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Crash of a Beechcraft B200 Super King Air in Wichita: 4 killed

Date & Time: Oct 30, 2014 at 0948 LT
Registration:
N52SZ
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wichita – Mena
MSN:
BB-1686
YOM:
1999
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
3139
Aircraft flight hours:
6314
Aircraft flight cycles:
7257
Circumstances:
The airline transport pilot was departing for a repositioning flight. During the initial climb, the pilot declared an emergency and stated that the airplane "lost the left engine." The airplane climbed to about 120 ft above ground level, and witnesses reported seeing it in a left turn with the landing gear extended. The airplane continued turning left and descended into a building on the airfield. A postimpact fired ensued and consumed a majority of the airplane. Postaccident examinations of the airplane, engines, and propellers did not reveal any anomalies that would have precluded normal operation. Neither propeller was feathered before impact. Both engines exhibited multiple internal damage signatures consistent with engine operation at impact. Engine performance calculations using the preimpact propeller blade angles (derived from witness marks on the preload plates) and sound spectrum analysis revealed that the left engine was likely producing low to moderate power and that the right engine was likely producing moderate to high power when the airplane struck the building. A sudden, uncommanded engine power loss without flameout can result from a fuel control unit failure or a loose compressor discharge pressure (P3) line; thermal damage prevented a full assessment of the fuel control units and P3 lines. Although the left engine was producing some power at the time of the accident, the investigation could not rule out the possibility that a sudden left engine power loss, consistent with the pilot's report, occurred. A sideslip thrust and rudder study determined that, during the last second of the flight, the airplane had a nose-left sideslip angle of 29°. It is likely that the pilot applied substantial left rudder input at the end of the flight. Because the airplane's rudder boost system was destroyed, the investigation could not determine if the system was on or working properly during the accident flight. Based on the available evidence, it is likely that the pilot failed to maintain lateral control of the airplane after he reported a problem with the left engine. The evidence also indicates that the pilot did not follow the emergency procedures for an engine failure during takeoff, which included retracting the landing gear and feathering the propeller. Although the pilot had a history of anxiety and depression, which he was treating with medication that he had not reported to the Federal Aviation Administration, analysis of the pilot's autopsy and medical records found no evidence suggesting that either his medical conditions or the drugs he was taking to treat them contributed to his inability to safely control the airplane in an emergency situation.
Probable cause:
The pilot's failure to maintain lateral control of the airplane after a reduction in left engine power and his application of inappropriate rudder input. Contributing to the accident was the pilot's failure to follow the emergency procedures for an engine failure during takeoff. Also contributing to the accident was the left engine power reduction for reasons that could not be determined because a postaccident examination did not reveal any anomalies that would have precluded normal operation and thermal damage precluded a complete examination.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) in Cleburne

Date & Time: Jul 22, 2010 at 1100 LT
Operator:
Registration:
N601AT
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cleburne - Mena
MSN:
61-0332-095
YOM:
1976
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
28000
Captain / Total hours on type:
332.00
Circumstances:
After takeoff, the right engine experienced a loss of power followed by the left engine losing power. The pilot maneuvered the airplane toward the nearest open field and the airplane impacted terrain during landing, resulting in a circumferential split in fuselage near the aft pressure bulkhead. The airplane was equipped with 4 fuel tanks: 2 located in each wing outboard of the engine nacelle (65-gallon capacity), 1 main fuselage tank (about 44-gallon capacity), and 1 auxiliary tank located in forward section of baggage compartment (45-gallon capacity). The airplane was capable of carrying 209.5 gallons usable fuel and the pilot stated that prior to departure he filled the main fuselage tank to capacity, added 20 gallons in the auxiliary tank and 25 gallons in each wing tank, which he equated to a total of 131 gallons on board. The fuselage contained two fuel filler necks, one for each fuselage tank (main and auxiliary). The auxiliary tank was clearly placarded with a red placard visibly standing out against a silver paint stripe; the main tank was not clearly placarded, with a red placard blending easily with red paint stripe. A salvage retriever recalled that during recovery the left wing contained 17 gallons of fuel, the right wing contained 57 gallons of fuel, the main fuselage tank contained 2.5 gallons of fuel, and the auxiliary fuselage tank contained 28 gallons of fuel. A postaccident examination of the airplane and engines revealed no anomalies that would have precluded normal operation. The main fuselage tank and auxiliary fuselage tank were not breached and the fuel sumps contained check valves which prevent the back-flow of fuel from one fuel tank to another. Based on the evidence it is likely that the pilot exhausted the airplane's fuel supply in the main fuselage tank, which resulted in the loss of power to both engines.
Probable cause:
A total loss of engine power due to fuel starvation as a result of the pilot’s improper fuel management. Contributing to the accident were the critical fuel placards that were difficult to see due to the airplane's paint scheme.
Final Report:

Crash of a Beechcraft 1900C in Eagleton: 3 killed

Date & Time: Dec 9, 2002 at 1140 LT
Type of aircraft:
Operator:
Registration:
N127YV
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Wichita - Mena
MSN:
UC-127
YOM:
1990
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
10200
Aircraft flight hours:
12473
Circumstances:
The aircraft collided with mountainous terrain in a level descent during a visual approach to the destination airport. According to recorded radar data, 10 minutes after descending from 15,000 feet, the flight impacted about 200 feet below the top of the partially obscured ridgeline (elevation of 2550 feet), and 8 miles from the destination. The data indicates the flight path was similar to the global positioning satellite (GPS) approach to the airport. Six minutes before the accident, and the pilot's last transmission to air traffic control, he was informed and acknowledged that radar service was terminated. The flight was 12.4 miles from the accident site when radar contact was lost. Reduced visibility due to fog hampered search & rescue efforts, and the aircraft wreckage was located the next day. The aircraft was equipped with a GPS navigation system; however the installation was incomplete, restricting its use to visual flight rules (VFR) only. The investigation did not determine if the GPS was being used at the time. A non-enhanced Ground Proximity Warning System was also installed. The maximum elevation figure listed on the sectional aeronautical chart covering the area of the accident site and destination airport was 3000 feet mean sea level. The chart also shows an advisory for the area to use caution due to rapidly rising.
Probable cause:
In-flight collision with terrain due to the pilot's failure to maintain clearance and altitude above rapidly rising terrain while on a VFR approach. Contributing factors were the obscuration of the terrain due to clouds.
Final Report:

Crash of a Cessna 501 Citation I in Umpire: 1 killed

Date & Time: Dec 2, 1998 at 1216 LT
Type of aircraft:
Operator:
Registration:
N501EZ
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Mena - Texarkana
MSN:
501-0058
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3700
Aircraft flight hours:
5874
Aircraft flight cycles:
5436
Circumstances:
The certificated commercial pilot picked up his newly painted airplane for a visual flight to the home base. About 17 miles south of the departure airport, witnesses initially observed the airplane in a 90 degree right bank. It continued to roll to an inverted position while simultaneously nosing down to a near vertical descent. The pilot's second class medical certificate application (July 7, 1997) indicated 3,700 hours flight time. A flight log indicted the pilot flew this aircraft 6.4 hours during the 60 days preceding the accident. No evidence was found that the pilot had not obtained sufficient rest before the flight. There was no evidence found to either suggest a medical cause for incapacitation or to rule out incapacitation for medical reasons. Aircraft maintenance records did not reveal any open discrepancies. All of the airplane was accounted for in the wreckage debris. No evidence of an in-flight fire and/or explosion, or in-flight mechanical and/or flight control malfunction was found.
Probable cause:
The pilot's in flight loss of control for undetermined reasons.
Final Report:

Crash of a Cessna 414A Chancellor in Mena: 2 killed

Date & Time: Feb 15, 1984 at 1656 LT
Type of aircraft:
Operator:
Registration:
N6815Z
Flight Type:
Survivors:
No
Schedule:
Addison - Mena
MSN:
414A-0648
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
10100
Aircraft flight hours:
411
Circumstances:
The aircraft was cleared for Mena NDB approach and to maintain 5,000 feet msl until established on the approach. Aircraft descended to 4,800 feet msl on approximately ground track of 040° to 030° after NDB passage. Aircraft then turned to a ground track of 116°. After 12 seconds the aircraft turned to a ground track of 350° during which the ground speed decreased to 93 knots. The aircraft descended to 4,600 feet msl with ground speed increasing to 140 knots. N68152 reported 'we've broken below - will cancel in just a moment.' Radar contact was lost with the aircraft descending to 3,000 feet msl on a heading of 304°. The wreckage was found 6 miles northwest of the airport at an elevation of 2,000 feet msl. The outbound approach heading is 080° with procedure turn heading of 125° and 305°. Reported winds aloft at 5,000 feet msl, 4,000 feet msl and 3,000 feet msl were 191° at 34 knots, 169° at 30 knots and 151° at 32 knots respectively. Both occupants were killed.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: approach - faf/outer marker to threshold (IFR)
Findings
1. (f) compensation for wind conditions - not performed - pilot in command
2. (f) minimum descent altitude - not attained - pilot in command
3. (c) ifr procedure - not followed - pilot in command
4. (f) terrain condition - mountainous/hilly
5. (f) weather condition - low ceiling
6. (f) object - tree(s)
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Mena

Date & Time: Jul 12, 1978 at 1015 LT
Registration:
N404RC
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Mena - Mena
MSN:
31-7552060
YOM:
1975
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3815
Captain / Total hours on type:
125.00
Circumstances:
The pilot, sole on board, was performing a local test flight at Mena Airport. During initial climb, one of the engine failed. He elected to return but misjudged his altitude and clearance when the airplane struck trees and crashed near the airport. The aircraft was destroyed and the pilot was injured.
Probable cause:
Powerplant failure for undetermined reasons. The following findings were reported:
- Misjudged altitude and clearance,
- High obstructions,
- Complete engine failure,
- Forced landing of airport on land.
Final Report: