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Crash of a Dassault Falcon 900EX in San Diego

Date & Time: Feb 13, 2021 at 1150 LT
Type of aircraft:
Operator:
Registration:
N823RC
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
San Diego - Kona
MSN:
201
YOM:
2008
Crew on board:
3
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8800
Captain / Total hours on type:
1.00
Copilot / Total flying hours:
567
Copilot / Total hours on type:
17
Aircraft flight hours:
2914
Circumstances:
The flight crew was conducting a flight with two passengers and one flight attendant onboard the multiengine jet airplane. The flight crew later stated that at rotation speed, the captain applied back pressure to the control yoke; however, the nose did not rotate to a takeoff attitude. The captain attempted to rotate the airplane once more by relaxing the yoke then pulling it back again, and, with no change in the airplane’s attitude, he made the decision to reject the takeoff by retarding the thrust levers and applying maximum braking. The airplane overran the end of the runway onto a gravel pad where the landing gear collapsed. Continuity was confirmed from the flight controls to the control surfaces. No mechanical anomalies with the engines or airplane systems were noted during the investigation that would have precluded normal operation. A review of performance data indicated that the flight crew attempted to takeoff with the airplane 2,975 lbs over the maximum takeoff weight (MTOW), a center of gravity (CG) close to the most forward limit, and an incorrect stabilizer trim setting. The digital flight data recorder (DFDR) data indicated that the captain attempted takeoff at a rotation speed 23 knots (kts) slower than the calculated rotation speed for the airplane at maximum weight. Takeoff performance showed the departure runway was 575 ft shorter than the distance required for takeoff at the airplane’s weight. The captain, who was the pilot flying, did not hold any valid pilot certificates at the time of the accident because they had been revoked 2 years prior due to his falsification of logbook entries and records. Additionally, he had never held a type rating for the accident airplane and had started, but not completed, training in the accident airplane model before the accident. The first officer had accumulated about 16 hours of flight experience in the make and model of the airplane and was not authorized to operate as pilot-in-command. The airplane’s flight management system (FMS) data were not recovered; therefore, it could not be determined what data the flight crew entered into the FMS that allowed the airspeed numbers to be generated. The investigation revealed that had the actual performance numbers been entered, a “FIELD LIMITED” amber message would have illuminated warning the crew that the MTOW was exceeded, and airspeed numbers would not have been generated. Therefore, it is likely that the crew entered incorrect data into the FMS either by manually entering a longer runway length and/or decreased the weight of the fuel, passengers, and/or cargo.
Probable cause:
The flight crew’s operation of the airplane outside of the manufacturer’s specified weight and balance limitations and with an improper trim setting, which resulted in the airplane’s inability to rotate during the attempted takeoff. Contributing to the accident, was the captain’s lack of proper certification and the crew’s lack of flight experience in the airplane make and model.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain off Hilo: 1 killed

Date & Time: Aug 25, 2000 at 1735 LT
Operator:
Registration:
N923BA
Survivors:
Yes
Schedule:
Kona – Kona
MSN:
31-8252024
YOM:
1982
Flight number:
BIA057
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2067
Captain / Total hours on type:
465.00
Aircraft flight hours:
3492
Circumstances:
The pilot ditched the twin engine airplane in the Pacific ocean after experiencing a loss of engine power and an in-flight engine fire while in cruise flight. The flight was operating at 1,000 feet msl, when the pilot noticed a loss of engine power in the right engine. At the same time the pilot was noticing the power loss, passengers noted a fire coming from the right engine cowling. The pilot secured the right engine and feathered the propeller. He attempted to land the airplane at a nearby airport; however, when he realized that the airplane was unable to maintain altitude he elected to ditch the airplane in the ocean. Prior to executing the forced landing, the pilot instructed the passengers to don their life jackets and assume the crash position. After touchdown, all but one passenger exited the airplane through the main cabin and pilot doors. It was reported that the remaining passenger was frightened, and could not swim. One survivor saw the remaining passenger sitting in the seat with the seat belt still secured and the life vest inflated. The pilot and passengers were then rescued from the ocean via rescue helicopter and boat. Postaccident examination of the airplane revealed that the right engine's oil converter plate gasket had deteriorated and extruded from behind the converter plate, allowing oil to spray in the accessory section and resulting in the subsequent engine fire. The engine manufacturer had previously issued a mandatory service bulletin (MSB) requiring inspection of the gasket every 50 hours for evidence of gasket extrusion around the cover plate or oil leakage. Maintenance records revealed that the inspection had been conducted 18.3 hours prior to the accident. At the time of the accident, the right engine had accumulated 386.8 hours since its last overhaul, and gasket replacement. The MSB was issued one month prior to the accident, after the manufacturer received reports of certain oil filter converter plate gaskets extruding around the oil filter converter plate. The protruding or swelling of the gasket allowed oil to leak and spray from between the plate and the accessory housing. A series of tests were conducted on exemplar gaskets by submerging them in engine oil heated to 245 degrees F; after about 290 hours, the gasket material displayed signs of deterioration similar to that of the accident gasket. A subsequent investigation revealed that the engine manufacturer had recently changed gasket suppliers, which resulted in a shipment of gaskets getting into the supply chain that did not meet specifications. As a result of this accident, the engine manufacturer revised the MSB to require the replacement of the gasket every 50 hours. The FAA followed suit and issued an airworthiness directive to mandate the replacement of the gasket every 50 hours.
Probable cause:
Deterioration and failure of the oil filter converter plate gasket, which resulted in a loss of engine power and a subsequent in-flight fire.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain on Mt Mauna Loa: 10 killed

Date & Time: Sep 25, 1999 at 1726 LT
Operator:
Registration:
N411WL
Flight Phase:
Survivors:
No
Site:
Schedule:
Kona - Kona
MSN:
31-8352039
YOM:
1983
Flight number:
BIA058
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
11500
Aircraft flight hours:
4523
Circumstances:
On September 25, 1999, about 1726 Hawaiian standard time, Big Island Air flight 58, a Piper PA-31-350 (Chieftain), N411WL, crashed on the northeast slope of the Mauna Loa volcano near Volcano, Hawaii. The pilot and all nine passengers on board were killed, and the airplane was destroyed by impact forces and a postimpact fire. The sightseeing tour flight was operating under 14 Code of Federal Regulations Part 135 as an on-demand air taxi operation. A visual flight rules flight plan was filed, and visual meteorological conditions existed at the Keahole-Kona International Airport, Kona, Hawaii, from which the airplane departed about 1622. The investigation determined that instrument meteorological conditions prevailed in the vicinity of the accident site.
Probable cause:
The pilot's decision to continue visual flight into instrument meteorological conditions (IMC) in an area of cloud-covered mountainous terrain. Contributing to the accident were the pilot's failure to properly navigate and his disregard for standard operating procedures, including flying into IMC while on a visual flight rules flight plan and failure to obtain a current preflight weather briefing.
Final Report:

Crash of a Rockwell Grand Commander 680FLP in Kona: 1 killed

Date & Time: Sep 10, 1989 at 1518 LT
Registration:
N22LR
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Kona - Honolulu
MSN:
680-1503-18
YOM:
1965
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
203
Captain / Total hours on type:
23.00
Aircraft flight hours:
4790
Circumstances:
As the aircraft was departing from runway 17, smoke was observed coming from the right engine. The pilot confirmed a loss of power and made a right turn back toward the runway, then reported he had 'lost both engines.' The aircraft was extensively damaged during a landing on rough, rocky terrain about 1/4 mile southwest of the runway threshold. Investigation revealed the aircraft had just changed ownership. During pre-purchase inspection in Florida, metal particles were found in the oil screens of both engines. Oil was changed and flushed, but metal particles were found after another engine run. In May 1989, the right engine was replaced with an engine from another aircraft. The aircraft was flown to Oakland, CA, where it was painted and new interior was installed. A local mechanic noted metal particles in both eng oil screens and recommended oil analysis, but ferrying pilot refused. After flight to Hawaii, no oil stain noted on fuselage before flight on 9/9/89. Exam of wreckage revealed both engines failed from detonation. Heavy oil streaks found behind right engine, some streaks of oil found behind left engine. Right engine crankshaft/rod bearing surface was 0.010' under standard, but rod bearings were standard size. While the passenger was seriously injured, the pilot was killed.
Probable cause:
Inadequate maintenance, and operation by the pilot with known deficiencies in the aircraft. Factors related to the accident were: excessive wear in both engines, improper use of powerplant controls by the pilot, subsequent overtemperature/detonation in both engines, improper emergency procedures by the pilot (including premature gear extension and/or failure to properly reduce drag on the aircraft after loss of engine power), and the pilot's lack of experience in multi engine and this make and model of aircraft.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Honolulu

Date & Time: Nov 20, 1987 at 1124 LT
Operator:
Registration:
N27512
Survivors:
Yes
Schedule:
Kona - Honolulu
MSN:
31-7852035
YOM:
1978
Flight number:
PV084
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4190
Captain / Total hours on type:
1685.00
Aircraft flight hours:
6315
Circumstances:
The pilot estimated that the aircraft's reduced fuel quantity was adequate for the flight during his preflight inspection. As the aircraft descended for the traffic pattern near the destination airport both engines failed. After the loss of power the pilot executed a forced landing into a park with the landing gear not fully extended. The aircraft impacted the terrain and slid into a fence before coming to a stop.
Probable cause:
Occurrence #1: loss of engine power (total) - nonmechanical
Phase of operation: descent - normal
Findings
1. (c) fluid, fuel - exhaustion
2. (c) fuel consumption calculations - inaccurate - pilot in command
3. (f) preflight planning/preparation - inadequate - pilot in command
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
----------
Occurrence #3: on ground/water collision with object
Phase of operation: landing
Findings
4. (f) object - fence
5. Gear extension - not attained - pilot in command
Final Report:

Crash of a Beechcraft H18 off Kona

Date & Time: Sep 8, 1983 at 0934 LT
Type of aircraft:
Operator:
Registration:
N2990F
Flight Phase:
Survivors:
Yes
Schedule:
Kona - Honolulu
MSN:
BA-753
YOM:
1968
Flight number:
PV060
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8026
Captain / Total hours on type:
2960.00
Aircraft flight hours:
16873
Circumstances:
About one minute after takeoff, between 400-500 feet msl and during the first power reduction, the right engine backfired. Following some more violent backfires the rpm went to zero. The right engine was restarted but the same result occurred. The pilot attempted to feather the right prop but to no avail. The aircraft was then deliberately ditched to avoid an outcropping of lava. The aircraft came to rest in about 25-30 feet of water. Engine inspection revealed that the #2 cylinder exhaust rocker arm shaft, p/n45937, was missing. Drive train continuity was established with the exception of the #2 exhaust valve. Centrifugal stops prevent feathering of the prop below an engine speed of 500 rpm. All 10 occupants were rescued.
Probable cause:
Occurrence #1: loss of engine power (total) - mech failure/malf
Phase of operation: takeoff - initial climb
Findings
1. (c) exhaust system, actuator - separation
----------
Occurrence #2: ditching
Phase of operation: landing - flare/touchdown
Findings
2. (f) propeller feathering - not possible - pilot in command
Final Report:

Crash of a Short SC.7 Skyvan 3 Variant 200 in Kona: 2 killed

Date & Time: Aug 25, 1977 at 0540 LT
Type of aircraft:
Registration:
N4917
Flight Type:
Survivors:
No
Schedule:
Honolulu - Kona
MSN:
1850
YOM:
1968
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
25107
Captain / Total hours on type:
161.00
Circumstances:
On final approach to Kona-Keahole Airport, the twin engine airplane stalled and crashed short of runway threshold. The aircraft was destroyed and both occupants were killed.
Probable cause:
Stall on final approach after the pilot-in-command failed to maintain flying speed.
Final Report:

Crash of a Beechcraft H18 near Hilo: 11 killed

Date & Time: Apr 11, 1974 at 0941 LT
Type of aircraft:
Operator:
Registration:
N28358
Flight Phase:
Survivors:
No
Site:
Schedule:
Kailua-Kona – Kahului
MSN:
BA-755
YOM:
1969
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
11
Captain / Total flying hours:
4490
Captain / Total hours on type:
522.00
Circumstances:
While flying in poor weather conditions, the twin engine airplane struck the slope of a mountain located northwest of Hilo. The wreckage was found a day later and all 11 occupants have been killed.
Probable cause:
It was determined that the pilot was flying under VFR mode in adverse weather conditions. High obstructions and low ceiling were considered as contributing factors.
Final Report: