Crash of a Cessna 208B Grand Caravan in Saint Mary's: 4 killed

Date & Time: Nov 29, 2013 at 1824 LT
Type of aircraft:
Operator:
Registration:
N12373
Survivors:
Yes
Schedule:
Bethel - Mountain Village - Saint Mary's
MSN:
208B-0697
YOM:
1998
Flight number:
ERR1453
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
25000
Captain / Total hours on type:
1800.00
Aircraft flight hours:
12653
Circumstances:
The scheduled commuter flight departed 40 minutes late for a two-stop flight. During the first leg of the night visual flight rules (VFR) flight, weather at the first destination airport deteriorated, so the pilot diverted to the second destination airport. The pilot requested and received a special VFR clearance from an air route traffic controller into the diversion airport area. Review of automatic dependent surveillance-broadcast data transmitted by the airplane showed that, after the clearance was issued, the airplane's track changed and proceeded in a direct line to the diversion airport. Postaccident examination of the pilot's radio showed that his audio panel was selected to the air route traffic control (ARTCC) frequency rather than the destination airport frequency; therefore, although the pilot attempted to activate the pilot-controlled lighting at the destination airport, as heard on the ARTCC frequency, it did not activate. Further, witnesses on the ground at St. Mary's reported that the airport lighting system was not activated when they saw the accident airplane fly over, and then proceed away from the airport. Witnesses in the area described the weather at the airport as deteriorating with fog and ice. About 1 mile from the runway, the airplane began to descend, followed by a descending right turn and controlled flight into terrain. The pilot appeared to be in control of the airplane up to the point of the right descending turn. Given the lack of runway lighting, the restricted visibility due to fog, and the witness statements, the pilot likely lost situational awareness of the airplane's geographic position, which led to his subsequent controlled flight into terrain. After the airplane proceeded away from the airport, the witnesses attempted to contact the pilot by radio. When the pilot did not respond, they accessed the company's flight tracking software and noted that the airplane's last reported position was in the area of the airplane's observed flightpath. They proceeded to search the area where they believed the airplane was located and found the airplane about 1 hour later. Postaccident examination of the airframe and engine revealed no mechanical malfunctions or anomalies that would have precluded normal operation. About 3/4 inch of ice was noted on the nonprotected surfaces of the empennage. However, ice formation on the airplane's inflatable leading edge de-ice boots was consistent with normal operation of the de-ice system, and structural icing likely was not a factor in the accident. According to the company's General Operations Manual (GOM), operational control was held by the flight coordinator for the accident flight, and the flight coordinator and pilot-in-command (PIC) were jointly responsible for preflight planning, flight delay, and release of the flight, which included the risk assessment process. The flight coordinator assigned the flight a risk level of 2 (on a scale of 1 to 4) due to instrument meteorological and night conditions and contaminated runways at both of the destination airports. The first flight coordinator assigned another flight coordinator to create the manifest, which listed eight passengers and a risk assessment level of 2. According to company risk assessment and operational control procedures, a risk level of 2 required a discussion between the PIC and flight coordinator about the risks involved. However, the flight coordinators did not discuss with the pilot the risks and weather conditions associated with the flight. Neither of the flight coordinators working the flight had received company training on the risk assessment program. At the time of the accident, no signoff was required for flight coordinators or pilots on the risk assessment form, and the form was not integrated into the company manuals. A review of Federal Aviation Administration (FAA) surveillance activities revealed that aviation safety inspectors had performed numerous operational control inspections and repeatedly noted deficiencies within the company's training, risk management, and operational control procedures. Enforcement Information System records indicated that FAA inspectors observed multiple incidences of the operator's noncompliance related to flight operations and that they opened investigations; however, the investigations were closed after only administrative action had been taken. Therefore, although FAA inspectors were providing surveillance and noting discrepancies within the company's procedures and processes, the FAA did not hold the operator sufficiently accountable for correcting the types of operational deficiencies evident in this accident, such as the operator's failure to comply with its operations specifications, operations training manual, and GOM and applicable federal regulations.
Probable cause:
The pilot's decision to initiate a visual flight rules approach into an area of instrument meteorological conditions at night and the flight coordinators' release of the flight without discussing the risks with the pilot, which resulted in the pilot experiencing a loss of situational awareness and subsequent controlled flight into terrain. Contributing to the accident were the operator's inadequate procedures for operational control and flight release and its inadequate training and oversight of operational control personnel. Also contributing to the accident was the Federal Aviation Administration's failure to hold the operator accountable for correcting known operational deficiencies and ensuring compliance with its operational control procedures.
Final Report:

Crash of a Beechcraft 1900C-1 in Saint Mary's

Date & Time: Feb 11, 1999 at 2345 LT
Type of aircraft:
Operator:
Registration:
N31240
Flight Type:
Survivors:
Yes
Schedule:
Anchorage – Saint Mary’s
MSN:
UC-28
YOM:
1988
Flight number:
AER91
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12326
Captain / Total hours on type:
1587.00
Aircraft flight hours:
19588
Circumstances:
The airline transport pilot was cleared for the localizer approach. The airplane impacted the ground 3.2 nautical miles from the runway threshold. The minimum descent altitude (MDA) for the approach was 560 feet msl, which is 263 feet above touchdown. Night, instrument meteorological conditions prevailed at the time of the accident. The surrounding terrain was flat, snow-covered, and featureless. The reported weather was 200 feet overcast, 1 1/2 miles visibility in snow, and winds of 12 knots, gusting to 32 knots. The pilot reported he was established on the final approach course, descending to the MDA, and then woke up in the snow. He said he did not remember any problems with the airplane. No pre accident mechanical anomalies were discovered with the airplane during the investigation. The airport has high intensity runway lights, sequenced flashing lead-in lights, and visual approach slope indicator lights. All airport lights and navigation aids were functioning. The airplane was not equipped with an autopilot. Captains have the option of requesting a copilot, but, the captain's pay is reduced by a portion equal to one-half the copilot's pay. The pilot had returned from the previous nights trip at 0725. He had three rest periods, four hours, two hours, and five hours 15 minutes, since his previous nights flight. Each rest period was interrupted by contact with the company. The company indicated that it is the pilot's responsibility to tell the company if duty times are being exceeded. 14 CFR 135.267 states, in part: '(d) Each assignment ... must provide for at least 10 consecutive hours of rest during the 24 hours that precedes the planned completion of the assignment.'
Probable cause:
The pilot's descent below the minimum descent altitude on the instrument approach. Factors were pilot fatigue resulting from the pilot's rest period being interrupted by scheduling discussions and the night weather conditions of low ceilings and whiteout.
Final Report:

Crash of a De Havilland DHC-4A Caribou in Sparrevohn: 1 killed

Date & Time: Jan 29, 1997 at 2310 LT
Type of aircraft:
Operator:
Registration:
N702SC
Flight Type:
Survivors:
Yes
Schedule:
Saint Mary's - Kenai
MSN:
126
YOM:
1963
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4987
Captain / Total hours on type:
220.00
Aircraft flight hours:
13923
Circumstances:
The CFR Part 135 cargo flight departed at night on an IFR flight with a load of mining equipment. Route of flight was over remote/mountainous terrain. About 2 hours after takeoff, while cruising at 12,000' feet msl, the right engine and propeller began to overspeed. The captain feathered the #2 engine and declared an emergency. He began to divert to an alternate destination, about 120 miles away in an area of lower terrain, but the aircraft would not maintain altitude (single engine service ceiling, as loaded, was about 8,700 feet). The captain increased power to the left engine, but it began to produce banging and coughing noises. The captain elected to perform an emergency landing at a nearby, remote, military airfield (A/F). The A/F was located in mountainous terrain and had a one-way, daylight only approach. The captain lowered the gear and flaps, and began a visual approach while attempting to keep the runway end identifier lights (REIL) in view. The aircraft encountered severe turbulence, and the captain applied full throttle to the left engine in an attempt to climb. The REIL disappeared from view, and the aircraft collided with snow covered terrain about 2 miles west of the A/F. Ground personnel at the A/F reported high winds and blowing snow with limited visibility. Postcrash exam of the right engine revealed a loss of the propeller control system hydraulic oil. Flight at 12,000 feet was conducted without crew oxygen. The crew had exceeded their maximum allowable duty day without adequate crew rest.
Probable cause:
Loss of the right engine propeller control oil, which led to an overspeed of the right engine and propeller, and necessitated a shut-down of the right engine; and failure of the pilot to maintain adequate altitude/distance from terrain during visual approach for a precautionary landing at an alternate airport. Factors relating to the accident were: fluctuation of the left engine power, premature lowering of the airplane flaps, and an encounter with adverse weather conditions (including high winds, severe turbulence, and white-out conditions) during the approach.
Final Report:

Crash of a Cessna 207 Skywagon in Saint Mary's: 1 killed

Date & Time: Jun 16, 1986 at 1955 LT
Operator:
Registration:
N9699M
Flight Type:
Survivors:
No
Schedule:
Marshall - Saint Mary's
MSN:
207-0718
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2644
Captain / Total hours on type:
2293.00
Aircraft flight hours:
3858
Circumstances:
The pilot stalled the airplane while making a steep turn to avoid high voltage power lines. The airplane caught fire on impact and the air taxi pilot subsequently died of extensive thermal injuries. The pilot was flying in formation with another aircraft at low altitude. When the power lines were sighted the other aircraft successfully pulled up and avoided the wires. The accident pilot turned steeply and lost control of the aircraft before crashing.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: maneuvering
Findings
1. (c) procedures/directives - not followed - pilot in command
2. (f) improper use of procedure - pilot in command
3. (c) airspeed - not maintained - pilot in command
4. (c) clearance - not maintained - pilot in command
Final Report:

Crash of a Beechcraft G90 King Air in Saint Mary's: 2 killed

Date & Time: Feb 13, 1985 at 2200 LT
Type of aircraft:
Registration:
N2019U
Survivors:
No
Schedule:
Dubois - Saint Mary's
MSN:
LJ-792
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
9000
Captain / Total hours on type:
500.00
Aircraft flight hours:
2930
Circumstances:
The aircraft crashed during a LOC DME approach. According to ATC the aircraft crashed after making a procedure turn at the faf. The winds in the area were being called 250° at 10 knots gusting to 28 knots. A caution on the approach plate has a remark, 'precipitous terrain - expect turbulence'. Both occupants were killed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: approach - faf/outer marker to threshold (ifr)
Findings
1. (c) in-flight planning/decision - improper - pilot in command
2. (c) ifr procedure - improper - pilot in command
3. (c) planned approach - improper - pilot in command
4. (c) minimum descent altitude - below - pilot in command
Final Report:

Crash of a Cessna 207 Skywagon in Chevak: 2 killed

Date & Time: Dec 21, 1978 at 1430 LT
Registration:
N7378U
Survivors:
Yes
Schedule:
Saint Mary’s – Chevak
MSN:
207-0426
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2075
Captain / Total hours on type:
600.00
Circumstances:
While approaching Chevak, the pilot encountered whiteout conditions and limited visibility due to snow falls. The pilot suffered a spatial disorientation and the airplane collided with ground while in traffic pattern-circling. Two passengers were killed while five other occupants were seriously injured.
Probable cause:
Controlled flight into terrain while in traffic pattern-circling after the pilot continued VFR flight in adverse weather conditions. The following contributing factors were reported:
- The pilot suffered a spatial disorientation,
- Whiteout conditions.
Final Report:

Crash of a De Havilland DH.84 Dragon 2 in Land’s End: 1 killed

Date & Time: Jun 25, 1938 at 1010 LT
Type of aircraft:
Operator:
Registration:
G-ADCR
Survivors:
Yes
Schedule:
Saint Mary’s – Land’s End
MSN:
6094
YOM:
1935
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The approach to Land’s End Airport was completed in very bad weather conditions. During the last segment, the twin engine aircraft hit the runway surface, went out of control and crashed. All six passengers were injured and the pilot, Captain David Louis Dustin was killed.

Crash of a Travel Air 6000B in Kane: 4 killed

Date & Time: Sep 29, 1929 at 1900 LT
Type of aircraft:
Registration:
NC9929
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Saint Mary’s – Bradford
MSN:
1080
YOM:
1929
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The aircraft departed St Mary's on a private trip to Bradford, north Pennsylvania. En route, the pilot encountered poor visibility due to foggy conditions. He reduced his altitude and apparently attempted an emergency landing when the aircraft crashed in a pasture near Kane. The aircraft was destroyed and all four occupants were killed.