Crash of a Lockheed 18-50-01 LodeStar in Jacksonville

Date & Time: Jan 8, 1947
Type of aircraft:
Operator:
Registration:
NC25687
Survivors:
Yes
MSN:
18-2039
YOM:
1940
Crew on board:
3
Crew fatalities:
Pax on board:
12
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On final approach, the crew encountered low visibility due to poor weather conditions. During the final segment, the captain realized he was aligned with the taxiway instead of the runway, so he increased power on both engines and attempted a go around. The aircraft overflew the airport and then stalled before crashing in a wooded area located near the runway end. All 15 occupants were rescued while the aircraft was destroyed.

Crash of a Douglas C-53-DO Skytrooper in Jacksonville: 1 killed

Date & Time: Dec 22, 1945 at 1656 LT
Operator:
Registration:
42-15562
Flight Type:
Survivors:
Yes
Schedule:
Augusta - Morrison
MSN:
7357
YOM:
1942
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The crew was performing a flight from Augusta-Bush Field, Georgia, to Morrison AFB in West Palm Beach. Enroute, he encountered engine trouble and the captain elected to divert to Jacksonville Airport. On final approach, the aircraft stalled and crashed short of runway. A crewman was killed while the second occupant was injured. The aircraft was destroyed.
Probable cause:
Engine trouble caused by fuel mismanagement on part of the crew.

Crash of a Lockheed 18 LodeStar in Banana River NAS

Date & Time: Oct 11, 1945 at 0234 LT
Type of aircraft:
Operator:
Registration:
NC15555
Survivors:
Yes
Schedule:
New York-La Guardia – Raleigh – Jacksonville – Miami
MSN:
2207
YOM:
1942
Flight number:
NA023
Crew on board:
2
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3059
Captain / Total hours on type:
2632.00
Copilot / Total flying hours:
1219
Copilot / Total hours on type:
363
Aircraft flight hours:
11396
Circumstances:
Flight 23 departed La Guardia Field at 1842 October 10, 1945, for Miami, Florida, with scheduled stops at Raleigh, N. C., and Jacksonville, Florida. Until landing at Jacksonville, the flight had been of a routine nature. However, during the flight the captain paid particular attention to an oil leak from the right engine which could be seen across the top of the engine cowl. Although the leak appeared to be very slight and had not necessitated excessive refill at either New York or Raleigh, Captain S. E. Stoia reported it to the National Airlines maintenance department at Jacksonville, with instructions that the leak be investigated. The aircraft was removed to a repair hangar and returned to the line after approximately one hour delay during which time two new oil hoses had been replaced. At 0123, October 11, 1945, the flight departed Jacksonville, on an instrument clearance to cruise at 2,000 feet to Miami. In order to avoid a slight turbulence at that flight altitude, Captain Stoia requested change of clearance to 4,000 feet. Approval for change of altitude was obtained after a delay due to traffic, and shortly after passing Daytona Beach, the flight climbed to 4,000 feet. At approximately 0210, First Officer W, S. Blomeley, who was seated in the co-pilot position, called Captain Stoia’s attention to spark which were coming from the right engine. Upon inspecting the engine with a flashlight, it was observed that thick smoke was pouring from under the engine cowl and that a wide band of oil was streaming back over the top of the nacelle. Realizing the danger of an oil fire and being anxious to avoid damage to the engine in the event of complete loss of oil, Captain Stoia immediately shut the engine down and feathered the right propeller. He advised the company station at Jacksonville of his difficulty and elected to continue to Melbourne, Florida, about 15 miles away for an emergency landing. Upon reaching Melbourne, however, the flight was advised by Melbourne Tower that the runway lights were inoperative and that considerable delay would be necessary before the mobile flood light apparatus would be available. Captain Stoia decided, therefore, to proceed to Banana River, 11 miles north, and Banana River Operations was advised by the Melbourne Tower Operator of his intentions and requested to prepare for his arrival. Although the captain had tuned to the Banana River Tower frequency, the tower was not equipped to receive the company frequency and two-way conversation was, therefore, not possible. As the flight approached the Banana River Naval Air Station, the captain observed that runway No. 6 was lighted, and being unable to establish radio contact with the tower, he assumed that it was the direction of landing intended. However, shortly before the aircraft arrived over the field, the tower personnel changed the runway lights to No. 15 since that runway was the longest one available at Banana River. The aircraft passed over the field at an altitude of 1500 feet, but the traffic pattern established by the flight was too close to the landing area, and, when on the final approach, Captain Stoia realized he was too high for a landing. When over the edge of the field at 300 feet with full flaps and gear extended and the airspeed at 100 mph, the captain decided to go around for another approach. Forty inches of manifold pressure was applied with full low pitch, the gear was fully retracted, and the flaps were retracted to the 30% position. During the missed approach procedure the captain intentionally held a nose-low attitude in order to accelerate to a normal climb airspeed; however, in spite of the loss of altitude, no increase in airspeed indication was obtained, and the aircraft continued to lose altitude while maintaining a straight course. Approximately 1/2 mile south southeast of the field, the aircraft struck the ground in a fairly level attitude longitudinally. The right wing made the first impact, the aircraft subsequently turning approximately 270 degrees as it skidded to a stop.
Probable cause:
On the basis of the foregoing the Board determines that the probable cause of this accident was an excessively hurried approach for an emergency single-engine landing and the faulty execution of a missed approach procedure. The came of engine malfunction was faulty installation of an cil hose and connecting clamp. A contributing factor to the accident was the failure of the company to maintain an adequate training program for pilot personnel and to provide the facilities required for such a program.
Final Report:

Crash of a Consolidated PBY-5 Catalina in Julington Creek: 1 killed

Date & Time: Oct 27, 1944
Type of aircraft:
Operator:
Registration:
08321
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Jacksonville - Jacksonville
MSN:
1235
YOM:
1941
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The crew was involved in a training flight in the region of the Jacksonville-Towers Field NAS when an unexpected situation forced the crew to attempt an emergency landing. The seaplane came to rest in a field near the Julington Creek. The aircraft was damaged beyond repair and a crew member was killed while both other occupants were injured.
Crew (TBC):
Cpt Moore,
Lt Rick,
Ens. John C. Thornton.

Crash of a Consolidated PBY-5 Catalina in Jacksonville NAS: 6 killed

Date & Time: Sep 15, 1944
Type of aircraft:
Operator:
Registration:
2406
Survivors:
Yes
Schedule:
Jacksonville - Jacksonville
MSN:
222
YOM:
1941
Crew on board:
8
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
Following a maritime patrol flight, the seaplane was returning to its base at Jacksonville-Towers Field NAS. On final approach by night, the aircraft was too low and hit an approach light and crashed into the St Johns River short of runway threshold. Six crew members were killed while two others were rescued.

Crash of a Martin A-30A-30-MA Baltimore off Dry Tortugas

Date & Time: Mar 2, 1944 at 1558 LT
Type of aircraft:
Operator:
Registration:
43-8890
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Wilmington - Raleigh - Jacksonville - Nassau
MSN:
7747
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1100
Captain / Total hours on type:
60.00
Circumstances:
The airplane departed Wilmington-New Castle County Airport on a delivery flight to Nassau. The crew made two fuel stops in Raleigh and Jacksonville. En route to Nassau, the crew encountered restricted visibility with scattered to broken cumulus with base at 2,000 feet and top at 6,000 feet. The crew deviated from the prescribed route and due to a fuel exhaustion, was forced to ditch the airplane off Dry Tortugas, west of Key West. The crew evacuated the airplane that sank within a minute. The crew was rescued about 15 minutes later by the ship SS Paulsboro. At the time of the accident, the aircraft was still registered 43-8890 and operated by the USAAF as it was supposed to be delivered to the Royal Air Force in Nassau and registered FW733.
Crew:
1st Lt Robert E. Allen, pilot,
Cpl Robert D. Arigoni.
Probable cause:
The aircraft was ditched by the crew due to a fuel exhaustion caused by a pilot error and poor judgment in navigation. At the time of the accident, the directional finding equipment was inoperative and the crew was flying under VMR mode.
Final Report:

Crash of a Consolidated PBY-5 Catalina in Jacksonville: 6 killed

Date & Time: Dec 18, 1943
Type of aircraft:
Operator:
Registration:
2330
Flight Phase:
Flight Type:
Survivors:
Yes
Crew on board:
12
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
Crashed into the St Johns River while performing a training mission out from the Jacksonville NAS. Six crew members were killed while six others were rescued.

Crash of a Pitcairn PA-6 Mailwing in Edgemoor

Date & Time: Nov 19, 1932 at 0315 LT
Type of aircraft:
Operator:
Registration:
NC546K
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Richmond – Jacksonville
MSN:
86
YOM:
1929
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot, sole on board, departed Richmond on a night mail flight to Jacksonville. En route, weather conditions deteriorated and the visibility was poor due to foggy conditions. The pilot got lost and because the aircraft ran out of fuel, the pilot decided to bail out and abandoned the airplane that crashed in a pasture. The pilot was found alive.

Crash of a Keystone LB-6A in Jacksonville

Date & Time: Jan 6, 1931
Type of aircraft:
Operator:
Registration:
32-168
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Jacksonville – Miami
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After takeoff from Jacksonville, while in initial climb, one of the engine failed. The aircraft lost height, impacted trees and crashed two miles east from the airfield, coming to rest broken in two. All four crew members were injured.
Probable cause:
Engine failure after takeoff.