Crash of a Cessna 414 Chancellor on Mt Beech Knob: 2 killed

Date & Time: Nov 26, 1996 at 1208 LT
Type of aircraft:
Registration:
N73CP
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Summersville – Waynesboro
MSN:
414-0505
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
8000
Captain / Total hours on type:
2720.00
Aircraft flight hours:
9358
Circumstances:
Shortly after takeoff, the pilot contacted Charleston Approach Control to pick up his IFR clearance to the destination. The controller instructed the pilot to maintain VFR and he then attempted to coordinate with Washington Center for the clearance. The controller subsequently was unable to establish radar contact with the flight and he also lost radio contact with the pilot. The aircraft collided with the upslope of high terrain in weather conditions comprised of fog, sleet, and snow. The accident site was about 14 miles from the departure point. Toxicological testing of the pilot revealed benzoylecgonine.
Probable cause:
The pilot's inadequate inflight decision which resulted in VFR flight into instrument meteorological conditions and his failure to maintain adequate terrain clearance which resulted in an inflight collision with terrain. The low ceiling was a factor.
Final Report:

Crash of a Piper PA-61P Aerostar (Ted Smith Aerostar 601) in Mount Storm

Date & Time: Jan 27, 1996 at 0120 LT
Operator:
Registration:
N162GA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Grand Rapids – Norfolk
MSN:
61-0050-095
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4048
Captain / Total hours on type:
70.00
Aircraft flight hours:
5791
Circumstances:
The pilot stated that the airplane was in cruise flight at 8,000 feet MSL, when the right engine lost power. He advised ATC of the loss of power and received radar vectors toward an airport. The pilot said he maintained the best single-engine rate-of-climb speed, but the airplane's altitude 'drifted down.' When the airplane entered clouds, it began to accumulate structural icing and would not maintain sufficient altitude. The airplane impacted mountainous terrain about 16 miles northwest of the airport. The pilot stated that he had departed on the cargo flight with 5 hours of fuel on board for what he estimated to be a 2 1/2 hour flight. Also, he reported that conditions were dark and foggy, when the accident occurred. Postaccident examination of the engines and their systems revealed no evidence of preimpact mechanical malfunction. Examination of the airplane wreckage revealed no evidence of preimpact failure of the airframe or its systems. During a postaccident engine test run, the right engine started normally and operated satisfactorily.
Probable cause:
Loss of power in the right engine for undetermined reason(s), and the accumulation of structural ice on the airplane, which resulted in an increased rate of descent and a subsequent forced landing before the pilot could reach an alternate airport. Factors relating to the accident were: the adverse weather (icing) conditions, darkness, fog, and the lack of suitable terrain in the emergency landing area.
Final Report:

Crash of a Cessna 414 Chancellor in Marlinton: 1 killed

Date & Time: Nov 28, 1995 at 0940 LT
Type of aircraft:
Operator:
Registration:
N28901
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Sutton - Lynchburg
MSN:
414-0353
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4850
Aircraft flight hours:
3378
Circumstances:
The pilot took off from an uncontrolled airport. He attempted to obtain an IFR clearance and reported that he was VFR at 3,500 feet. While air traffic control personnel were locating the flight plan and coordinating the IFR clearance, they lost radio contact with the pilot. The pilot continued to fly towards his destination, transiting rising mountainous terrain which was partially obscured by clouds. Wreckage was located about 28 nautical miles from the departure airport, at the 4,050-foot level. There was no evidence of mechanical failure or malfunction. According to FAR Part 91.3, the pilot had the ultimate authority for the operation of the airplane, and in the case of an in-flight emergency, had the authority to deviate from flight rules "to the extent required to meet that emergency." According to the AIM, an emergency could be either "a distress or an urgency condition." An urgency condition would exist "the moment the pilot becomes doubtful about position... weather, or any other condition that could adversely affect flight safety." Under FAR Part 91.3, the pilot would have been authorized to climb the airplane under IFR conditions, even if he were to enter controlled airspace.
Probable cause:
The pilot's continued VFR flight into obscured, rising mountainous terrain, and his failure to climb the airplane as conditions worsened. Factors included the rising terrain and the weather obscuration.
Final Report:

Crash of a Mitsubishi MU-2B-40 Marquise in South Charleston

Date & Time: Aug 29, 1993 at 1550 LT
Type of aircraft:
Operator:
Registration:
N965MA
Survivors:
Yes
Schedule:
Rochester - Roanoke
MSN:
404
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6370
Captain / Total hours on type:
2500.00
Aircraft flight hours:
2739
Circumstances:
The pilot reported the right engine failed, followed by the left engine approximately one minute later while he was in cruise at 25,000 feet. He said he initiated a steep descent to get below 18,000 feet, and attempts at restarting the left engine were unsuccessful. The pilot landed 500 feet down a 1,900 feet long runway and ran off the departure end, 300 feet, into a wooded area. Post accident investigation found 130 gallons of fuel onboard in the main tanks. The fuel was tested and found to be free of water. The fuel lines were free of obstructions and the fuel pumps worked. A failed torque sensor was found on the left engine which would disconnect the left engine driven fuel pump. The right engine was test run satisfactorily.
Probable cause:
Improper emergency procedures by the pilot which resulted in the shutdown of an operative engine, following a power loss due to a failed torque sensor in the other engine, which resulted in a total power loss approach, landing, and overrun.

Crash of a Lockheed C-130E Hercules near Berkeley Springs: 6 killed

Date & Time: Oct 7, 1992 at 0930 LT
Type of aircraft:
Operator:
Registration:
63-7881
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Martinsburg - Martinsburg
MSN:
3952
YOM:
1964
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The crew departed Martinsburg-Eastern West Virginia-Shepherd Field for a local training flight. While flying at low height, the four engine aircraft struck power cables and crashed onto a house located 3 km northwest of Berkeley Springs. All six crew members were killed while the unique person in the house was slightly injured.

Crash of a BAe 3101 Jetstream 31 in Beckley

Date & Time: Jan 30, 1991 at 2355 LT
Type of aircraft:
Operator:
Registration:
N167PC
Survivors:
Yes
Schedule:
Charlotte - Beckley
MSN:
710
YOM:
1986
Crew on board:
2
Crew fatalities:
Pax on board:
17
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5000
Captain / Total hours on type:
3400.00
Aircraft flight hours:
8841
Circumstances:
Aircraft was dispatched with inoperative airframe deice system, tho an operational deice system was required for flight in known icing conditions. During descent to land, aircraft encountered light icing conditions. Capt believed aircraft could 'handle it' and continued descent. As he began ILS final approach, he noted significant increase of ice accumulation and used higher than normal approach speed. As full (50°) flaps were set, aircraft began buffet and pitched nose down. Capt corrected with full back pressure on control column, but aircraft landed hard, gear collapsed and aircraft slid about 3,600 feet to a stop. No preimpact mechanical anomaly was found, except for inoperative deice system. Investigation revealed pilots had received printout of weather from company computer system with surface observation and terminal forecast, but no area forecast (FA). Pilots and ground personnel were not aware that FA was available at company weather terminal. FA forecasted light and occasional moderate rime and mixed icing in clouds and precipitation above freezing level. Weather deteriorated, but pilots did not require inflight weather info or pireps. Flight mnl noted tailplane ice may cause nose down trim change with flap extension. There was evidence of tail plane stall, lack of company training in cold weather operations, deficiencies in use of deicing systems, and lack of FAA surveillance.
Probable cause:
Flight into known adverse weather conditions by the pilot, which resulted in ice accumulation on the aircraft and subsequent loss of aircraft control (tail plane stall) as the flaps were fully extended. Factors related to the accident were: the pilot's inadequate use of the preflight briefing service, inadequate training provided to the pilots by company/management personnel, inadequate surveillance by the faa, and icing conditions.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601P) in Greater Cumberland: 1 killed

Date & Time: Sep 19, 1990 at 1655 LT
Registration:
N8249J
Survivors:
No
Schedule:
Williamsburg – Greater Cumberland
MSN:
61-0653-7963302
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1350
Circumstances:
The pilot was cleared for an approach to the airport. He received airport advisories from the airport unicom operator and asked that the runway lights be turned up. Soon afterwards, the airplane was seen approaching runway 23, which was served by a localizer approach. A witness at the airport said he saw the plane flying in and out of low hanging clouds. He said the airplane appeared to be at level flight, about 400 to 500 feet agl, then it passed over the airport and went in a steep left turn. After about 90° of turn, the airplane began a shallow descent. It rolled out of the turn before it descended into the ground about 1/4 mile from the approach end of runway 28. The witness said he heard engine sounds throughout the descent. An examination of the airplane did not disclose evidence of mechanical malfunction. A post-mortem examination did not reveal evidence of impairment or incapacitation of the pilot. The pilot, sole on board, was killed.
Probable cause:
The pilot's improper ifr procedure by not maintaining sufficient altitude, while circling to land. Factors related to the accident were: the low ceiling and visibility conditions in fog.
Final Report:

Crash of a Douglas DC-3A in Capon Bridge: 2 killed

Date & Time: May 19, 1990 at 1130 LT
Type of aircraft:
Operator:
Registration:
N1FN
Flight Phase:
Survivors:
No
Schedule:
Martinsburg - Winchester
MSN:
11685
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
22000
Captain / Total hours on type:
3000.00
Aircraft flight hours:
34906
Circumstances:
While spraying gypsy moths with dimilin over wooded/hilly terrain, the DC-3 collided with power lines in a valley area. Witnesses in an nearby observation aircraft reported the DC-3 entered a gradual climb, which continued until the DC-3 was in a steep nose high attitude. The pilot of the observation aircraft tried to communicate with the DC-3 pilots, but could not make radio contact. The observation pilot reported the DC-3 entered a stall/spin at about 1,200 feet agl, then crashed. An investigation revealed no evidence of a preimpact failure. The DC-3 was not equipped with a wire cutter kit. Both pilots were killed.
Probable cause:
Inadequate visual lookout by the pilots of the DC-3, which resulted in their failure to see-and-avoid the powerlines. Factors related to the accident were: the obstruction (transmission wires), and the lack of visual cues for the pilots.
Final Report:

Crash of a Dassault Falcon 20D in Wheeling

Date & Time: Feb 1, 1988 at 1703 LT
Type of aircraft:
Operator:
Registration:
N287W
Survivors:
Yes
Schedule:
Akron - Wheeling
MSN:
194
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8175
Captain / Total hours on type:
2816.00
Aircraft flight hours:
7163
Circumstances:
The aircraft landed after an ILS approach to runway 03. According to the pilot shortly after touchdown he saw deer ahead on the runway. Before he could take evasive action the aircraft struck two deer. Afterwards brake pressure was lost. The pilot steered the aircraft onto grass off the right side of the runway to avoid going past the runway end and down a hill. Examination of the aircraft revealed that the deer were struck with the left main gear, fracturing a hydraulic brake line. All nine occupants escaped uninjured.
Probable cause:
Occurrence #1: on ground/water collision with object
Phase of operation: landing - roll
Findings
1. (f) weather condition - fog
2. (c) object - animal(s)
3. (c) clearance - not possible
----------
Occurrence #2: nose gear collapsed
Phase of operation: landing - roll
Findings
4. (c) landing gear, normal brake system - disabled
5. Brakes (normal) - unavailable
6. Landing gear, nose gear assembly - overload
Final Report:

Crash of a Beechcraft D18S in Huntington: 1 killed

Date & Time: Sep 25, 1985 at 0537 LT
Type of aircraft:
Registration:
N25Q
Flight Type:
Survivors:
No
Schedule:
Indianapolis - Huntington
MSN:
A-823
YOM:
1952
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3900
Captain / Total hours on type:
20.00
Circumstances:
The aircraft contacted the terrain with the left wing tip, cartwheeled and came to rest inverted during an ILS runway 12 approach at Huntington (HTS). Minimum approach visibility for the ILS is 3/4 of a mile. While en route the pilot was informed the HTS visibility was 1/8 of a mile. A missed approach was performed on the first ILS. During the missed approach climb the transponder code in the aircraft was changed to 7600. Radar data indicated that after the 2nd ILS approach, the aircraft made a climbing left turn. When approximately 2 miles southeast of the airport, at 2,100 feet, the aircraft made a sharp right turn. The radar target disappeared shortly thereafter. The aircraft contacted the terrain on a heading of 260° between runway 30 and the parallel taxiway. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: circling (ifr)
Findings
1. Weather condition - below approach/landing minimums
2. (c) ifr procedure - improper - pilot in command
3. (c) procedures/directives - not followed - pilot in command
4. (c) missed approach - not performed - pilot in command
5. Air/ground communications - improper use of - pilot in command
Final Report: