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Crash of a Pilatus PC-12/47 in Mesquite

Date & Time: Apr 23, 2020 at 1600 LT
Type of aircraft:
Operator:
Registration:
N477SS
Flight Type:
Survivors:
Yes
Schedule:
Dallas – Muscle Shoals
MSN:
813
YOM:
2007
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2283
Captain / Total hours on type:
1137.00
Aircraft flight hours:
7018
Circumstances:
Shortly after takeoff the pilot reported to the air traffic controller that he was losing engine power. The pilot then said he was going to divert to a nearby airport and accepted headings to the airport. The pilot then reported the loss of engine power had stabilized, so he wanted to return to his departure airfield. A few moments later the pilot reported that he was losing engine power again and he needed to go back to his diversion airport. The controller reported that another airport was at the pilot’s 11 o’clock position and about 3 miles. The pilot elected to divert to that airport. The airplane was at 4,500 ft and too close to the airport, so the pilot flew a 360° turn to set up for a left base. During the turn outbound, the engine lost all power, and the pilot was not able to reach the runway. The airplane impacted a field, short of the airport. The airplane’s wings separated in the accident and a small postcrash fire developed. A review of the airplane’s maintenance records revealed maintenance was performed on the day of the accident flight to correct reported difficulty moving the Power Control Lever (PCL) into reverse position. The control cables were inspected from the pilot’s control quadrant to the engine, engine controls, and propeller governor. A static rigging check of the PCL was performed with no anomalies noted. Severe binding was observed on the beta control cable (propeller reversing cable). The cable assembly was removed from the engine, cleaned, reinstalled, and rigged in accordance with manufacturer guidance. During a post-accident examination of the engine and propeller assembly, the beta control cable was found mis-rigged and the propeller blades were found in the feathered position. The beta valve plunger was extended beyond the chamfer face of the propeller governor, consistent with a position that would shut off oil flow from the governor oil pump to the constant speed unit (CSU). A wire could be inserted through both the forward and aft beta control cable clevis inspection holes that function as check points for proper thread engagement. The forward beta control cable clevis adjustment nut was rotated full aft. The swaging ball end on the forward end of the beta control cable was not properly secured between the clevis rod end and the push-pull control terminal and was free to rotate within the assembly. Before takeoff, the beta valve was in an operational position that allowed oil flow to the CSU, resulting in normal propeller control. Vibration due to engine operation and beta valve return spring force most likely caused the improperly secured swaging ball to rotate (i.e. “unthread”) forward on the beta control cable. The resulting lengthening of the reversing cable assembly allowed the beta valve to stroke forward and shut off oil flow to the propeller CSU. Without propeller servo oil flow to maintain propeller control, the propeller faded to the high pitch/feather position due to normal leakage in the transfer bearing. The reported loss of power is consistent with a loss of thrust due to the beta control cable being mis-rigged during the most recent maintenance work.
Probable cause:
The loss of engine power due to a mis-rigged beta control cable (propeller reversing cable), which resulted in a loss of thrust inflight.
Final Report:

Crash of a Beechcraft B100 King Air in Jackson: 1 killed

Date & Time: Nov 13, 1997 at 1238 LT
Type of aircraft:
Registration:
N500ML
Survivors:
No
Schedule:
Muscle Shoals – Jackson
MSN:
BE-78
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3646
Captain / Total hours on type:
162.00
Aircraft flight hours:
4231
Circumstances:
During an IFR arrival, vectors were provided for an ILS runway 16L approach. While on assigned heading and altitude of 270 degrees and 3,000 feet, about 8 miles north of the final approach fix, the pilot was told to turn left to 185 degrees and maintain 2,200 feet until established on the localizer, then he was cleared for the approach. The pilot acknowledged the instructions. About 1 minute later, communication and radar contact with the airplane were lost. Eye witnesses near the accident site observed the airplane as it descended below the cloud layer. The airplane was described as being in a steep left bank with the nose down. Witnesses also stated that the engines were revving. Within seconds of the visual sighting, the airplane crashed. Examination of the airframe failed to disclose a mechanical problem. No fire or smoke was seen coming from the airplane before it crashed. The pilot did not report experiencing a problem with the airplane to the tower controller. Toxicology tests of the pilot indicated O.323 mcg/ml chlorpheniramine (a sedating antihistamine) in liver fluid and 0.073 mcg/ml chlorpheniramine in kidney fluid. Also, unspecified levels of dextromethorphan (a cough suppressant), pseudoephedrine (a decibgestabt), and phenylpropanolamine (a decongestant) were reported in kidney and liver fluids. All medications are available in over-the-counter cold remedies.
Probable cause:
The pilot's failure to maintain control of the aircraft due to spatial disorientation. A related factor was: the instrument weather conditions.
Final Report:

Crash of a Beechcraft A100 King Air in Muscle Shoals

Date & Time: Jun 22, 1978 at 0712 LT
Type of aircraft:
Operator:
Registration:
N941K
Survivors:
Yes
Schedule:
Chattanooga - Muscle Shoals
MSN:
B-111
YOM:
1972
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
20834
Captain / Total hours on type:
24.00
Circumstances:
On final approach to Muscle Shoals Airport, the airplane lost speed, stalled and crashed short of runway. All six occupants were seriously injured and the aircraft was destroyed.
Probable cause:
Stall on final approach after the pilot-in-command failed to maintain flying speed. The following contributing factors were reported:
- Improper operation of powerplant and powerplant controls,
- Lack of familiarity with aircraft,
- Fog,
- Poor crew coordination,
- Visibility one mile or less,
- The pilot-in-command reduced props instead of throttles.
Final Report:

Crash of a Beechcraft E18S in Sumter: 4 killed

Date & Time: Sep 17, 1972 at 1745 LT
Type of aircraft:
Operator:
Registration:
N21DD
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Sumter - Muscle Shoals
MSN:
BA-369
YOM:
1958
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
Just after liftoff, while in initial climb, one of the engine failed. The crew lost control of the aircraft that stalled and crashed in flames. All four occupants were killed.
Probable cause:
Powerplant failure for undetermined reason. The following factors were reported:
- The pilot-in-command failed to maintain flying speed,
- Improper emergency procedures,
- The crew failed to retract the landing gear,
- Improperly loaded aircraft,
- The aircraft was approximately 300 pounds over gross weight.
Final Report: