Crash of a McDonnell Douglas MD-88 in LaGuardia

Date & Time: Mar 5, 2015 at 1102 LT
Type of aircraft:
Operator:
Registration:
N909DL
Survivors:
Yes
Schedule:
Atlanta – New York
MSN:
49540/1395
YOM:
1987
Flight number:
DL1086
Crew on board:
5
Crew fatalities:
Pax on board:
125
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15200
Captain / Total hours on type:
11000.00
Copilot / Total flying hours:
11000
Copilot / Total hours on type:
3000
Aircraft flight hours:
71196
Aircraft flight cycles:
54865
Circumstances:
The aircraft was landing on runway 13 at LaGuardia Airport (LGA), New York, New York, when it departed the left side of the runway, contacted the airport perimeter fence, and came to rest with the airplane’s nose on an embankment next to Flushing Bay. The 2 pilots, 3 flight attendants, and 98 of the 127 passengers were not injured; the other 29 passengers received minor injuries. The airplane was substantially damaged. Flight 1086 was a regularly scheduled passenger flight from Hartsfield-Jackson Atlanta International Airport, Atlanta, Georgia, operating under the provisions of 14 Code of Federal Regulations Part 121. An instrument flight rules flight plan had been filed. Instrument meteorological conditions prevailed at the time of the accident. The captain and the first officer were highly experienced MD-88 pilots. The captain had accumulated about 11,000 hours, and the first officer had accumulated about 3,000 hours, on the MD-88/-90. In addition, the captain was previously based at LGA and had made many landings there in winter weather conditions. The flight crew was concerned about the available landing distance on runway 13 and, while en route to LGA, spent considerable time analyzing the airplane’s stopping performance. The flight crew also requested braking action reports about 45 and 35 minutes before landing, but none were available at those times because of runway snow clearing operations. The unavailability of braking actions reports and the uncertainty about the runway’s condition created some situational stress for the captain, who was the pilot flying. After runway 13 became available for arriving airplanes, the flight crews of two preceding airplanes (which landed on the runway about 16 and 8 minutes before the accident landing) reported good braking action on the runway, so the flight crew expected to see at least some of the runway’s surface after the airplane broke out of the clouds. However, the flight crew saw that the runway was covered with snow, which was inconsistent with their expectations based on the braking action reports and the snow clearing operations that had concluded less than 30 minutes before the airplane landed. The snowier-than-expected runway, along with its relatively short length and the presence of Flushing Bay directly off the departure end of the runway, most likely increased the captain’s concerns about his ability to stop the airplane within the available runway distance, which exacerbated his situational stress. The captain made a relatively aggressive reverse thrust input almost immediately after touchdown. Reverse thrust is one of the methods that pilots use to decelerate the airplane during the landing roll. Reverse thrust settings are expressed as engine pressure ratio (EPR) values, which are measurements of engine power (the ratio of the pressure of the gases at the exhaust compared with the pressure of the air entering the inlet). Both pilots were aware that 1.3 EPR was the target setting for contaminated runways.As reverse thrust EPR was rapidly increasing, the captain’s attention was focused on other aspects of the landing, which included steering the airplane to counteract a slide to the left and ensuring that the spoilers had deployed (a necessary action for the autobrakes to engage). The maximum EPR values reached during the landing were 2.07 on the left engine and 1.91 on the right engine, which were much higher than the target setting of 1.3 EPR. These high EPR values likely resulted from a combination of the captain’s stress; his relatively aggressive reverse thrust input; and operational distractions, including the airplane’s continued slide to the left despite the captain’s efforts to steer it away from the snowbanks alongside the runway. All of these factors reduced the captain’s monitoring of EPR indications. The high EPR values caused rudder blanking (which occurs on MD-80 series airplanes when smooth airflow over the rudder is disrupted by high reverse thrust) and a subsequent loss of aerodynamic directional control. Although the captain stowed the thrust reversers and applied substantial right rudder, right nosewheel steering, and right manual braking, the airplane’s departure from the left side of the runway could not be avoided because directional control was regained too late to be effective.
Probable cause:
The National Transportation Safety Board determines that the probable cause of this accident was the captain’s inability to maintain directional control of the airplane due to his application of excessive reverse thrust, which degraded the effectiveness of the rudder in controlling the airplane’s heading. Contributing to the accident were the captain’s:
- situational stress resulting from his concern about stopping performance and
- attentional limitations due to the high workload during the landing, which prevented him from immediately recognizing the use of excessive reverse thrust.
Final Report:

Crash of a Piper PA-46-500TP Malibu Meridian in White Plains: 1 killed

Date & Time: Jun 13, 2014 at 0808 LT
Registration:
N5335R
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
White Plains - Portland
MSN:
46-97100
YOM:
2001
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5100
Captain / Total hours on type:
134.00
Aircraft flight hours:
1931
Circumstances:
The pilot arrived at the fixed-base operator on the morning of the accident and requested that his airplane be brought outside and prepared for an immediate departure; this occurred 1 hour 15 minutes before his scheduled departure time. Radar data showed that the airplane departed 23 minutes later. According to air traffic control data, shortly thereafter, the ground and departure controllers contacted the tower controller and asked if the airplane had departed yet; the tower controller responded, "I have no idea. We have zero visibility." Weather conditions about the time of the accident included a 200-ft overcast ceiling with about 1/4-mile visibility. Only five radar targets identified as the accident airplane were captured, and all of the targets were located over airport property. The first three radar targets began about midpoint of the 6,500-ft-long runway, and each of these targets was at an altitude of about 60 ft above ground level (agl). The final two targets showed the airplane in a shallow right turn, consistent with the published departure procedure track, at altitudes of 161 and 261 ft agl, respectively. The final radar target was about 1/2 mile from the accident site. Witnesses reported observing the airplane impact trees in a wings-level, slightly right-wing-down attitude at high speed. Examination of the wreckage revealed no preimpact mechanical malfunctions or anomalies of the airplane. The pilot's personal assistant reported that the pilot had an important meeting that required his attendance on the day of the accident flight. His early arrival to the airport and his request to have the airplane prepared for an immediate departure were actions consistent with self-induced pressure to complete the flight. Due to the poor weather conditions, which were expected to continue or worsen, he likely felt pressure to expedite his departure to ensure he was able to make it to his destination and to attend the meeting. This pressure may have further affected his ability to discern the risk associated with departing in low-visibility and low-ceiling conditions. As noted, the weather conditions were so poor that the local air traffic controller stated that he could not tell whether the airplane had departed. Such weather conditions are highly conducive to the development of spatial disorientation. Further, the altitude profile depicted by the radar data and the airplane's near wings-level attitude and high speed at impact were consistent with the pilot experiencing a form of spatial disorientation known as "somatogravic illusion," in which the pilot errantly perceives the airplane's acceleration as increasing pitch attitude, and efforts to hold the nose down or arrest the perception of increasing pitch attitude can exacerbate the situation. Such an illusion can be especially difficult to overcome because it typically occurs at low altitudes after takeoff, which provides little time for recognition and subsequent corrective inputs, particularly in very low-visibility conditions.
Probable cause:
The pilot's failure to maintain a positive climb rate after takeoff due to spatial disorientation (somatogravic illusion). Contributing to the accident was the pilot's self-induced pressure to depart and his decision to depart in low-ceiling and low-visibility conditions.
Final Report:

Crash of a Boeing 737-7H4 in New York

Date & Time: Jul 22, 2013 at 1744 LT
Type of aircraft:
Operator:
Registration:
N753SW
Survivors:
Yes
Schedule:
Nashville – New York
MSN:
29848/400
YOM:
1999
Flight number:
WN345
Crew on board:
5
Crew fatalities:
Pax on board:
145
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12522
Captain / Total hours on type:
7909.00
Copilot / Total flying hours:
5200
Copilot / Total hours on type:
1100
Aircraft flight hours:
49536
Circumstances:
As the airplane was on final approach, the captain, who was the pilot monitoring (PM), realized that the flaps were not configured as had been briefed, with a setting of 40 degrees for the landing. Data from the flight data recorder (FDR) indicate that the captain set the flaps to 40 degrees as the airplane was descending through about 500 ft altitude, which was about 51 seconds from touchdown. When the airplane was between 100 to 200 ft altitude, it was above the glideslope. Concerned that the airplane was too high, the captain exclaimed repeatedly "get down" to the first officer about 9 seconds from touchdown. About 3 seconds from touchdown when the airplane was about 27 ft altitude, the captain announced "I got it," indicating that she was taking control of the airplane, and the first officer replied, "ok, you got it." According to FDR data, after the captain took control, the control column was relaxed to a neutral position and the throttles were not advanced until about 1 second before touchdown. The airplane touched down at a descent rate of 960 ft per minute and a nose-down pitch attitude of -3.1 degrees, resulting in the nose gear contacting the runway first and a hard landing. The airplane came to a stop on the right side of the runway centerline about 2,500 ft from its initial touchdown. The operator's stabilized approach criteria require an immediate go-around if the airplane flaps or landing gear were not in the final landing configuration by 1,000 ft above the touchdown zone; in this case, the flaps were not correctly configured until the airplane was passing through 500 ft. Further, the airplane's deviation about the glideslope at 100 to 200 ft would have been another opportunity for the captain, as the PM at this point during the flight, to call for a go-around, as indicated in the Southwest Airlines Flight Operations Manual (FOM). Accident data suggest that pilots often fail to perform a go-around or missed approach when stabilized approach criteria are not met. A review of NTSB investigated accidents by human factors researchers found that about 75% of accidents were the result of plan continuation errors in which the crew continued an approach despite cues that suggested it should not be continued. Additionally, line operations safety audit data presented at the International Air Safety Summit in 2011 suggested that 97% of unstabilized approaches were continued to landing even though doing so was in violation of companies' standard operating procedures (SOPs). The Southwest FOM also states that the captain can take control of the airplane for safety reasons; however, the captain's decision to take control of the airplane at 27 ft above the ground did not allow her adequate time to correct the airplane's deteriorating energy state and prevent the nose landing gear from striking the runway. The late transfer of control resulted in neither pilot being able to effectively monitor the airplane's altitude and attitude. The first officer reported that, after the captain took control of the airplane, he scanned the altimeter and airspeed to gain situational awareness but that he became distracted by the runway "rushing" up to them and "there was no time to say anything." The captain should have called for a go-around when it was apparent that the approach was unstabilized well before the point that she attempted to salvage the landing by taking control of the airplane at a very low altitude. In addition, the captain did not follow SOPs at several points during the flight. As PM, she should have made the standard callout per the Southwest FOM when the airplane was above glideslope, stating "glideslope" and adding a descriptive word or words to the callout (for example, "one dot high"). Rather than make this callout, however, the captain repeatedly said "get down" to the first officer before stating "I got it." The way she handled the transfer of airplane control was also contrary to the FOM, which indicates that the PM should say "I have the aircraft." The flight crew's performance was indicative of poor crew resource management.
Probable cause:
The captain's attempt to recover from an unstabilized approach by transferring airplane control at low altitude instead of performing a go-around. Contributing to the accident was the captain's failure to comply with standard operating procedures.
Final Report:

Crash of a Grumman G-44 Widgeon in Catskill: 1 killed

Date & Time: May 2, 2013 at 1629 LT
Type of aircraft:
Registration:
N8AS
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Copake - Copake
MSN:
1315
YOM:
1943
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5735
Captain / Total hours on type:
411.00
Aircraft flight hours:
2251
Circumstances:
Michael B. Braunstein, aged 72, was the owner of this vintage aircraft built in 1943 and was performing a local flight within the State of New York. Aircraft was destroyed when it impacted the waters of the Hudson River, near Catskill, New York. The certificated airline transport pilot was fatally injured. Visual meteorological conditions prevailed, and no flight plan had been filed for the local personal flight conducted under Title 14 Code of Federal Regulations Part 91, which departed from B Flat Farm Airport (3NK8), Copake, New York about 1600. Approximately 25 witnesses were interviewed. Witnesses reported observing the twin-engine amphibious airplane flying southbound low above a river and hearing the engine running. The airplane then made a 180-degree left turn, which was consistent with the pilot flying a tight traffic pattern before attempting a water landing. The airplane then descended, leveled off above the water, and suddenly banked left. The airplane’s nose and left pontoon then struck the water, and the airplane nosed over, caught fire, and sank. Postrecovery examination of the wreckage revealed that the landing gear was in the “up” position and that the flaps were extended, which indicates that the airplane had been configured for a water landing. No evidence of any preimpact failures or malfunctions of the airplane or engines was found that would have precluded normal operation. At the time of the accident, a light breeze was blowing, the river was at slack tide, and the water conditions were calm, all of which were conducive to glassy water conditions. It is likely that the glassy water conditions adversely affected the pilot’s depth perception and led to his inability to correctly judge the airplane’s height above the water. He subsequently flared the airplane too high, which resulted in the airplane exceeding its critical angle-of-attack, entering an aerodynamic stall, and impacting the water in a nose-low attitude.
Probable cause:
The pilot’s misjudgment of the airplane’s altitude above the water and early flare for a landing on water with a glassy condition, which led to the airplane exceeding its critical angle-of-attack and experiencing an aerodynamic stall.
Final Report:

Crash of a De Havilland Dash-8-Q402 in Buffalo: 50 killed

Date & Time: Feb 12, 2009 at 2217 LT
Operator:
Registration:
N200WQ
Survivors:
No
Site:
Schedule:
Newark - Buffalo
MSN:
4200
YOM:
2008
Flight number:
CO3407
Crew on board:
4
Crew fatalities:
Pax on board:
45
Pax fatalities:
Other fatalities:
Total fatalities:
50
Captain / Total flying hours:
3379
Captain / Total hours on type:
111.00
Copilot / Total flying hours:
2244
Copilot / Total hours on type:
774
Aircraft flight hours:
1819
Aircraft flight cycles:
1809
Circumstances:
On February 12, 2009, about 2217 eastern standard time, a Colgan Air, Inc., Bombardier DHC-8-400, N200WQ, operating as Continental Connection flight 3407, was on an instrument approach to Buffalo-Niagara International Airport, Buffalo, New York, when it crashed into a residence in Clarence Center, New York, about 5 nautical miles northeast of the airport. The 2 pilots, 2 flight attendants, and 45 passengers aboard the airplane were killed, one person on the ground was killed, and the airplane was destroyed by impact forces and a post crash fire. The flight was operating under the provisions of 14 Code of Federal Regulations Part 121. Night visual meteorological conditions prevailed at the time of the accident.
Probable cause:
The captain’s inappropriate response to the activation of the stick shaker, which led to an aerodynamic stall from which the airplane did not recover.
Contributing to the accident were:
1) The flight crew’s failure to monitor airspeed in relation to the rising position of the low speed cue,
2) The flight crew’s failure to adhere to sterile cockpit procedures,
3) The captain’s failure to effectively manage the flight,
4) Colgan Air’s inadequate procedures for airspeed selection and management during approaches in icing conditions.
Final Report:

Crash of an Airbus A320-214 in New York

Date & Time: Jan 15, 2009 at 1531 LT
Type of aircraft:
Operator:
Registration:
N106US
Flight Phase:
Survivors:
Yes
Schedule:
New York - Charlotte
MSN:
1044
YOM:
1999
Flight number:
US1549
Crew on board:
5
Crew fatalities:
Pax on board:
150
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
19663
Captain / Total hours on type:
4765.00
Copilot / Total flying hours:
15643
Copilot / Total hours on type:
37
Aircraft flight hours:
25241
Aircraft flight cycles:
16299
Circumstances:
Aircraft experienced an almost complete loss of thrust in both engines after encountering a flock of birds and was subsequently ditched on the Hudson River about 8.5 miles from La Guardia Airport (LGA), New York City, New York. The flight was en route to Charlotte Douglas International Airport, Charlotte, North Carolina, and had departed LGA about 2 minutes before the in-flight event occurred. The 150 passengers, including a lap held child, and 5 crew members evacuated the airplane via the forward and overwing exits. One flight attendant and four passengers were seriously injured, and the airplane was substantially damaged.
Probable cause:
The ingestion of large birds into each engine, which resulted in an almost total loss of thrust in both engines and the subsequent ditching on the Hudson River. Contributing to the fuselage damage and resulting unavailability of the aft slide/rafts were:
-the Federal Aviation Administration’s approval of ditching certification without determining whether pilots could attain the ditching parameters without engine thrust,
-the lack of industry flight crew training and guidance on ditching techniques,
-the captain’s resulting difficulty maintaining his intended airspeed on final approach due to the task saturation resulting from the emergency situation.
Contributing to the survivability of the accident was:
-the decision-making of the flight crew members and their crew resource management during the accident sequence,
-the fortuitous use of an airplane that was equipped for an extended overwater flight, including the availability of the forward slide/rafts, even though it was not required to be so equipped
-the performance of the cabin crew members while expediting the evacuation of the airplane,
-the proximity of the emergency responders to the accident site and their immediate and appropriate response to the accident.
Final Report:

Crash of a Dassault Falcon 20C in Jamestown

Date & Time: Dec 21, 2008 at 0100 LT
Type of aircraft:
Operator:
Registration:
N165TW
Flight Type:
Survivors:
Yes
Schedule:
Tulsa – Jamestown
MSN:
65
YOM:
1966
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3028
Captain / Total hours on type:
1160.00
Copilot / Total flying hours:
2086
Copilot / Total hours on type:
80
Aircraft flight hours:
16360
Circumstances:
The co-pilot was performing a nighttime approach and landing to runway 25. No runway condition reports were received by the flight crew while airborne, and a NOTAM was in effect, stating, “thin loose snow over patchy thin ice.” After landing, the co-pilot called out that the airplane was sliding and the wheel brakes were ineffective. The captain took the controls, activated the air brakes, and instructed the co-pilot to deploy the drag chute. The crew could not stop the airplane in the remaining runway distance and the airplane overran the runway by approximately 100 feet. After departing the runway end, the landing gear contacted a snow berm that was the result of earlier plowing. The captain turned the airplane around and taxied to the ramp. Subsequent inspection of the airplane revealed a fractured nose gear strut and buckling of the fuselage. The spring-loaded drag chute extractor cap activated, but the parachute remained in its tail cone container. Both flight crewmembers reported that the runway was icy at the time of the accident and braking action was “nil.” The airport manager reported that when the airplane landed, no airport staff were on duty and had not been for several hours. He also reported that when the airport staff left for the evening, the runway conditions were adequate. The runway had been plowed and sanded approximately 20 hours prior to the accident, sanded two more times during the day, and no measurable precipitation was recorded within that time frame. The reason that the drag chute failed to deploy was not determined.
Probable cause:
The inability to stop the airplane on the remaining runway because of icy runway conditions. A factor was the failure of the drag chute to properly deploy.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) near Penn Yan

Date & Time: Oct 28, 2007 at 1330 LT
Operator:
Registration:
N717SB
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Rochester – Danbury
MSN:
61-0808-8063418
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2413
Captain / Total hours on type:
1683.00
Aircraft flight hours:
2619
Circumstances:
The private pilot was continuing a cross-country flight after having stopped for fuel. About 20 minutes into the flight, the pilot said both engines started running rough, and he turned the airplane toward the nearest airport and descended. The pilot reported that he did not think the airplane would make it to the airport, and that due to the rugged terrain, he felt it was better to ditch the airplane in a large lake he was flying over. The pilot reported there were no mechanical anomalies prior to the loss of engine power. He said he felt that fuel contamination was the cause of the engine problem, and that not fueling during heavy rain might have prevented the problem. Fuel samples were taken from the fuel supply where he added fuel, and the equipment used to fuel the airplane. No other instances of fuel contamination were reported, and according to the FAA inspector the fuel samples were tested, and found to be clean. The airplane was not recovered from the lake, and has not been examined by the NTSB.
Probable cause:
The loss of engine power during cruise flight for an undetermined reason.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) in Jamestown: 1 killed

Date & Time: Jan 8, 2007 at 0950 LT
Operator:
Registration:
N720Z
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Jamestown – Buffalo
MSN:
61-0592-7963262
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5531
Captain / Total hours on type:
753.00
Aircraft flight hours:
2783
Circumstances:
During the initial climb, a "throbbing or surging" sound was heard as the airplane departed in gusting wind conditions with a 600-foot ceiling and 1/2 mile visibility in snow. Moments later the airplane came "straight down" and impacted the ground. During examination of the wreckage, it was discovered that that the fuel selector switch for the right engine had been in the "X-FEED" position during the accident. Examination of documents discovered in the wreckage revealed, three documents pertaining to operation of an Aerostar. These documents consisted of two airplane flight manuals (AFMs) from two different manufacturers, and a checklist. Examination of the first of the AFMs revealed, that it had the name of both the pilot and the operator on the cover of the document. Further examination revealed that it had been published 4 years prior to the manufacture of the accident airplane, and contained information for a Ted Smith Aerostar Model 601P, which the operator had previously owned. This document contained no warnings regarding the use of the crossfeed system during takeoff. Examination of the second of the two AFMs found in the wreckage revealed that it was the Federal Aviation Administration (FAA) approved AFM for the accident airplane. Unlike the first AFM, the second AFM advised that the fuel selector "X-FEED" position should be used in "level coordinated flight only." It also advised that each engine fuel selector "must be in the ON position for takeoff, climb, descent, approach, and landing." It also warned that, if the airplane was not in a level coordinated flight attitude, "engine power interruptions may occur on one or both engines" when "X-FEED" is selected "due to unporting of the respective engine's fuel supply intake port." Review of the checklist contained in the FAA approved AFM for the Piper Aircraft Model 601P under "STARTING ENGINES," required a check of the crossfeed system prior to engine start by selecting each fuel selector to "ON," then selecting "X-FEED," and after verifying valve actuation and annunciator light illumination, returning the fuel selector to "ON." Additionally, under "BEFORE TAKEOFF" It also required that the fuel selectors be checked in the "ON" position, and that the "X-FEED" annunciator light was out, prior to takeoff. Examination of the pilot's checklist revealed that, it consisted of multiple pages inserted into plastic protective sleeves and included both typed, and hand written information. A review of the section titled "BEFORE TAKEOFF" revealed that the checklist item "Fuel Selectors - ON Position," which was listed in the AFM, had been omitted.
Probable cause:
The pilot's incorrect selection of the right engine fuel selector position, which resulted in fuel starvation of the right engine, a loss of the right engine's power, and a loss of control during initial climb. Contributing to the accident were the pilot's inadequate preflight planning and preparation, and his improper use of the manufacturer's published normal operating procedures.
Final Report:

Crash of a Cessna 411 in East Hampton: 1 killed

Date & Time: Oct 23, 2005 at 1345 LT
Type of aircraft:
Registration:
N7345U
Flight Type:
Survivors:
No
Site:
Schedule:
Jefferson - Nantucket
MSN:
411-0045
YOM:
1965
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
452
Captain / Total hours on type:
0.00
Aircraft flight hours:
2808
Circumstances:
The pilot purchased the multiengine airplane about 18 months prior to the accident, and was conducting his first flight in the airplane, as he flew it from Georgia to Massachusetts. While en route, the airplane experienced a failure of the left engine. The airplane began maneuvering near an airport, as its groundspeed decreased from 173 miles per hour (mph) to 90 mph, 13 mph below the minimum single engine control speed. A witness reported that the airplane appeared to be attempting to land, when it banked to the left, and descended to the ground. The airplane impacted on a road, about 3 miles east-southeast of the airport. A 3-inch, by 2.5- inch hole was observed on the top of the left engine crankcase, and streaks of oil were present on the left gear door, left flap, and the left side of the fuselage. The number two connecting rod was fractured and heat distressed. The number 2 piston assembly was seized in the cylinder barrel. The airplane had been operated about 30 hours, during the 6 years prior to the accident, and it had not been flown since its most recent annual inspection, which was performed about 16 months prior to the accident. In addition, both engines were being operated beyond the manufacturer's recommended time between overhaul limits. The pilot did not possess a multiengine airplane rating. He attended an airplane type specific training course about 20 months prior to the accident. At that time, he reported 452 hours of total flight experience, with 0 hours of multiengine flight experience.
Probable cause:
The pilot's failure to maintain airspeed, while maneuvering with the left engine inoperative. Contributing to the accident were the failure of the left engine, and the pilot's lack of multiengine certification.
Final Report: