Crash of a Casa C-295M in Mirosławiec: 20 killed

Date & Time: Jan 23, 2008 at 1907 LT
Type of aircraft:
Operator:
Registration:
019
Flight Type:
Survivors:
No
Schedule:
Warsaw– Powidz – Poznań-Krzesiny – Mirosławiec – Świdwin – Krakow
MSN:
S-043
YOM:
2007
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
20
Aircraft flight hours:
300
Circumstances:
The aircraft departed Warsaw at 1651LT on a flight to Krakow with intermediate stops in Powidz, Poznań-Krzesiny, Mirosławiec and Świdwin, carrying 36 passengers and a crew of four. They were returning to their base after intending the 50th Annual Aviation Safety Conference held in Warsaw. Nine passengers deplaned at Powidz and 11 others at Poznań-Krzesiny AFB. On approach to Mirosławiec by night, the crew encountered poor weather conditions with a ceiling at 300 feet, visibility 2 sm and mist. On short final, the aircraft was unstable. With a rate of descent of 6,000 feet per minute and at a speed of 148 knots, the aircraft impacted trees and crashed in a wooded area located 1,300 metres short of runway threshold, bursting into flames. The aircraft was totally destroyed and all 20 occupants were killed.
Crew:
Maj Jarosław Haładus,
Adj Robert Kuźma,
Adj Michał Smyczyński,
Sgt Janusz Adamczyk.
Passengers:
Gen Brig Andrzej Andrzejewski,
Col Dariusz Maciąg,
Col Jerzy Piłat,
Lt Col Wojciech Maniewski,
Lt Col Zbigniew Książek,
Lt Col Dariusz Pawlak,
Lt Col Zdzisław Cieślik,
Maj Robert Maj,
Maj Mirosław Wilczyński,
Maj Grzegorz Jułga,
Maj Piotr Firlingier,
Maj Krzysztof Smołucha,
Cpt Karol Szmigiel,
Cpt Paweł Zdunek,
Cpt Leszek Ziemski,
Cpt Grzegorz Stepaniuk,

Probable cause:
Inadvertent loss of spatial and situational awareness by the aircraft crew during final stages of PAR approach, which, within 12 seconds period before crash, resulted in the aircraft’s bank increasing unmonitored and accompanying altitude loss, while the flight crew apparently was trying to establish visual contact with runway and approach lights.

Among the secondary causes the Board listed:
- Improper flight crew selection for the flight:
- The PIC did not have any previous experience on this version of CASA C-295 aircraft, which was additionally equipped with 2 IRS/GPS LN-100G units instead of 2 TOPSTAR 100-2 GPS receivers, and, ironically, with EGPWS Mk. V - unfortunately lack of cryptographic modules in GPS receivers, which made IRS/GPS LN-100G system almost useless (IRS alone with no GPS enhancement) caused flight crew to use handheld GPS receivers (Garmin GPSMAP 196),
- The SIC was not rated in CASA C-295 aircraft for night/IMC operations,
- Poor flight crew coordination and cooperation (poor MCC & CRM):
- improper altimeter setting procedures,
- probably both pilots were looking for visual cues and nobody was observing flight instruments in the very last seconds before they crash),
- Poor weather conditions in vicinity of Miroslawiec AB; ceiling 300 feet, visibility 2 sm, in mist. Icing was excluded as a factor.
- Spatial disorientation of the flight crew,
- EGPWS Audio warning was inhibited (the flight crew missed EGPWS test before departure from Warsaw, even though it was a checklist item, and never corrected the problem - the PIC was not familiar with the system - he has never flown before CASA C-295M equipped with EGPWS) - in result no audio warning of excessive bank angle, high terrain closure rate and high sink rate was available to the flight crew, as well as no automatic height above ground callouts were given,
- The flight crew failed to monitor radio-altimeter indication during both approaches,
- Both pilots concentrated their attention outside of the cockpit during final seconds before crash and did not scan flight instruments.
- The military PAR controller did a poor job during the approach, he let for the non-stabilized approach, he was not compensating properly for left crosswind of 20 kts and allowed the aircraft to stay high above glide slope during both PAR approaches, he also was not fully aware of altimeter setting (QNH or QFE) and altitude reports by flight crew– improper values QNH/QFE were used by the flight crew during first approach, additionally PIC has set his altimeter to QFE, while SIC to QNH. During the approach the controller’s instructions were hesitant and inconsistent, probably making the flight crew to believe their approach was going well.
- The military PAR controller was giving improper suggestions to the flight crew - he was questioning them during final stage of approach whether they see approach or runway lights or not, instead of continuous talking them down to the runway threshold,
- Altimeter indications were improperly interpreted by the flight crew,
- Improperly performed search for visual contact by the flight crew during final stage of approach,
- Improper, lacking weather situation analysis performed by the PIC before the flight,
- The flight crew did not properly set DH/MDA (they did the same error on previous two legs before crash).

Contributing factors were:
- The SIC was not rated in CASA C-295 aircraft for night/IMC operations (the SIC total flight time was 800 hours including 100 hours in CASA C-295M),
- The PIC has no previous experience on the accident version of CASA C-295 aircraft, (although he logged 800+ hours in another version of CASA C-295M aircraft used by Polish AF and his total flight time was 2500 hours),
- Because of lack of GPS enhancement to IRS, the flight crew used Garmin GPSMAP 196 handheld GPS receiver,
- The PIC had no previous experience in PAR approaches in IMC, close to minimums, which in Miroslawiec AB were reported to be aprox. ceiling 270 feet and visibility of 3300 feet,
- The military PAR controller had no previous experience in conducting PAR approaches of aircraft other than Sukhoi Su-22,
- The aircraft was improperly vectored to final approach by military APP controller (the same person performing PAR controller duties) which resulted in rushed, non-stabilized first approach, because the aircraft started descent on final approach segment being twice as high as glide slope,
- Lack of instrument approach procedures meeting ICAO standards at Polish military airports, including Miroslawiec AB, published in Aeronautical Information Publication (AIP),
- Use of different units by pilots and controller (the aircraft’s altimeters were scaled in feet and hPa, while the controller was using meters and millimeters of Hg, there was also misunderstanding regarding use of QNH and QFE),
- Even though the aircraft was equipped with ILS receiver, the ILS equipment at Miroslawiec AB was inoperative (it was installed in 2001, but since then has never worked properly, and therefore was not used, despite several repair attempts - now, 2 months after the crash, it is reported to work properly - the crew had available only military PAR (unable to meet ICAO standards), assisted with 2 military NDBs located 4 km and 1 km from the threshold of runway 30),
- The information on minimum weather conditions and available navaids in Miroslawiec AB were improperly disseminated (dispatch personnel had no information the ILS in Miroslawiec AB was inoperative).

Crash of a Beechcraft 300LW Super King Air on Piz Sarsura: 2 killed

Date & Time: Feb 14, 2002 at 1720 LT
Operator:
Registration:
D-ICBC
Flight Phase:
Survivors:
No
Site:
Schedule:
Poznań – Samedan
MSN:
FA-227
YOM:
1993
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4158
Captain / Total hours on type:
1835.00
Aircraft flight hours:
4141
Circumstances:
D-ICBC was refuelled in Poznan to its maximum capacity of 2040 litres. An ATC flight plan was filed for an IFR flight. After the RENTA waypoint, VFR had actually been entered, but the crew had not filed the flight plan as a Y flight plan, as is prescribed for flights which begin under IFR rules and then end as a VFR flight. However, the flight plan was entered and transmitted as a Y flight plan by the competent unit in Brussels. Take-off time was scheduled for 14:20 UTC. Take-off actually took place at 14:35 UTC. No details are known about the history of the first part of the flight. The aircraft reached the border with Italian airspace in the planned air corridor M736 at flight level 250. The crew reported at 15:54:14 UTC to Padua ACC, sector LOW NORD on frequency 125.900 MHz: “..ua Buongiorno D-ICBC, Flight level 250, appro…approaching LIZUM Point” The air traffic controller instructed the crew to fly “LIZUM, LUSIL direct”. The crew confirmed “LIZUM .... direct DBC”. On enquiring, they received the information that they would be able to descend in about 10 miles. On the radar plot it can be seen that the aircraft did not fly as required direction LUSIL, but turned onto a heading of approximately 240° and was flying in the direction of Samedan. At 15:59:18 UTC, the clearance to flight level 170 was given; which is the lowest IFR flight level (minimum enroute altitude – MEA) in this area. At 16:02:03 UTC, the crew of D-ICBC was asked whether they were flying direct to Samedan. This was confirmed by them. They were then requested to report as soon as they wished to change from instrument flight rules to visual flight rules. At 16:05:16 UTC, the crew change from instrument flight rules to visual flight rules and were requested to contact Samedan Tower on frequency 135.325 MHz, which they did after a brief delay. The Samedan air traffic controller informed the crew that runway 21 was in use and that the QNH was 1012 hPa. He additionally requested them to report as soon as they flew into the valley. After leaving flight level 170, the aircraft turned slightly to the right onto a course of approximately 265° and maintained its continuous descent. At 16:11:25 UTC, the aircraft passed flight level 130 and began to turn slowly to the left. This turn brought the aircraft precisely onto the extended centre line of runway 21 in Samedan. The aircraft was last captured by the radar at 16:15:24. The last flight level indicated on the secondary radar was FL 101. A little later, the aircraft collided with the elevated terrain of the Sarsura glacier at an elevation of 9640 ft AMSL. Both pilots were killed immediately. The aircraft was destroyed.
Probable cause:
The accident is caused by the fact that the crew on its approach according to visual flight rules to Samedan aerodrome, under critical weather conditions and applying inappropriate flying tactics lost the situational awareness and theby the aircraft D-ICBC collided with the terrain.
The following findings were identified:
- The pilot was in possession of a senior commercial pilots licence, issued by the Polish authorities.
- There are no indications of any health problems affecting the pilot during the flight involved in the accident.
- The aircraft was admitted for traffic.
- The investigation produced no indications of any pre-existing technical faults which might have caused the accident.
- The mass and centre of gravity at the time of the accident were within the prescribed limits.
- As weather information, only METAR and TAF for Innsbruck, Zurich, Milan Malpensa and Milan Linate were found.
- No documentation for visual approaches to Samedan were found in the aircraft.
- In the documentation which was available to the investigators, it was not evident that any of the crew members had previously flown to Samedan.
Final Report:

Crash of a Beechcraft C90B King Air in Poznań

Date & Time: Nov 12, 1999 at 0930 LT
Type of aircraft:
Operator:
Registration:
D-IDIX
Survivors:
Yes
Schedule:
Melle-Grönegau – Poznań
MSN:
LJ-1495
YOM:
1997
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew departed Melle-Grönegau Airport at 0736LT on a charter flight to Poznań, carrying four passengers and two pilots. While descending to Poznań at an altitude of 7,000 feet, the crew was informed about weather conditions at destination with a visibility of 700 metres, an RVR of 650 metres and a ceiling at 200 feet. After being cleared to descent to runway 29, the crew was informed about local patches of fog at the airport and the RVR dropped to 350 metres. On short final, at a height of about 500 feet, as the crew was unable to establish any visual contact with the approach lights and the runway lights, the captain decided to initiate a go-around procedure. Shortly later, the aircraft struck the ground to the left of the runway. Upon impact, the undercarriage were torn off. The aircraft slid for about 150 metres and came to rest with both engines and the left wing torn of as well. All six occupants escaped uninjured.
Final Report: