Crash of a Convair B-36F-10-CF Peacemaker in Carswell AFB

Date & Time: Mar 6, 1952
Type of aircraft:
Operator:
Registration:
50-1067
Flight Type:
Survivors:
Yes
MSN:
175
YOM:
1950
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On touchdown, the left main gear partially failed. A fuel leak occurred on the left side of the airplane that slid for several yards before coming to rest in flames. While all occupants were able to evacuate safely, the aircraft was destroyed by fire.
Probable cause:
Failure of the left main gear on landing.

Crash of a Convair B-36B-20-CF Peacemaker in Fairchild AFB

Date & Time: Jan 29, 1952
Type of aircraft:
Operator:
Registration:
44-92080
Flight Type:
Survivors:
Yes
Schedule:
Fairchild - Fairchild
MSN:
77
YOM:
1946
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On final approach to Fairchild AFB, the six engine aircraft crashed short of runway and came to rest in flames against a snow bank. All crew members were evacuated safely while the aircraft was destroyed by fire.

Crash of a Convair B-36D-25-CF Peacemaker in Kirtland AFB: 23 killed

Date & Time: May 6, 1951 at 1230 LT
Type of aircraft:
Operator:
Registration:
49-2660
Flight Type:
Survivors:
Yes
Schedule:
Carswell - Kirtland
MSN:
117
YOM:
1949
Crew on board:
9
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
23
Circumstances:
On final approach to Kirtland AFB, the crew encountered strong crosswinds up to 35 knots. After passing over the runway 08 threshold, while at a height of 200 feet, the aircraft banked right, causing the engine number six to hit the runway surface. On impact, the engine was seriously damaged and caught fire. The pilot in command attempted to make a go around when the aircraft nosed down and crashed in a huge explosion. Two passengers were seriously injured while 23 other occupants were killed.
Crew:
Maj Edward L. Warner Jr., pilot, †
Cpt Grant H. Fenn, pilot, †
Cpt Albert J. Gregg Jr., navigator, †
Cpt George W. Lee, radar observer, †
1st Lt Mitchell J. Buckalew, flight engineer, †
Sgt Kenneth R. Cota, radio operator, †
S/Sgt Arthur I. Botten, senior gunner, †
S/Sgt Robert A. Baker, senior gunner, †
1st Lt John L. Corley, flight engineer. †
Passengers:
Cpt Fred M. Mitchem, †
S/Sgt Thomas C. Gustavson, †
Sgt Henry C. Dox, †
S/Sgt Estill Myrick, †
Sgt Lloyd L. Goolsby, †
S/Sgt Dale F. Curtis, †
Sgt George F. Soroe Jr., †
M/Sgt John Ritz, †
T/Sgt John T. Thompson, †
S/Sgt James Margoee, †
Sgt Charles E. Linn, †
Sgt Berry Hays, †
Cpl Wilfred S. Leclair Jr., †
Pfc William J. Powers, †
Cpl Richard N. Fogwell,
S/Sgt Jack E. Erickson.
Probable cause:
It was determined that strong crosswinds were gusting up to 35 knots when the aircraft was approaching Kirtland AFB runway 08. The approach configuration on part of the flying crew was improper and the reaction of the pilot in command was excessive, causing the aircraft to bank right.

Crash of a Convair B-36D-25-CF Peacemaker near Perkins: 13 killed

Date & Time: Apr 27, 1951 at 1341 LT
Type of aircraft:
Operator:
Registration:
49-2658
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Carswell - Carswell
MSN:
115
YOM:
1949
Crew on board:
17
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
13
Circumstances:
Aircraft Commander Major Charles Crecelius, Pilot Major William Apgar, and Co-pilot Captain Harold Barry, a crew of thirteen, and a civilian observer took off from Carswell AFB in B-36D, 49-2658 of the 436th Bomb Squadron of the 7th Bomb Wing at 8:00 A.M. on April 27, 1951. 49-2658 was an element in a flight of three B-36Ds. Their mission included bombing practice at the Midland, Texas bombing range followed by gunner training with a simulated air attack by North American F-51D Mustangs near Oklahoma City. Four Mustangs from the 185th Tactical Reconnaissance Squadron took off from Will Rogers Field in Oklahoma City at 1:20 in the afternoon. They climbed to 20,000 feet altitude to intercept the bombers. They made a series of passes by the bombers to give their gunners practice tracking real airplanes. Training began with a series of high side passes. Then the B-36D reversed course for a series of high frontal passes. Major Crecelius flew the B-36D straight and level at 20,000 feet altitude. One of the regular gunners was back at Carswell AFB occupied by other duties, so Crew Chief M/Sgt William Blair was invited back to the rear compartment to man the lower left gunner station. Each Mustang flew past the B-36D, headed the same direction as the bomber, and then made a 180 degree turn to approach it from the front. The gunners aboard the B-36D tracked the F-51Ds with their General Electric manufactured gun sighting mechanisms, shooting pictures instead of bullets. A flight of two Mustangs piloted by Captain Robinson Risner and 1st Lt Fred Black made a high frontal pass on the bomber. The gunners estimated that Captain Risner's Mustang passed less than 100 feet below the wing of the B-36D. Radio Operator T/Sgt Albert Wolf commented over the intercom, "Man, he nearly hit the props". In the rear compartment, Crew Chief M/Sgt William Blair exclaimed, "He went between the props, didn't he?" As Lt Black approached in his F-51D, Wolf asked, "What's this guy going to do?" The gunners in the rear compartment never saw Lt. Black's Mustang, but they felt the collision. The F-51D hit the fuselage of the B-36D on the top left about nine feet back from the nose. The Mustang broke into two big pieces and lots of small chunks and burst into flames. The three surviving Mustang pilots saw two flaming objects tumble away from the B-36D. The B-36D porpoised for several seconds and pitched up into a steep climb. Then it fell off to the left into a spiral dive. Flight Engineer 1st Lt. Elroy Melberg manned the lower left gunner's station in the rear compartment. His first attempt to head for the exit hatch was thwarted by the web safety straps that connected his parachute harness to the floor. Precious seconds passed as he struggled to unclip his parachute harnesses from the safety straps. He had to use both hands to unfasten the clips as the pitching of the B-36D kept throwing him off balance. Gunner T/Sgt Milton Hewitt was in the lower right gunner's station across from 1st Lt Melberg. T/Sgt Hewitt refused to wear his parachute pack and had ridiculed crew members who wore them. His first impulse was to get to the bunk where he had left his parachute pack. Crew Chief M/Sgt William Blair was giving Gunner T/Sgt Milton Hewitt a replacement gun film canister when the collision occurred. M/Sgt. Blair injured his left leg as he was thrown against the bunks by the impact. He grabbed the exit hatch, but it would not open against the compartment pressurization. M/Sgt Blair called to T/Sgt. Hewitt to open the emergency pressure dump valve, but Hewitt was trying to get to his bunk to retrieve his parachute pack. They ran into each other as Blair reached for the pressure dump valve. Gunner T/Sgt Dick Thrasher occupied the upper left gunner's station. He had been aboard B-36B, 44-92075 when the crew was forced to bail out over Vancouver Island on February 13, 1950. Gunner T/Sgt Ellis Maxon sat across from T/Sgt. Thrasher in the upper right gunner's station. They climbed down the ladders to the exit hatch as the gyrations of the crippled bomber flung them about. M/Sgt. Blair dumped the pressure in the compartment and T/Sgt Thrasher pulled open the exit hatch. T/Sgt Thrasher lay down on his left side next to the exit hatch, grabbed the edge of the hatch and rolled himself headfirst out through the narrow opening. Having never bailed out of an airplane before, M/Sgt Blair paid careful attention to T/Sgt Thrasher's method of egress, intending to copy his moves. M/Sgt Blair assisted 1st Lt Melberg to release his parachute harness from the safety straps. He found the exit hatch blocked by the seven-foot long wooden dip stick that was used to measure the amount of fuel in the tanks. He moved the dip stick out of the way, but it fell across the hatch again. He injured the fingers of his right hand in the effort to get out the hatch. He crawled under the dipstick and stuck his head out the hatch. At that moment, the tail section of the B-36D ripped away from the rest of the fuselage from the bottom to the top at the forward bulkhead of the rear crew compartment. T/Sgt Maxon, 1st Lt Melberg, and M/Sgt Blair were thrown from the rear crew compartment as it ripped open. T/Sgt Hewitt was last seen trying to get his parachute pack from his bunk, but he did not survive the crash. The air around the survivors was filled with falling metal debris. One of the turret bay doors struck the shroud lines of M/Sgt Blair and the tail section tumbled past him on the way down. 1st Lt Melberg's parachute shroud lines struck him in the throat as his parachute opened. His disorientation and the nausea from the pain caused him to vomit repeatedly during the descent. The chest strap and quick release button of TSgt. Maxon's parachute hit him in the face and throat as his parachute opened, but he was too relieved to have escaped from the airplane to notice any pain. None of the twelve men in the forward compartment were able to escape from the falling bomber as it spun to the ground:
Maj Charles Crecelius, pilot,
Maj William Apgar, copilot,
Cpt Harold Barry, copilot,
Maj Aurther Burmeister, navigator,
Maj Robert Renner, radar observer,
Cpt William Walsh, radar observer,
Cpt William Zurivitza, radar observer,
Ernest Cox Jr., flight engineer,
T/Sgt Nathan Fetters, radio operator,
T/Sgt Albert Wolf, radio operator,
T/Sgt Edward Ennis, radar mechanic,
Benedict O'Conner, civilian observer.
Wreckage from the B-36D fell across 3-1/2 miles of Oklahoma pasture land, ten miles south of the town of Perkins, Oklahoma and 37 miles north northeast of Tinker AFB at 1:41 P.M. CST. The F-51D impacted 12 miles south of Stillwater with 1st Lt Fred Black still in the cockpit. The four survivors saw several other empty parachutes descending with them. They were unable to control the oscillation of their parachutes. Each of them hit the ground in an uncontrolled fashion. T/Sgt Maxon landed in a 3-foot deep ditch and injured the medial meniscus of both knees. As he was dragged a short distance by his parachute, he suffered abrasions to his right knee, contusions to his left thumb and the left side of his neck, and a laceration to his scalp. M/Sgt Blair's parachute dragged him a few feet after landing, and he suffered additional abrasions on his leg, abdomen, and lower left eyelid. T/Sgt Thrasher and 1st Lt Melberg also suffered rough landings. M/Sgt Blair landed just 100 yards from the home of a civilian oil company employee. The civilian got his company car and drove Blair to the place where T/Sgt Maxon and 1st Lt Melberg had come down. Melberg looked pretty beat up, so the civilian took him and Blair to the doctor in Perkins, Oklahoma. T/Sgt Thrasher and T/Sgt Maxon were picked up by officers of the Oklahoma Highway Patrol and were also transported to the doctor in Perkins. The fuel tanks in the wings of the B-36D ruptured when it hit the ground. The gasoline erupted in flames, but a large portion of the fuel drained down the hill away from the crash. The resulting grass fire burned about 8 acres. It burned itself out before emergency vehicles from Tinker AFB arrived at the crash site approximately two hours after the crash. The parachute and billfold of one of the deceased crew members on the B-36D were found 40 miles northeast of the main crash site.
Source & photos:
http://www.air-and-space.com/b-36 wrecks.htm#49-2658

Crash of a Convair B-36B-1-CF Peacemaker near Crowley: 2 killed

Date & Time: Nov 22, 1950 at 0950 LT
Type of aircraft:
Operator:
Registration:
44-92079
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Carswell - Carswell
MSN:
76
YOM:
1946
Location:
Crew on board:
16
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
Aircraft Commander 1st Lt. Oliver Hildebrandt, Pilot 1st Lt. Walter Ross, and Co-pilot Captain Wilbur Evans, and a crew of thirteen took off from Carswell AFB in B-36B, 44-92035 of the 26th Bomb Squadron of the 7th Bomb Wing at 5:05 A.M. on November 22,1950. The planned 30-hour training mission consisted of air-to-air gunnery, bombing, simulated radar bombing, and navigational training. Immediately after take-off, the #4 alternator would not stay in parallel with the other three alternators, so it was taken off-line and de-excited three minutes into the flight. About one minute after the #4 alternator was shut down, flames 8 to 12 feet long erupted from around the air plug of the number-one engine. The left scanner reported the flames to the pilot. Six minutes after take-off, the flight engineer shut down the number-one engine, feathered its propeller, and expended one of its Methyl bromide fire extinguishing bottles. The mission continued on the power of the remaining five engines. 44-92035 cruised to the gunnery range on Matagorda Island at an altitude of 5,000 feet. It arrived at 7:00 A.M. and the gunners began practicing. Radar Observer S/Sgt. Ray Earl manned the tail turret. The charger for the right gun burned out, so he expended just half of his ammunition. Then the APG-3 radar for the tail turret started acting up, so S/Sgt. Earl secured the set. Aircraft Commander 1st Lt. Oliver Hildebrandt noted that the vibration from firing the 20mm cannons increased significantly during the fourth gunnery pass. Immediately afterward, radar operator Captain James Yeingst notified Hildebrandt that the APQ-24 radar set blew up and was smoking. Vibration from the firing of the guns was causing shorting between the internal components of the radar. Then the liaison transmitter failed as well. The cannons in the left forward upper turret and the left rear upper turret stopped firing. The gunners attempted to retract the gun turrets, but the failed turrets would not retract. Gunner S/Sgt. Fred Boyd entered the turret bay, but other problems began to take precedence over the stuck turrets. Boyd was called out of the bay before he could manually crank the turret down. At 7:31 A.M. the number-three engine suffered an internal failure. The torque pressure fell to zero. The manifold pressure dropped to atmospheric pressure. The fuel flow dropped off, and the flight engineer could not stabilize the engine speed. The pilot shut down the number-three engine and feathered its propeller. The B-36B had only one operating engine on the left wing, so the pilot aborted the remainder of the training mission and set course for Kelly Air Force Base. Flight engineer Captain Samuel Baker retarded the spark, set the mixture controls to "normal", and set the engine RPMs to 2,500 to increase the power from the remaining engines. Unknown to Captain Baker, the vibration from the guns had disabled the electrical systems controlling the spark settings and fuel mixture. He immediately discovered that the turbo control knobs no longer affected the manifold pressure. The B-36B could not maintain its airspeed on the power of the four remaining engines. It descended about 1,000 feet and its airspeed bled off to 135 miles per hour. The pilot called for more power. The flight engineer attempted to increase engine speed to 2,650 RPM and enrich the fuel mixture, but got no response from the engines except for severe backfiring. The fuel mixture indicators for all of the engines indicated lean. The second flight engineer, M/Sgt. Edward Farcas, checked the electrical fuse panel. Although the fuses appeared to be intact, he replaced the master turbo fuse and all of the individual turbo fuses. He noticed that the turbo-amplifiers and mixture amplifiers were all cooler than normal. He climbed into the bomb bay to check the aircraft power panels and fuses, but could not find any problem there. Kelly Air Force Base had a cloud overcast at just 300 feet and the visibility was restricted to two miles. The weather at Bergstrom Air Force Base not as bad, with scattered clouds at 1,000 feet, broken clouds at 2,000 feet and 10 miles visibility. Carswell Air Force Base was clear with 10 miles visibility, but it was 155 miles farther away than Bergstrom. Air traffic control cleared all airspace below 4,000 feet aead of the crippled B-36B. Aircraft Commander Hildebrandt was flying on instruments in thick clouds. The poor weather at Kelly Air Force Base convinced Hildebrandt to change course from Kelly to Carswell Air Force Base, passing by Bergstrom Air Force Base on the way in case the airplane could not make it to Carswell. Bombardier Captain Robert Nelson made two attempts to salvo the 1,500 pounds of practice bombs in the rear bomb bay, but the bomb bay doors would not open by automatic or manual control, or emergency procedure. There was no way to dump fuel to reduce the weight of the B-36B. The flight engineers resorted to holding down the switches used to prime the fuel system in an attempt to increase fuel flow to the engines. M/Sgt. Edward Farcas held down the prime switches for the number-two and number-four engines while Captain Baker held down the prime switch for the number-five engine and operated the flight engineer's panel. The configuration of the switches did not allow them to prime the number-five engine and the number-six engine at the same time. The high power demand coupled with the lean fuel mixture made the cylinder head temperatures of the engines climb to 295 degrees C. Flight engineer Baker jockeyed the throttles, decreasing the throttle setting of the engine with the highest cylinder head temperature until another engine grew even hotter. The high temperature caused the gasoline/air mixture in the cylinders to detonate before the pistons reached top dead center, diminishing power and damaging the engines. Despite the critical situation with the engines, Aircraft Commander Hildebrandt decided to continue past Bergstrom Air Force Base to Carswell. Bergstrom was overcast and its runway was only 6,000 feet long. Carswell offered a much longer runway. By the time the B-36B reached Cleburne, the backfiring on all engines increased in violence. The number-2, number-5, and number-6 engines were running at 70% power and the number-4 engine was producing only 20% power. The airspeed had dropped off to 130 miles per hour. Aircraft Commander Hildebrandt attempted to restart the number-one engine, the one that had spouted flames on take-off, but fuel was not getting to its induction system. He tried to restart the number-three engine, but could not unfeather the propeller on that engine. As the bomber passed to the west of Cleburne, the right scanner reported dense white smoke, oil, and metal particles coming from the number-five engine. After a short while the number-five engine lost power, and Aircraft Commander Hildebrandt feathered the propeller on that engine while still twenty-one miles from Carswell Air Force Base. The B-36B could not stay airborne on the power of the three remaining failing engines. It was flying at just 125 miles per hour, seven miles per hour above the stall speed, losing both altitude and airspeed. Howard McCullough and W. Boeten were flying Civil Aeronautics Authority DC-3 N342 near Cleburne. They were notified by Meacham Tower to be on the lookout for 44-92035. They spotted it about five miles south of Cleburne. They observed that the number-one and number-three propellers were feathered and the number-five engine was on fire. They turned to follow the descending bomber. Aircraft Commander Hildebrandt ordered the crew to bail out of the stricken bomber. Bombardier Captain Robert Nelson had bailed out of airplanes on two previous occasions. He had crash landed twice and ditched once. He was the first man to bail out from the forward crew compartment. He suffered contusions of his lower spine when he landed. Radar Operator Captain James Yeingst responded to stress with laughter and jokes. He was a bit giddy before the bailout. He was the second man to exit from the forward crew compartment. His parachute streamed after he pulled the rip cord. He passed Captain Nelson going down. Captain Yeingst's parachute mushroomed open just before he hit the ground, but he suffered fatal injuries. Co-pilot Captain Wilbur Evans was the third man to exit from the forward crew compartment. He had bailed out of airplanes twice before and crash landed several times during WW-II. This time he broke both bones in his lower right leg when he landed. Navigator Captain Horace Stewart had previously tried to get off flying status because he felt that the B-36 was too dangerous. It is reported that during the hour before bailout, he was tense, nervous, and chain-smoking. He was the fourth man to bail out from the forward crew compartment. He pulled his rip cord right as he exited the forward escape hatch on the left side of the fuselage. His parachute opened and pulled him toward the number three propeller. His head hit the downward pointing blade of the propeller, killing him instantly. Radio Operator Cpl. Paul Myers followed Captain Stewart out the escape hatch. Myers landed with minor injuries. Flight Engineer M/Sgt. Edward Farcas jumped head first through the exit hatch of the forward crew compartment right after Cpl. Myers. His parachute did not open when he pulled the rip cord. He pulled the parachute out of its pack with his hands and landed with only minor injuries. Radar Mechanic Robert Gianerakis and Flight Engineer Captain Samuel Baker were the next to escape from the forward compartment. Both landed with only minor injuries. Radio Operator Sgt. Armando Villareal bailed out after Captain Baker. Villareal did not trust his parachute to open, so he pulled the rip cord while he was still in the forward crew compartment. He held his parachute in his arms as he jumped feet first through the escape hatch. Despite his unorthodox method of escape, he landed with only minor injuries. Pilot 1st Lt. Walter Ross was the next to last to leave the forward compartment. He landed with only minor injuries. Gunner S/Sgt. Andrew Byrne and Radar Observer S/Sgt. Ray Earl were the first two crew members to bail out of the rear crew compartment. Both landed with only minor injuries. Gunner Cpl. Calvin Martin was the third man to exit the rear crew compartment. He was swinging under his parachute as he hit the ground. He broke his right ankle as he landed. He fell backward onto a rock, fracturing his third lumbar vertebra and compressing his tailbone. Gunner S/Sgt. Ronald Williams followed Cpl. Martin out the rear escape hatch. He landed with only minor injuries. Gunner S/Sgt. Fred Boyd was the last man to exit the rear crew compartment. He called to Aircraft Commander Hildebrandt over the intercom to let him know that everyone had escaped from the aft compartment. When he turned back to the exit hatch, it had fallen shut. He had to open the hatch again to make his escape. He broke the fibula of his left leg when he landed farther to the north than the other crew members. After S/Sgt. Boyd reported that all other crew members had bailed out of the rear compartment, Aircraft Commander Hildebrandt set the autopilot and jumped clear when the bomber was less than 1,000 feet above the ground. He and nine other crew members escaped from the B-36B with only minor injuries. When McCullough and Boeten in DC-3, N342 saw the parachutes of the escaping crew members, they announced the bail-out on the emergency frequency of 121.25 megacycles. Each Report of Emergency Parachute Jump indicates that the incident occurred 20 miles south southeast of Carswell Air Force Base. The descent of the B-36B was witnessed by Mr. Buck Bell and his wife, who lived about 5 to 7 miles southwest of Crowley, Texas. Mr. Bell saw the crew members parachuting from the bomber, but did not see it hit the ground about one mile north of his house. Mr. James Bandy and his wife were on the road to Cleburne about 4 miles from their house on Route 1 near Joshua when they spotted the B-36B trailing smoke, flying in a nose-high attitude. They saw it hit the ground in a level attitude, raising a cloud of dust. The B-36B descended straight ahead in a nose-high attitude for a mile after Aircraft Commander Hildebrandt bailed out. It stalled, pitched nose down, and impacted in a terraced field on Less Armstrong's Dairy, 14 miles south of Carswell Air Force Base, 2 miles west of the South leg FTW range, and six miles west of Crowley at 9:50 in the morning. The forward crew compartment separated and folded underneath the rest of the fuselage. The tail section broke off, and the rear crew compartment came away from the mid-fuselage as the wreckage slid 850 feet along the ground and twisted to the right. The rear sections of the airplane remained largely intact. The elevation at the crash site was approximately 700 feet. Mr. W. Doggett witnessed the bail-out and crash from his home on Route 1 near Joshua. The B-36B impacted about 2-1/2 miles north of his house. He drove to the crash site in his pickup truck and helped the surviving crew members to regroup. Four minute after the crash, McCullough and Boeten in DC-3, N342 reported that two Navy aircraft were circling the wreckage. The wreckage smoldered for about eight minutes before a fire broke out in the number-six engine. The 15,000 gallons of remaining fuel consumed the forward fuselage and wings. The civilians and crew members were driven away from the crash site by exploding ammunition and the knowledge of the presence of 1,500 pounds of bombs aboard the airplane. Three helicopters arrived at the scene within an hour and twenty minutes of the crash.
Source : http://www.air-and-space.com/b-36 wrecks.htm#44-92035
Probable cause:
It was felt that a conventional cable-driven, back-up mixture control system would have prevented this accident.

Crash of a Convair B-36B-15-CF Peacemaker on Mt Kologet: 5 killed

Date & Time: Feb 14, 1950 at 0254 LT
Type of aircraft:
Operator:
Registration:
44-92075
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Eielson - Carswell
MSN:
72
Country:
Crew on board:
16
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The aircraft and its crew were taking part in an air exercise intended to ascertain the feasibility of operations against the Soviet Union in wintertime. Seven hours into the planned 24-hour flight, and over the Northern Pacific Ocean, three of the giant bomber's six engines caught fire owing to carburetor icing in the intense cold and had to be shut down. The three remaining engines were only producing limited power and the plane could not maintain height. The Mark IV atomic bomb being carried was jettisoned at 8,000 feet inside Canadian waters, and its high explosive detonator created a large shock wave that was visible on the surface. A dummy core was inserted in the bomb before it was dropped, so there was no nuclear explosion. To give his crew a chance of survival the captain took the B-36 to Princess Royal Island where the 16 crew members and one observer bailed out. 12 of the 17 survived their ordeal, but the first 4 to jump were never found, and are presumed to have descended into the freezing sea and died. Capt. Schreier's body was recovered from the crash site in the summer of 1954. The aircraft flew on for another 210 miles with Capt. Schreier at the controls before crashing on the side of Mount Kologet, in British Columbia, 6,000 feet above sea level and northwest of Hazelton. The resting place of 44-92075 went unknown until September 1953 when the wreckage was sighted during an unrelated air search.
Crew killed were:
Cpt Theodore F. Schreier, copilot,
Cpt William Phillips, navigator,
1st Lt Holiel Ascol, bombardier,
S/Sgt Neal A. Straley, gunner,
S/Sgt Elbert W. Pollard, gunner.
Source: ASN
Probable cause:
Engine fire and icing.

Crash of a Convair B-36B-15-CF Peacemaker in Carswell AFB: 5 killed

Date & Time: Sep 15, 1949 at 1945 LT
Type of aircraft:
Operator:
Registration:
44-92079
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Carswell - Carswell
MSN:
76
YOM:
1946
Crew on board:
13
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
Shortly after takeoff from runway 36 at Carswell AFB, while in initial climb, the aircraft suffered a technical failure, lost height and crashed into Lake Worth. Eight crew members were rescued while five others were killed. The aircraft sank and was lost. The crew was performing a local training sortie for the 9th BS.
Probable cause:
The propellers of two engines switched to reverse thrust shortly after liftoff, probably due to a failure of the thrust reverser system.