Zone

Crash of a Cessna 208B Super Cargomaster off Mobile: 1 killed

Date & Time: Oct 23, 2002 at 1945 LT
Type of aircraft:
Registration:
N76U
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Mobile - Montgomery
MSN:
208B-0775
YOM:
1999
Flight number:
BDC282
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4584
Captain / Total hours on type:
838.00
Aircraft flight hours:
4001
Circumstances:
The airplane was destroyed by impact forces. There was no evidence of fire. Wreckage examinations and all recovered wreckage from the impact area revealed no evidence of an inflight collisionor breakup, or of external contact by a foreign object. An examination of the engine and the propeller indicated that the engine was producing power at impact. The recovered components showed no evidence of preexisting powerplant, system, or structural failures. Wreckage examinations showed crushing and bending consistent with a moderate angle of descent and a moderate right-wing-down attitude at impact. The amount of wreckage recovered indicates that all parts of the airplane were at the crash site. The wreckage was scattered over an area of about 600 feet. An examination of radar and airplane performance data indicated that the accident airplane initiated a descent from 3,000 feet immediately after the accident pilot was given a second traffic advisory by air traffic control. The pilot reported that the traffic was above him. At the time the pilot stated that he needed to deviate, data indicate that the accident airplane was in or entering an uncontrolled descent. Radar data indicated that, after departure from the airport, the closest identified airplane to the accident airplane was a DC-10, which was at an altitude of about 4,000 feet. The horizontal distance between the two airplanes was about 1.1 nautical miles, and the vertical distance between the airplanes was about 1,600 feet. The accident airplane was never in a location at which wake turbulence from the DC-10 would have intersected the Cessna's flightpath (behind and below the DC-10's flightpath). Given the relative positions of the accident airplane and the DC-10, wake turbulence was determined to not be a factor in this accident. Although the DC-10 was left of the position given to the pilot by Mobile Terminal Radar Approach Control, air traffic controllers do not have strict angular limits when providing traffic guidance. The Safety Board's airplane performance simulation showed that, beginning about 15 seconds before the time of the pilot's last transmission ("I needed to deviate, I needed to deviate"), his view of the DC-10 moved diagonally across the windscreen from his left to straight in front of the Cessna while tripling in size. The airplane performance simulation also indicated that the airplane experienced high bank and pitch angles shortly after the pilot stated, "I needed to deviate" (about 13 seconds after the transmission, the simulation showed the airplane rolling through 90° and continuing to roll to a peak of about 150° 3 seconds later) and that the airplane appeared to have nearly recovered from these extreme attitudes at impact. Performance data indicated that the airplane would had to have been structurally/aerodynamically intact to reach the point of ground impact from the point of inflight upset. There was no evidence of any other aircraft near the accident airplane or the DC-10 at the time of the accident. Soon after the accident, U.S. Coast Guard aircraft arrived at the accident scene. The meaning of the pilot's statement that he needed to deviate could not be determined. A review of air traffic control radar and transcripts revealed no evidence of pilot impairment or incapacitation before the onset of the descent and loss of control. A sound spectrum study conducted by the Safety Board found no evidence of loud noises during the pilot's last three radio transmissions but found that background noise increased, indicating that the cockpit area was still intact and that the airspeed was increasing. The study further determined that the overspeed warning had activated, which was consistent with the performance study and extreme fragmentation of the wreckage. Radar transponder data from the accident airplane were lost below 2,400 feet. The signal loss was likely caused by unusual attitudes, which can mask transponder antenna transmissions. A garbled transponder return recorded near the DC-10 was likely caused by the accident airplane's transponder returns masking the DC-10's returns (since the accident airplane was projected to be in line between the DC-10 and the ground radar) or by other environmental phenomena. Red transfer or scuff marks were observed on many pieces of the airplane wreckage, and these marks were concentrated on the lower airframe skin forward of the main landing gear and the nose landing gear area. The Safety Board and four laboratories compared the red-marked airplane pieces to samples of red-colored items found in the wreckage. These examinations determined that most of the red marks were caused by parts of the airplane, cargo, and items encountered during the wreckage recovery. The marks exhibited random directions of motion, and none of the marks exhibited evidence of an in-flight collision with another aircraft. A small piece of black, anodized aluminum found embedded in the left wing was subsequently identified as a fragment from a cockpit lighting dimmer. The accident occurred at night, with the moon obscured by low clouds. Instrument meteorological conditions prevailed, although visual conditions were reported between cloud layers. The terminal aerodrome forecast reported a possible cloud layer at 3,000 feet. Weather data and observations by the DC-10 pilot indicated that, after flying about 100 to 500 feet above the cloud layer and soon after sighting the DC-10, the accident airplane would have entered clouds. A number of conditions were present on the night of the accident that would have been conducive to spatial disorientation. For example, no visible horizon references existed between the cloud layers in which the pilot was flying because of the night conditions. In addition, to initiate a visual search and visually acquire the DC-10, varying degrees of eye and head movements would have accompanied the pilot's shifting of attention outside the cockpit. Once the DC-10 was visually acquired by the pilot, it would have existed as a light source moving against an otherwise featureless background, and its relative motion across and rising in the Cessna's windscreen could have been disorienting, especially if the pilot had fixated on it for any length of time. Maneuvering the airplane during this search would likely have compounded the pilot's resultant disorientation.
Probable cause:
The pilot's spatial disorientation, which resulted in loss of airplane control. Contributing to the accident was the night instrument meteorological conditions with variable cloud layers.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Reading: 1 killed

Date & Time: Sep 5, 2001 at 1313 LT
Operator:
Registration:
N8PK
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Reading – Montgomery
MSN:
31-8152141
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3230
Captain / Total hours on type:
20.00
Aircraft flight hours:
6204
Circumstances:
After takeoff, the pilot reported "an engine problem," but did not elaborate. A witness on the ground saw that the left engine was trailing smoke, but the engine was still operating, and did not sound like it was "missing". When asked by the tower controller if he required assistance, the pilot answered "no". The controller cleared the pilot for left traffic to a landing, and provided the current weather. There were no further transmissions from the pilot. Smoothed radar tracking data revealed that the airplane turned toward a left downwind, and leveled off at 1,400 feet msl (about 1,050 feet agl) and 156 knots. During the next 14 seconds, the airplane descended to 1,100 feet and increased airspeed to 173 knots. Then radar contact was lost. Witnesses observed the airplane variously in a right snap roll and a left wingover, followed by a sharp dive to the ground. The airplane had just undergone maintenance. During maintenance, unused oil was found in the left engine cowling, which the pilot admitted he had previously spilled. Following maintenance, the pilot was observed adding 3 additional quarts of oil to the left engine. The engine oil dipsticks were calibrated on both sides, with each side pertaining to the oil level in a specific engine. The side for the right engine was calibrated to read 1 3/4 quarts lower than the left engine. The airplane's wreckage was fragmented. No evidence of mechanical defect was found, nor was there any evidence of an extreme out-of-trim condition. There was also no evidence of engine failure, detonation, or pre-impact failure. The pilot held an airline transport pilot certificate. He reported 3,210 hours of flight time to the operator, and had recently been cleared to fly the airplane on 14 CFR Part 91 flights. The flight to the maintenance facility was the pilot's first solo flight in the airplane. An autopsy of the pilot revealed the presence of a prostate adenocarcinoma; however, according to his physician, the pilot was unaware of it.
Probable cause:
The pilot's loss of control for undetermined reasons, which resulted in a high speed dive to the ground.
Final Report:

Crash of a Piper PA-60 Aerostar (Ted Smith 600) in Montgomery

Date & Time: May 29, 1999 at 1724 LT
Registration:
N601JS
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Montgomery – Columbus
MSN:
60-0553-179
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5000
Captain / Total hours on type:
1000.00
Aircraft flight hours:
2322
Circumstances:
During the takeoff roll and initial climb both engines were producing normal power. As the airplane climbed through 150 feet, the left engine lost power. The pilot reported that he feathered the left propeller. He further stated that following the securing of the left engine, the right engine began to 'power down.' The pilot reported that he was unable to maintain a climb attitude and was forced to land on the airport in a grassy area. The subsequent examination of the cockpit disclosed that the left engine throttle was in the full forward position, and the right throttle lever was in the mid-range position. Both propeller levers were found full forward. The left engine mixture lever was in the full forward position, and the right mixture lever full aft, or lean, position. The functional check of both engines was conducted. Initially the left engine would not start, but after troubleshooting the fuel system, the left fuel boost pump was determined to have been defective. The 'loss of engine power after liftoff' checklist requires that the pilot identify the inoperative engine and to feather the propeller for the inoperative engine.
Probable cause:
The pilot's inadvertent shutdown of the wrong engine that resulted in the total loss of engine power. A factor was the loss of engine power due to fuel starvation when the left fuel boost pump failed.
Final Report:

Crash of a Mitsubishi MU-2B-20 Marquise in Batesville

Date & Time: Apr 7, 1996 at 1155 LT
Type of aircraft:
Registration:
N310MA
Flight Type:
Survivors:
Yes
Schedule:
Montgomery - Batesville
MSN:
167
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1400
Captain / Total hours on type:
89.00
Aircraft flight hours:
5400
Circumstances:
The pilot reported that loss of power occurred in both engines after he entered the traffic pattern for a full stop landing. The airplane collided with trees during an emergency landing in a cotton field near the airport. Subsequent review of the aircraft maintenance logs disclosed that Mitsubishi MU-2 Service Bulletin (SB) 130A had not been accomplished on this airplane. According to the manufacturer, an inadvertent failure or the improper installation of a filler cap after refueling may cause an air pressure differential between the center and outboard portions of the main integral fuel tank. Air leakage from the filler cap may result in failure of the fuel transfer system to move fuel from the outboard tank section to the center tank section. To eliminate this possible malfunction, the operator was to remove vent check valves from the bulkhead between the tanks in accordance with SB 130A. The operator's maintenance policies required that, company jet and turbo propeller aircraft be maintained under a maintenance program in accordance with FAR Parts 135.415, 135.417, 135.423, 135.443, and a corporate flight management approved aircraft inspection program (AAIP). The maintenance inspection program also included compliance with manufacturers' service bulletins and service letters.
Probable cause:
An anomaly in the fuel system that allowed a pressure differential to occur between the center and outer portions of the main integral fuel tank, which in turn resulted in fuel starvation of both engines. A factor relating to the accident was: failure of company maintenance personnel to remove fuel system vent check valves as recommended by Mitsubishi MU-2 Service Bulletin 130A.
Final Report:

Crash of a Dassault Falcon 20DC in Cartersville: 2 killed

Date & Time: Jun 29, 1989 at 0004 LT
Type of aircraft:
Operator:
Registration:
N125CA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Cartersville - Montgomery
MSN:
208
YOM:
1970
Flight number:
PHX125
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
7940
Captain / Total hours on type:
770.00
Aircraft flight hours:
13547
Circumstances:
The crew arrived at the airport about 20 minutes before the planned midnight takeoff time, after the pilot-in-command had spent the day moving furniture. A night watchman noted that the preflight inspection and takeoff roll to rotation/lift-off was normal. There was no post-takeoff radio call to either unicom or ATC, although the crew had filed an IFR flight plan. After taking off from runway 36, the aircraft crashed about 1.8 mile north of the runway. The wreckage was found after interruption of electrical power to a nearby city. Initial impact was with trees, while in a shallow/left/descending turn. An area of trees about 1/2 mile long was damaged by impact and fire. Before coming to rest, the aircraft hit a powerline support tower. There was evidence the aircraft was traveling at about 260 knots, when it crashed. No preimpact part failure or malfunction was found that would have resulted in the accident. Both pilots were killed.
Probable cause:
Failure of the pilot-in-command (pic) to assure that the aircraft maintained a climb profile after takeoff. Factors related to the accident were: dark night, the crew's lack of visual perception at night, the pic's lack of rest (fatigue), and the copilot's failure to attain remedial action.
Final Report:

Crash of a Piper PA-31T Cheyenne II in Utica: 2 killed

Date & Time: Feb 22, 1985 at 2000 LT
Type of aircraft:
Operator:
Registration:
N100RN
Survivors:
No
Schedule:
Montgomery - Utica
MSN:
31-7820091
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
11000
Captain / Total hours on type:
800.00
Aircraft flight hours:
1516
Circumstances:
The pilot attempted a VOR approach and missed. He advised ATC he was going to attempt the NDB and if he could not see the runway he would go to metro at Detroit or Pontiac. On the NDB approach the aircraft struck trees 960 feet below the MDA. The aircraft flipped over landing on the nose and top of the fuselage. Both occupants were killed.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: approach - faf/outer marker to threshold (ifr)
Findings
1. (f) in-flight planning/decision - not corrected - pilot in command
2. (f) ifr procedure - not followed - pilot in command
3. (f) judgment - poor - pilot in command
4. (c) minimum descent altitude - not used - pilot in command
5. (c) decision height - not maintained - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Cessna 421B Golden Eagle II in Cullman: 6 killed

Date & Time: Mar 5, 1984 at 1836 LT
Operator:
Registration:
N3291Q
Survivors:
No
Schedule:
Montgomery - Cullman
MSN:
421B-0911
YOM:
1975
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
3423
Captain / Total hours on type:
1599.00
Aircraft flight hours:
2478
Circumstances:
Pilot cleared for night NDB runway 19 approach to Folsom Field. Erratic radar track during procedure turn and inbound intercept. Witnesses described 200 feet ceiling and reduced visibility in fog at airport. Other witnesses observed aircraft on northbound course, followed by turn to west at rooftop height, well below MDA, at a point one mile northeast of airport. Engine operation sounded normal. Aircraft contacted trees at about airport elevation, one mile north of airport. Wreckage produced 632 feet path. Severed limbs, prop damage and engine examination revealed evidence of power at impact. 62 year old pilot had not flown with cfi in years, instrument currency unknown. Pilot found to have severe coronary atherosclerosis with near total occlusion of right coronary artery and evidence of past total occlusion of left circumflex coronary artery. Ceiling lower than forecast for area. Flight purpose to carry employees to meet truck, go job site. Limitation on pilot medical certificate, not for night flight. Sunset at 1745 cst, 51 minutes before accident. All six occupants were killed.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: approach - faf/outer marker to threshold (IFR)
Findings
1. (f) weather condition - low ceiling
2. (f) weather condition - fog
3. (f) light condition - dark night
4. (f) object - tree(s)
5. (c) IFR procedure - not followed - pilot in command
6. (c) visual/aural perception - pilot in command
7. (c) minimum descent altitude - not maintained - pilot in command
8. (c) lack of recent instrument time - pilot in command
9. (c) missed approach - not performed - pilot in command
10. (c) physical impairment - pilot in command
Final Report:

Crash of a Beechcraft 60 Duke near Jackson: 8 killed

Date & Time: Nov 6, 1978 at 2046 LT
Type of aircraft:
Registration:
N135D
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Montgomery - Tulsa
MSN:
P-7
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
2000
Captain / Total hours on type:
60.00
Circumstances:
The twin engine aircraft was completing a demo flight from Montgomery, Alabama, to Tulsa, Oklahoma, carrying seven passengers and a pilot. While cruising at an altitude of 14,000 feet in icing conditions, the pilot informed ATC about an engine failure and was cleared to divert to Jackson-Municipal Airport. On descent, the aircraft went out of control and crashed few miles from Jackson Airport. The aircraft was destroyed and all eight occupants were killed.
Probable cause:
Uncontrolled collision with ground on final approach due to powerplant failure for undetermined reasons. The following contributing factors were reported:
- Diverted attention from operation of aircraft,
- Improper in-flight decisions,
- Icing conditions including sleet, freezing rain,
- Fog,
- Complete failure on one engine,
- Weather briefing included freezing level 13,000 to 15,000 feet,
- Cruising altitude 14,000 feet.
Final Report:

Crash of a Cessna 402B in Tuscaloosa: 1 killed

Date & Time: Feb 1, 1978 at 2022 LT
Type of aircraft:
Operator:
Registration:
N8210Q
Flight Type:
Survivors:
Yes
Schedule:
Montgomery - Tuscaloosa
MSN:
402B-0390
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7000
Captain / Total hours on type:
1500.00
Circumstances:
On final approach to Tuscaloosa Airport by night, the pilot failed to realize his altitude was too low when the airplane struck trees and crashed few hundred yards short of runway 04 threshold. The pilot was seriously injured while the passenger was killed.
Probable cause:
Collision with trees and undershoot on final approach after the pilot misjudged distance and altitude. The following contributing factors were reported:
- Rain,
- Fog,
- High obstructions,
- Visibility 3 miles or less,
- Drizzle,
- Runway 04 also has sequential flasher and steady burner type approach lights.
Final Report:

Crash of a Beechcraft G18S in Troy: 1 killed

Date & Time: Mar 6, 1975 at 0350 LT
Type of aircraft:
Operator:
Registration:
N6614B
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Montgomery - Dothan
MSN:
BA-487
YOM:
1960
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1921
Captain / Total hours on type:
641.00
Circumstances:
While cruising by night under VFR mode, the pilot's attention diverted from operation and he failed to realize his altitude was too low when the airplane struck trees and crashed near Troy. The aircraft was destroyed and the pilot, sole on board, was killed.
Probable cause:
Collision with trees during normal cruise after the pilot diverted attention from operation of aircraft. The following contributing factors were reported:
- Misjudged altitude,
- Continued VFR flight into adverse weather conditions,
- Operated carelessly,
- Dense fog in area.
Final Report: