crossfed fuel from the right tank to both engines, & left engine power was restored. ATC vectored the flight for an emergency ILS runway 3 approach. The PIC was distracted during the approach & maneuvered the airplane to re-intercept the localizer. About 500' agl in IMC, both engines lost power. During a forced landing at night, the airplane struck a raised berm & was damaged. No evidence of fuel was found in the left tank; 125 gal of fuel was found in the right tank. Unusable fuel was published as 3 gal. During an exam of the engines & fuel system components, no preimpact failure was found. Historical data from the manufacturer indicated that when the airplane had a low fuel state, unporting of fuel tank outlets could occur during certain maneuvers. This information was not in the Convair 340 flight manual, although unporting of the outlets on this flight was not verified.
Probable cause:
The pilot's improper management of the fuel/system, which resulted in loss of power in both engines, due to fuel starvation. Factors relating to the accident were: false indications of the cockpit fuel gauges, darkness, and the presence of a berm in the emergency landing area.
Final Report:

Crash of a Cessna 340A on Mt Spokane: 1 killed

Date & Time: Dec 13, 1995 at 1816 LT
Type of aircraft:
Registration:
N5GM
Flight Phase:
Survivors:
No
Site:
Schedule:
Spokane – Sandpoint
MSN:
340A-0317
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3500
Captain / Total hours on type:
132.00
Circumstances:
The pilot's departure plans were changed, when, instead of flying direct to his originally planned destination, he was asked to pick up a passenger at another airport prior to returning home. He departed for his alternative destination in dark night conditions, leveled off at his cruise altitude and impacted the side of a mountain in level flight about 25 miles from his departure point. Air Traffic Control vectored another aircraft to the vicinity after communications and radar contact were lost. The crew of that aircraft stated that instrument meteorological conditions prevailed at the time in the vicinity of the crash site.
Probable cause:
The pilot's failure to maintain terrain clearance in mountainous terrain. Factors contributing to the accident were: dark night conditions, mountainous terrain, and instrument meteorological conditions.
Final Report:

Crash of a Douglas DC-3C in Spokane: 2 killed

Date & Time: Mar 18, 1994 at 0156 LT
Type of aircraft:
Operator:
Registration:
N3433Y
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Spokane - Portland
MSN:
43089
YOM:
1947
Flight number:
SAL2991
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3877
Captain / Total hours on type:
3114.00
Aircraft flight hours:
37190
Circumstances:
Shortly after takeoff, the copilot reported that the flight was returning with the right engine shut down. Seconds later, the tower controller saw a fire. The airplane collided with level terrain, 3,450 feet from the end of runway 21 in a 75° to 80° nose down attitude. The right engine propeller was found in the feathered position. The left engine indicated evidence that it was producing power at the time of impact. A fatigue crack was found that separated the head from the barrel on the number eight cylinder of the right engine. No other evidence was found to indicate a mechanical failure or malfunction. Both pilots were killed.
Probable cause:
The failure of the pilot-in-command to maintain airspeed. Factors to the accident were: cylinder fatigue, dark night and stall encountered.
Final Report:

Crash of a Rockwell Grand Commander 680FL in Lester: 1 killed

Date & Time: Dec 25, 1992 at 2137 LT
Operator:
Registration:
N111MN
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Seattle - Spokane
MSN:
680-1806-150
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3108
Captain / Total hours on type:
138.00
Aircraft flight hours:
11219
Circumstances:
After departure, the airplane intercepted airway V-2, and appeared to climb normally until reaching 8,300 feet (9,000 assigned) while tracking approximately 110° magnetic. Radar analysis showed the airplane at 128 kias when it abruptly turned left 30° and then appeared to recover. Voice communication during this event was normal with no change in the pilot's level of anxiety. Immediately thereafter, the heading changed over 90° to the left (northbound), and a maximum 6,750 fpm rate of descent developed before the heading stabilized and the descent slowed. The airplane's ground impact site was approximately 1 nm southwest of the last radar target. Wreckage distribution was roughly parallel to V-2. The airplane impacted the mountainside in a steep nose low, left wing down attitude. The engines, propellers/governors were disassembled and inspected with no evidence of mechanical malfunction. Exam of the left propeller indicated low power on impact. There was no evidence of significant icing/turbulence. The pilot, sole on board, was killed.
Probable cause:
The exact cause of the accident could not be determined.
Final Report:

Crash of a De Havilland Dash-8-100 in Seattle

Date & Time: Apr 16, 1988 at 1832 LT
Operator:
Registration:
N819PH
Survivors:
Yes
Schedule:
Seattle - Spokane
MSN:
061
YOM:
1986
Flight number:
QX2658
Crew on board:
3
Crew fatalities:
Pax on board:
37
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9328
Captain / Total hours on type:
981.00
Copilot / Total flying hours:
3849
Copilot / Total hours on type:
642
Aircraft flight hours:
3106
Aircraft flight cycles:
4097
Circumstances:
Shortly after takeoff from Seattle-Tacoma Intl Airport, the crew noted a right engine power loss and decided to return for a precautionary landing. After lowering the landing gear, a massive fire was discovered in the right engine nacelle. After landing, directional control and all braking were lost. The aircraft departed the left side of the runway 16L after the left power lever was moved to flight idle. The f/o advised tower that the aircraft was out of control. The aircraft rolled onto the ramp area where it struck a runway designator sign, ground equipment, and jetways B7 and B9. The aircraft was subsequently destroyed by fire. Investigation revealed that during overhaul the high pressure fuel filter cover was improperly installed on the engine and the improper installation was not discovered drg company installation of the engine on the aircraft. This led to a massive fuel leak and the nacelle fire. The fire/explosion caused the loss of the engine panels, reducing the effectiveness of the fire suppression system and allowing other systems to be damaged.
Probable cause:
Improper installation of the high-pressure fuel filter cover that allowed a massive fuel leak and subsequent fire to occur in the right engine nacelle. The improper installation probably occurred at the engine manufacturer; however, the failure of airline maintenance personnel to detect and correct the improper installation contributed to the accident. Also contributing to the accident was the loss of the right engine centre access panels from a fuel explosion that negated the fire suppression system and allowed hydraulic line burn-through that in turn caused a total loss of airplane control on the ground.
Final Report:

Crash of a Beechcraft 99A Airliner in Spokane: 7 killed

Date & Time: Jan 20, 1981 at 1127 LT
Type of aircraft:
Operator:
Registration:
N390CA
Survivors:
Yes
Schedule:
Seattle - Moses Lake - Spokane
MSN:
U-101
YOM:
1969
Flight number:
CZ201
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
11680
Captain / Total hours on type:
7000.00
Copilot / Total flying hours:
8242
Copilot / Total hours on type:
3102
Aircraft flight hours:
23322
Circumstances:
The aircraft crashed during an instrument approach in IMC at Spokane-Intl Airport. The aircraft hit a hill about 4.5 miles from the runway threshold at an elevation of 2,546 feet. The minimum descent altitude for the instrument approach procedure was 2,760 feet. Of the nine persons aboard flight 201, seven were killed and two were injured seriously. The instrument approach procedure the fiightcrew used required that a altitude of 3,500 feet be maintained until the aircraft passed the final approach fix, located 4,5 miles from the runway threshold. The aircraft impacted the ground near the location of the final approach fix, which was about 1,800 feet southeast of the Spokane VORTAC.
Probable cause:
A premature descent to minimum descent altitude (MDA) based on the flight crew's use of an incorrect distance measuring equipment (DME) frequency and the flight crew's subsequent failure to remain at or above MDA. Contributing to the cause of the accident was the design of the DME mode selector which does not depict the frequency selected and the failure of the flight crew to identify the localizer DME facility.
Final Report:

Crash of a Boeing B-17B Flying Fortress at Geiger Field: 5 killed

Date & Time: Dec 17, 1941
Operator:
Registration:
38-267
Flight Type:
Survivors:
Yes
MSN:
2026
YOM:
1938
Crew on board:
8
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
After takeoff from Spokane-Geiger Field, while climbing, one of the engine failed. The pilot circled the airfield and elected to return for an emergency landing when the airplane crashed on short final. Five crew members were killed and three others were injured. One of 500 pounds bombs detonated on impact.
Crew:
Cpt Eugene Dimitry Zadontseff, pilot,
S/Sgt Ester Brannon,
Cpl Clarence A. Cunningham,
1st Lt Elbert D. Hoffman,
Avc Edwin Bruce Perkins.
Probable cause:
Engine failure after takeoff.

Crash of a North American B-25A Mitchell in Spokane

Date & Time: Jul 25, 1941
Operator:
Registration:
40-2223
Flight Type:
Survivors:
Yes
MSN:
62A-2892
YOM:
1941
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed on landing for unknown reasons. There were no casualties.