Crash of a Boeing 707-3F9C in Kiri Kasama: 3 killed

Date & Time: Dec 19, 1994 at 1906 LT
Type of aircraft:
Operator:
Registration:
5N-ABK
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Jeddah - Kano
MSN:
20669
YOM:
1972
Flight number:
WT9805
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Aircraft flight hours:
31477
Circumstances:
The aircraft was on a cargo flight from Jeddah (JED) to Kano (KAN). The total cargo uplift was 35 tonnes packed in 13 pallets and some loose bundles of merchandise that were loaded in the lower cargo hold. The departure from Jeddah was delayed for thirteen hours because of problems starting the n°4 engine. The Boeing 707 departed at 13:48 UTC. As the aircraft approached N'Djamena at FL350, about 17:00 UTC, the flight engineer noted a strange smell in the cockpit. The ground engineer and the loadmaster who were sitting in the cargo compartment area of the aircraft confirmed that the smell had persisted for a while around them. It appeared that the area around pallet number 11 was misty. The pallet was sprayed with a fire extinguisher and the smoke evacuation procedure was carried out. This stopped the fumes temporarily. The aircraft was now halfway between N'Djamena and Kano with about 40 minutes flight time to go. At 18:00 the flight was cleared to descend. Then the Master Warning sounded, followed one minute later by a Fire Warning. Smoke entered the cabin. A descent was initiated with a descent rate close to 3,000 feet per minute. Later the pitch trims became ineffective before the aircraft crashed into marshland. Tire ground marks at the scene of the accident indicated that the aircraft must have descended very slowly into the elephant grass and may have somersaulted on contact with the water, then exploded and disintegrated along the wreckage trail. Both loadmasters were killed as well as one crew member. Both other occupants were injured.
Probable cause:
The probable cause of this accident was a heat generating substance that was hidden in a cargo of fabrics inside pallet n°11 in the cargo compartment of the aircraft. The heat that emanated from the pallet resulted in smoke that caused a major distraction in the cockpit and later caused an explosion which seriously impaired the flight controls of the aircraft.

Crash of a Douglas DC-8-61 in Jeddah: 261 killed

Date & Time: Jul 11, 1991 at 0838 LT
Type of aircraft:
Operator:
Registration:
C-GMXQ
Survivors:
No
Schedule:
Jeddah - Sokoto
MSN:
45982
YOM:
1968
Flight number:
WT2120
Country:
Region:
Crew on board:
14
Crew fatalities:
Pax on board:
247
Pax fatalities:
Other fatalities:
Total fatalities:
261
Aircraft flight hours:
49318
Aircraft flight cycles:
30173
Circumstances:
A McDonnell Douglas DC-8-61 passenger plane, registered C-GMXQ was destroyed in an accident near Jeddah-King Abdulaziz International Airport (JED), Saudi Arabia. All 261 on board were killed. The DC-8 jetliner was owned by Canadian airline Nationair which operated the plane on behalf of Nigeria Airways to fly hajj pilgrims between Nigeria and Saudi Arabia. Nigeria Airways flight 2120 took off from Jeddah's runway 34L at 08:28, bound for Sokoto (SKO), Nigeria. About 15 seconds after brake release an oscillating sound was heard in the cockpit. Within two seconds, the flight engineer said: "What's that?" The first officer replied: "We gotta flat tire, you figure?" Two seconds later, an oscillating sound was again heard. The captain asked the first officer: "You're not leaning on the brakes, eh?" The first officer responded: "No, I 'm not, I got my feet on the bottom of the rudder." By this time, the aircraft had accelerated to about 80 knots. Marks on the runway showed that the No.1 wheel started to break up at about this time. In addition, the left and right flanges of No.2 wheel began to trace on the runway; rubber deposit from No.2 tire continued which appeared to be from a deflated tire between the flanges. At 28 seconds after brake release, a speed of 90 knots was called by the captain and acknowledged by the first officer. The captain called V1 about 45 seconds after brake release. Two seconds later, the first officer noted "sort of a shimmy like if you're riding on one of those ah thingamajigs." The captain called "rotate" 51 seconds after brake release and the airplane lifted off the runway. Witnesses noticed flames in the area of the left main landing gear. The flames disappeared when the undercarriage was retracted. During the next three minutes several indications of system anomalies occurred, which included a pressurization system failure, a gear unsafe light and a loss of hydraulics. The captain requested a level-off at 2000 feet because of the pressurization problem. In his radio call the captain used the callsign "Nationair 2120" instead of "Nigerian 2120" and the controller mistook the transmission to be from a Saudi flight returning to Jeddah and cleared The Jeddah bound aircraft to 3000 feet. The captain of the accident aircraft, however, acknowledged the ATC transmission without a call sign, saying "understand you want us up to 3000 feet." This misunderstanding continued for the next three minutes with ATC assuming that all calls were from the Saudi flight, not from the accident aircraft. About four minutes after brake release the captain called ATC and reported that the aircraft was leveling at 3000 feet. The first officer then interrupted with " ... declaring an emergency. We 're declaring an emergency at this time. We believe we have ah, blown tires." As the aircraft continued on the downwind heading, a flight attendant came into the cockpit and reported "smoke in the back ... real bad." A few moments later, the first officer said "I've got no ailerons." The captain responded: "OK, hang on, I've got it." It was the last record on the CVR, which failed (along with the flight data recorder [FDR]) at 08:33:33. The ATC controller gave a heading to intercept the final approach and thereafter continued to give heading information. Meanwhile, during the downwind and base legs, the fire had consumed the cabin floor above the wheel wells , permitting cabin furnishing to sag into the wheel wells. When the gear was probably extended at 11 miles on the final approach, the first body fell out because fire had burned through the seat harness. Subsequently, with the gear down and a forceful air supply through the open gear doors, rapid destruction of more floor structure permitted the loss of more bodies and seat assemblies. Despite the considerable destruction to the airframe, the aircraft appeared to be controllable. Eight minutes after brake release and 10 miles from the runway, the captain declared an emergency for the third time, saying, "Nigeria 2120 declaring an emergency, we are on fire, we are on fire, we are returning to base immediately." The aircraft came in nose down and crashed 9,433 feet (2,875 meters) short of the runway at 08:38.
Probable cause:
The following findings were reported:
1. The organisational structure for the deployment team was ill-defined and fragmented.
2. Deployment maintenance personnel were not qualified or authorised to perform the function of releasing the aircraft as being fit to fly.
3. The release of the aircraft as being fit to fly was delegated to non-practising Aircraft Maintenance Engineers whose primary function was to operate the aircraft as flight crew members.
4. The aircraft was signed-off as fit for flight, in an unairworthy condition, by the operating flight engineer who had no involvement in the aircraft servicing.
5. The #2 and #4 tyre pressures were below the minimum for flight dispatch. Other tyres may also have been below minimum pressures.
6. Maintenance personnel were aware of the low tyre pressures but failed to rectify the faults.
7. The mechanic altered the only record of the actual low pressures, measured by the avionics specialist on 7 July, four days before the accident.
8. There was no evidence that the tyre pressures had been checked, using a tyre pressure gauge, after 7 July.
9. The lead mechanic was aware of the low tyre pressures.
10. The persons who were aware of the low pressures had insufficient knowledge of the hazards of operating at low tyre pressures.
11. The project manager was aware of a low tyre pressure but was not qualified to assess its importance.
12. The project manager was responsible for the aircraft schedule and directed that the aircraft depart without servicing the tyre.
13. The lead mechanic who was aware of the requirement for, and had requested nitrogen for tyre servicing, did not countermand the decision of the project manager.
14. There was no evidence to indicate that this flight crew were ever informed of the low tyre pressures.
15. The aircraft departed the ramp in an unairworthy condition.
16. During the taxi from the ramp to the runway, the transfer of the load from the under-inflated #2 tyre to #1 tyre on the same axle, resulted in over deflection, over-heating and structural weakening of the #1 tyre.
17. The #1 tyre failed very early on the take-off roll due to degeneration of the structure, caused by over-deflection.
18. The #2 tyre failed almost immediately after #1 due to over-deflection and rapid overheating when the load was transferred from the #1 tyre.
19. The #2 wheel stopped rotating for reasons not established. Friction between the wheel/brake assembly and the runway generated sufficient heat to raise the temperature of tyre remnants above that required for a tyre fire to be self-sustaining. Rubber remnants ignited during the take-off roll.
20. Numbers 1 and 2 wheels were severely damaged and at least one piece of #1 wheel rim struck the airframe, becoming embedded in the left flap.
21. The crew were aware of unusual symptoms early and throughout the takeoff roll; the captain continued the take-off.
22. The aircraft was not equipped with warning systems which would have provided the flight crew with adequate information on which to make a decision to reject the take-off after tyre(s) failure.
23. The captain did not receive sufficient cues to convince him that a rejected take-off was warranted.
24. The crew retracted the gear, consistent with company procedures, and burning rubber was brought into close proximity with hydraulic and electrical system components.
25. The evidence indicates that the wheel well fire involved tyres, hydraulic fluid, magnesium alloy and fuel. The fuel was probably introduced as a result of "burn through" of the centre fuel tank.
26. Fire within the wheel wells spread and intensified until the cabin floor was breached and control systems were disabled.
27. The fuel increased the intensity of the fire until, shortly before impact, airframe structural integrity was lost.
28. Tyre characteristics and performance are not adequately addressed during training and licensing of both flight crews and technical personnel.
29. The aircraft operator's tyre inflation pressures did not accurately reflect what was contained in the aircraft manufacturer's maintenance manual.
30. The operator's maintenance and operating documentation for the DC-8 does not contain adequate information for the proper maintenance and operation of aircraft tyres.

Crash of a Douglas DC-10-30 in Tripoli: 81 killed

Date & Time: Jul 27, 1989 at 0725 LT
Type of aircraft:
Operator:
Registration:
HL7328
Survivors:
Yes
Site:
Schedule:
Seoul - Bangkok - Jeddah - Tripoli
MSN:
47887
YOM:
1973
Flight number:
KE803
Country:
Region:
Crew on board:
18
Crew fatalities:
Pax on board:
181
Pax fatalities:
Other fatalities:
Total fatalities:
111
Aircraft flight hours:
49025
Aircraft flight cycles:
11440
Circumstances:
The approach to Tripoli Intl Airport was completed in below weather minima as the visibility was varying between 100 and 800 feet and the ILS on runway 27 was unserviceable. On short final, the crew failed to realize his altitude was too low when the aircraft struck the roof of a house, stalled and crashed in a residential area located 2,4 km short of runway. Three crew members and 72 passengers were killed as well as six people on the ground. 124 people in the aircraft were injured as well as few dozen on the ground.
Probable cause:
The crew decided to continue the descent below the glide until the aircraft struck obstacles and crashed. The following contributing factors were reported:
- Lack of visibility due to foggy conditions,
- Below minima weather conditions,
- The crew failed to initiate a go-around while he did not establish a visual contact with the runway,
- The ILS system for runway 27 was unserviceable,
- The crew failed to follow the approach procedures,
- The crew ignored ATC warnings,
- The approach speed was excessive and the flaps were not deployed in the correct angle,
- The crew of a Russian aircraft diverted to Malta an hour before the accident due to unsafe landing conditions.

Crash of a Lockheed C-130H Hercules in Jeddah

Date & Time: Mar 27, 1989
Type of aircraft:
Operator:
Registration:
470
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
4756
YOM:
1977
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed on takeoff for unknown reasons. Crew fate unknown.

Crash of a Lockheed L-1011 TriStar 200 in Riyadh: 301 killed

Date & Time: Aug 19, 1980 at 2205 LT
Type of aircraft:
Operator:
Registration:
HZ-AHK
Survivors:
No
Schedule:
Karachi - Riyadh - Jeddah
MSN:
193U-1169
YOM:
1979
Flight number:
SV163
Country:
Region:
Crew on board:
14
Crew fatalities:
Pax on board:
287
Pax fatalities:
Other fatalities:
Total fatalities:
301
Captain / Total flying hours:
7674
Captain / Total hours on type:
388.00
Copilot / Total flying hours:
1615
Copilot / Total hours on type:
125
Aircraft flight hours:
3023
Aircraft flight cycles:
1759
Circumstances:
About 2108LT, the airplane departed Riyadh Airport en route to Jeddah, Saudi Arabia. Six minutes and 54 seconds after takeoff, while climbing to FL350, visual and aural warnings indicated smoke in the aft cargo compartment C-3. Climbing through FL220, a return to Riyadh was initiated. About two minutes later smoke was noted in the aft of the cabin, and passengers were panicking. At 18:25:26 the no. 2 engine throttle was stuck. The flight landed at about 2136LT and then taxied clear of the runway and came to a stop on an adjacent taxiway. While parked on the taxiway, the aircraft was destroyed by the fire and the three hundred and one persons on board the flight were killed.
Survival aspects:
The accident was survivable. The first door was opened about 23 min after all engines had been shutdown. The first rescue attempt was conducted at L-1 door. Most witness statements agree in content but differ slightly in the time factor element. A witness who participated in the first two efforts to open the doors stated that he was aboard fire truck n°4 was it was positioned near the left rear portion of the aircraft. He observed thick white smoke flowing from the bottom rear fuselage. At that time the aircraft engines were still running. A few seconds later, he observed smoke near the top of the fuselage, forward of the n°2 engine inlet. According to him, this smoke was followed almost immediately by flames in the same area. As the driver of n°4 started applying agent via the monitor, the witness dismounted and moved toward exit L-1. His route was outboard of n°1 engine which he thought was still running. On approaching L-1, he observed the fire chief and other people attempting to reach the L-1 emergency handle via a ladder which was placed on top of fire truck n°6. While fire personnel steadied the ladder, he climbed up and pulled the emergency handle. He was not certain if the door moved or not. An additional effort was attempted while he held onto and rode the monitor. While on the monitor, he pushed on the door to no avail. Most of :he group then moved to R-2 where another ladder had been positioned by other firemen. A firemen then climbed the ladder, operated the handle and the door opened in the emergency mode. The cabin was observed to be full of smoke and no life was observed nor were any human sounds heard. R-2 door was opened at 1905, 26 min after the aircraft came to a stop and 23 min after the shutdown of all engines. Shortly after (about 3 min) R-2 was opened, flames were seen progressing forward from the rear section of the cabin.
Probable cause:
The initiation of a fire in the C-3 cargo compartment. The source of the ignition of the fire is undetermined. Factors contributing to the fatal results of this accident were:
- The failure of the captain to prepare the cabin crew for immediate evacuation upon landing and his failure in not making a maximum stop landing on the runway, with immediate evacuation,
- The failure of the captain to properly utilize his flight crew throughout the emergency,
- The failure of C/F/R headquarters management personnel to ensure that its personnel had adequate equipment and training to function as required during an emergency.
Final Report: