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Crash of a Rockwell Aero Commander 560F in Venice: 1 killed

Date & Time: Dec 26, 2011 at 1406 LT
Operator:
Registration:
N560WM
Flight Type:
Survivors:
No
Schedule:
Venice - LaFayette
MSN:
560-1305-58
YOM:
1964
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6000
Captain / Total hours on type:
1500.00
Aircraft flight hours:
5826
Circumstances:
The airplane departed and was climbing to an assigned altitude when the pilot informed an air traffic controller of a loss of engine power on the left engine. The pilot received radar vectors back to the departure airport and reported the airport in sight. There was no further communication with the controller. Review of radar data revealed that the airplane was about 825 feet from and 200 feet above the landing runway threshold. Seventeen seconds later, the airplane was at 100 feet above ground level and left of the intended landing runway. The last radar return was 5 seconds later, and the airplane was at 200 feet above ground level. A witness observed the airplane in the vicinity of landing runway. The airplane pitched straight up, stalled, spun to the left three times before it collided with the ground and caught fire. Postcrash examination of the airframe and flight controls revealed no anomalies. The left engine was disassembled and all connecting rods were intact except for the No.2 connecting rod. Metallugical examination of the connecting rod revealed that the bearing failed, most likely due to a progressive delamination of the bearing. Review of the airplane flight manual revealed a minimum of 300 feet of altitude is required to recover from power-off stalls with 7500 pounds at both forward and aft center of gravity. The stall speed with the landing gear and flaps up with 0 degree angle of bank is 83 miles per hour or 72 knots. The stall speed with the landing gear extended and the flaps down is 73 miles per hours or 63 knots.
Probable cause:
The pilot’s failure to maintain adequate airspeed during a single-engine approach, which resulted in an aerodynamic stall. Contributing to the accident was the total loss of power in the left engine due to a failed No. 2 connecting rod bearing.
Final Report:

Crash of a Beechcraft E18S in Venice

Date & Time: Jun 26, 2002 at 0800 LT
Type of aircraft:
Registration:
N1002C
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Venice - Cancún
MSN:
BA-251
YOM:
1957
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1750
Captain / Total hours on type:
250.00
Aircraft flight hours:
10500
Circumstances:
An airplane impacted the runway shortly after takeoff. According to the pilot, the airplane rolled sharply to the left immediately after liftoff from the runway. The passenger in the back seat stated the airplane banked sharply to the left after takeoff. The pilot then applied right rudder and aileron to stop the roll. Unable to level the airplane with the horizon, the pilot elected to reduce power to idle on both engines and land on the remaining runway. The airplane impacted the runway, slid into the grass and erupted into flames.
Probable cause:
The pilot's improper use of flight controls during takeoff, that resulted in the loss of control during takeoff.
Final Report:

Crash of a Cessna 411 in Venetie: 1 killed

Date & Time: Jan 27, 1988 at 0947 LT
Type of aircraft:
Registration:
N235UV
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Venice - West Palm Beach
MSN:
411-0052
YOM:
1965
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1500
Circumstances:
Witnesses stated that the aircraft was climbing and just after takeoff, the left wing dropped, the aircraft then leveled off, climbed approximately 75 more feet. The aircraft then abruptly turned hard left and went straight in, striking a wall surrounding a swimming pool, burst into flames and was consumed by post crash fire. Examination of the left engine revealed evidence that suggests that water was ingested into the cylinders prior to impact. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of engine power (partial) - nonmechanical
Phase of operation: takeoff - initial climb
Findings
1. (c) 1 engine - failure, partial
2. (f) propeller feathering - not performed - pilot in command
3. (c) fluid, fuel - water
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Occurrence #2: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
4. (c) airspeed (vmc) - not maintained - pilot in command
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Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report: