Crash of a Cessna 421C Golden Eagle III in Palm Beach County: 1 killed

Date & Time: Dec 8, 2012 at 1334 LT
Operator:
Registration:
N297DB
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Palm Beach County - Kendall
MSN:
421C-0826
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1219
Captain / Total hours on type:
100.00
Aircraft flight hours:
7040
Circumstances:
On December 8, 2012, at 1334 eastern standard time, a Cessna 421C, N297DB, operated by a private individual, was destroyed when it collided with trees and terrain following a loss of control after takeoff from North Palm Beach County Airpark (LNA), Lantana, Florida. The commercial pilot was fatally injured. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight, which was conducted under the provisions of Title 14 Code of Federal Regulations Part 91. The pilot took delivery of the airplane from a maintenance facility that had just completed an annual inspection and repainting of the airplane. According to the owner of the facility, who was a certificated pilot and an airframe and powerplant mechanic, the pilot completed the preflight inspection and the airplane was towed outside. The pilot started the airplane, but then shutdown to resolve an alternator charging light. Afterwards, the pilot stated that he planned to fly to Okeechobee, Florida, complete a few landings, and then continue to Miami. According to the mechanic, the pilot performed a ground run of the airplane for several minutes before taxiing to the approach end of Runway 3 for takeoff. The airplane lifted off about halfway down the runway and climbed at a "normal" rate. The mechanic then observed the airplane suddenly yaw to the left "for a second or two" and the airplane's nose continued to pitch up before rolling left and descending vertically, nose-down, until it disappeared from view. Several witnesses provided similar accounts to a Federal Aviation Administration (FAA) inspector and the local sheriff's department. One witness, a certificated flight instructor said, "The airplane just kept pitching up, and then it looked like a VMC roll."
Probable cause:
The pilot's failure to follow established engine-out procedures and to maintain a proper airspeed after the total loss of engine power on one of the airplane’s two engines during the initial climb. Contributing to the accident was the total loss of engine power due to a loss of torque on the crankcase bolts for reasons that could not be determined because of impact- and fire-related damage to the engine.
Final Report:

Crash of a Cessna 402B in Ocean Ridge

Date & Time: Jul 22, 2008 at 1350 LT
Type of aircraft:
Registration:
N3990C
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Lantana - Pompano Beach
MSN:
402B-0857
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1565
Aircraft flight hours:
7222
Circumstances:
The commercial pilot, who was also the former owner of the twin-engine airplane, stated that the purpose of the flight was to reposition the airplane to an airport approximately 22 miles south of the departure airport. Just prior to the flight, he purchased 10 gallons of fuel for each of the two main tanks. The pilot reported that about 5 minutes after takeoff, at an altitude of approximately 1,000 feet, he experienced a "loss of engine power." However, his three separate accounts of the event were inconsistent with respect to which engine had a problem, or the specific nature of the problem. The pilot reported that the airplane started to lose altitude "rapidly," and that he attempted to "wag the wings" in order to "get all the fuel to be useable." The airplane struck a building and terrain approximately 8 miles south of the departure airport. The pilot sustained serious injuries, but there was no fire. Damage to the left engine and propeller was consistent with the engine running at impact, and precluded an attempt to run the left engine in a test cell. Damage to the right engine and propeller was consistent with low or no power at impact. The right engine was subsequently successfully run in a test cell. No evidence of any pre-accident anomalies that could have contributed to the accident was noted with the airframe, engines, or propellers. The fuel selector valve placards did not accurately depict the fuel system configuration. The fuel quantity and its distribution in the tanks, either at the beginning of the flight or at the time of the accident, could not be determined.
Probable cause:
A partial loss of engine power due to fuel starvation. Contributing to the accident was the pilot’s decision to add only a limited amount of fuel prior to the flight, and the fuel selector valve placards' inaccurate depiction of the airplane fuel tank configuration.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 200 in Palm Beach

Date & Time: Apr 5, 1999 at 0945 LT
Operator:
Registration:
N838MA
Survivors:
Yes
Schedule:
Palm Beach - Kissimmee
MSN:
188
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8000
Captain / Total hours on type:
200.00
Aircraft flight hours:
16659
Circumstances:
The pilot reported that prior to takeoff, he completed a preflight inspection of the airplane that included checking the engine oil quantity. The line personnel topped off the oil reservoirs, and reportedly secured the engine oil reservoir filler caps. Approximately two minutes into the flight, the right engine oil pressure warning light illuminated. The pilot informed Palm Beach Approach Control of the engine oil pressure problem, shut down the right engine, and returned to Lantana. As the flight approached runway 03, the pilot heard a radio transmission from another airplane taxiing for takeoff. As the pilot continued the approach, with full flaps extended, he elected to go-around 1500 feet from the approach end of the 3000-foot runway. The airplane collided with the ground during the go-around maneuver to runway 15. The wreckage examination also disclosed that the right cowling showed oil streaming back from behind the engine and onto the wing strut. Inspection of the oil filler cap revealed that it had not been properly installed.
Probable cause:
The pilot's failure to secure the engine oil filler cap during the preflight inspection that resulted the subsequent loss of engine power, and his in-flight decision to attempt a single engine go-around with full wing flaps extended.
Final Report:

Crash of a Piper PA-31-325 Navajo C/R in Palm Beach: 2 killed

Date & Time: Jun 24, 1994 at 0905 LT
Type of aircraft:
Registration:
N27872
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Palm Beach - Palm Beach
MSN:
31-7912031
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1000
Captain / Total hours on type:
3.00
Circumstances:
The airplane was observed to rotate about 3,217 feet down the 3,746-feet runway. One or both engines were heard running rough. The airplane climbed to about 300 feet agl, banked left, pitched nose down and impacted the ground. During the investigation, the left engine operated to full rated rpm after replacement of the damaged ignition harness, adjustment of the turbocharger density controller, and adjustment of the magneto-to-engine timing. The right engine also operated normally after replacement of the magneto, ignition harness, and engine-driven fuel pump. The density controller required adjustment to obtain full rated rpm. The #3 cylinder fuel injector nozzle was also partially blocked by contaminant. The right engine magneto contact assemblies operationally checked ok. The capacitors were heat damaged. Right engine magneto-to-engine timing and internal timing of the magneto were not determined. Pilot's toxicological results were positive for butalbital (1.768 ug/ml blood, 0.553 ug/ml urine), and also positive for acetaminophen and salicylate (aspirin) in urine. Butalbital is a prescription medication (barbiturate) not approved for flying. Both occupants were killed.
Probable cause:
The pilot's impairment of judgment and performance due to drugs, his failure to abort the takeoff after experiencing reduced takeoff performance, and his failure to maintain minimum control speed. Factors in the accident were: a partial loss of engine power due to improper magneto-to-engine timing, and a partially blocked fuel nozzle.
Final Report:

Crash of a Cessna 402 in Lantana: 1 killed

Date & Time: Jan 11, 1992 at 1147 LT
Type of aircraft:
Operator:
Registration:
N3767C
Flight Type:
Survivors:
No
Schedule:
Lantana - Jacksonville
MSN:
402B-0617
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10400
Captain / Total hours on type:
300.00
Aircraft flight hours:
5501
Circumstances:
Flight departed and upon reaching a point approx 35 miles north of airport pilot requested return to airport from ATC. Pilot did not declare emergency or report an engine problem. Upon entering traffic pattern at uncontrolled airport pilot stated he would follow a Cessna 152 for landing. On short final aircraft was seen making s turns to maintain spacing behind 152. Pilot then declared he had an engine shutdown and needed to land. 152 was in landing flare and landed. With 152 on runway pilot attempted a go around with full flaps extended, gear down, left engine shutdown, and at a slow airspeed. Aircraft rolled to left upon application of right engine power and nosed down from which it crashed. The number two cylinder of the left engine had suffered separation of the head from the barrel. Pilot logbook did not reflect pilot having current biennial flight review. The pilot, sole on board, was killed.
Probable cause:
The pilot in commands failure to maintain airspeed above single engine minimum control speed resulting in an inflight loss of control and collision with terrain. Contributing to the accident was the pilot in command's failure to declare an emergency and request priority landing and his decision to follow a slower aircraft in the pattern.
Final Report:

Crash of a Rockwell Aero Commander 520 off Great Inagua: 2 killed

Date & Time: Nov 21, 1980
Operator:
Registration:
N515E
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Lantana - Great Inagua Island
MSN:
520-71
YOM:
1953
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The twin engine airplane crashed in unknown circumstances into the sea off Great Inagua Island. SAR operations were initiated but the wreckage nor both occupants were recovered.
Probable cause:
Due to lack of evidences, the exact cause of the accident could not be determined.
Final Report:

Crash of a Douglas C-47A-65-DL in Palm Beach

Date & Time: Apr 4, 1947
Registration:
N52710
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
19095
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Just after rotation, the right engine failed. As the crew failed to feather the propeller, the aircraft stalled and crashed into a lake near the airport. Both occupants were rescued while the aircraft sank and was lost.
Probable cause:
Failure of the right engine.