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Crash of a Piper PA-61P Aerostar (Ted Smith 601) near Carrollton

Date & Time: Oct 20, 2016 at 1110 LT
Operator:
Registration:
N601UK
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Hampton – Carrollton
MSN:
61-0183-012
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1338
Captain / Total hours on type:
36.00
Aircraft flight hours:
2236
Circumstances:
The pilot reported that the purpose of the flight was to reposition the airplane to another airport for refuel. During preflight, he reported that the airplane's two fuel gauges read "low," but the supplemental electronic fuel totalizer displayed 55 total gallons. He further reported that it is not feasible to visual check the fuel quantity, because the fueling ports are located near the wingtips and the fuel quantity cannot be measured with any "external measuring device." According to the pilot, his planned flight was 20 minutes and the fuel quantity, as indicated by the fuel totalizer, was sufficient. The pilot reported that about 12 nautical miles from the destination airport, both engines began to "surge" and subsequently lost power. During the forced landing, the pilot deviated to land in grass between a highway, the airplane touched down hard, and the landing gear collapsed. The fuselage and both wings sustained substantial damage. The pilot reported no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation. The pilot reported in the National Transportation Safety Board Pilot/ Operator Aircraft Accident Report that there was a "disparity" between the actual fuel quantity and the fuel quantity set in the electronic fuel totalizer. He further reported that a few days before the accident, he set the total fuel totalizer quantity to full after refueling, but in hindsight, he did not believe the fuel tanks were actually full because the wings may not have been level during the fueling. The "Preflight" chapter within the operating manual for the fuel totalizer in part states: "Digiflo-L is a fuel flow measuring system and NOT a quantity-sensing device. A visual inspection and positive determination of the usable fuel in the fuel tanks is a necessity. Therefore, it is imperative that the determined available usable fuel be manually entered into the system."
Probable cause:
The pilot's failure to verify the usable fuel in the fuel tanks, which resulted in an inaccurate fuel totalizer setting during preflight, fuel exhaustion, and a total loss of engine power.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Foley

Date & Time: Apr 26, 2016 at 1424 LT
Registration:
N3372Q
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Foley - Carrollton
MSN:
421B-0256
YOM:
1972
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5450
Circumstances:
The private pilot of the twin-engine airplane departed on the personal flight. During the takeoff roll, all indications were normal. When the airplane accelerated to between 75 and 80 knots, the pilot pulled back on the yoke slowly, and the airplane began to climb. After he raised the landing gear, the pilot noticed that the airplane was not continuing to climb and that the airspeed was 80 knots; he then heard the stall warning horn. The airplane impacted trees about 1/4 mile from the runway, caught fire, and was destroyed; the pilot egressed with minor injuries. The airplane's published minimum control speed was 86 knots and the break ground and climb speed was 106 knots. Given that information, it is likely that the pilot's attempt to rotate and climb the airplane below 80 knots resulted in the airplane being unable to gain altitude and climb above trees at the end of the runway.
Probable cause:
The pilot's failure to obtain proper takeoff speed before breaking ground, which resulted in the airplane's failure to gain altitude and a collision with trees and terrain.
Final Report:

Crash of an Embraer EMB-120RT Brasília in Carrollton: 8 killed

Date & Time: Aug 21, 1995 at 1253 LT
Type of aircraft:
Operator:
Registration:
N256AS
Survivors:
Yes
Schedule:
Atlanta - Gulfport
MSN:
120-122
YOM:
1989
Flight number:
EV529
Crew on board:
3
Crew fatalities:
Pax on board:
26
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
9876
Captain / Total hours on type:
7374.00
Copilot / Total flying hours:
1193
Copilot / Total hours on type:
363
Aircraft flight hours:
17151
Aircraft flight cycles:
18171
Circumstances:
Atlantic Southeast Airline Flight 529 was climbing through 18,000 feet, when a blade from the left propeller separated. This resulted in distortion of the left engine nacelle, excessive drag, loss of wing lift, and reduced directional control. The degraded performance resulted in a forced landing. While landing, the airplane passed through trees, impacted the ground, and was further damaged by post impact fire. An exam of the left propeller revealed the blade had failed due to a fatigue crack that originated from multiple corrosion pits in the taper bore surface of the blade spar. The crack had propagated toward the outside of the blade and around both sides of the taper bore. Due to 2 previous blade failures (separations), a borescope inspection procedure had been developed by Hamilton Standard to inspect returned blades (that had rejectable ultrasonic indications) for evidence of cracks, pits and corrosion. The accident blade was one of 490 rejected blades that had been sent to Hamilton Standard for further evaluation and possible repair. Maintenance technicians, who inspected the blade, lacked proper NDI familiarization training and specific equipment to identify the corrosion that resulted in fatigue. The captain and seven passengers were killed.
Probable cause:
The in-flight fatigue fracture and separation of a propeller blade resulting in distortion of the left engine nacelle, causing excessive drag, loss of wing lift, and reduced directional control of
the airplane. The fracture was caused by a fatigue crack from multiple corrosion pits that were not discovered by Hamilton Standard because of inadequate and ineffective corporate inspection and repair techniques, training, documentation, and communications. Contributing to the accident was Hamilton Standard's and FAA's failure to require recurrent on-wing ultrasonic inspections of the affected propellers. Contributing to the severity of the accident was the overcast cloud ceiling at the accident site.
Final Report:

Crash of a Mitsubishi MU-2B-30 Marquise in Hawesville

Date & Time: Jan 19, 1978 at 0935 LT
Type of aircraft:
Operator:
Registration:
N115S
Survivors:
Yes
Schedule:
Carrollton - Hawesville
MSN:
518
YOM:
1970
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5600
Captain / Total hours on type:
598.00
Circumstances:
On final approach, the twin engine airplane stalled and crashed short of runway. All seven occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Stall on final approach after the crew misjudged distance and altitude and failed to maintain flying speed.
Final Report: