Crash of a Cessna 208B Super Cargomaster in Pellston: 1 killed

Date & Time: Jan 15, 2013 at 1958 LT
Type of aircraft:
Operator:
Registration:
N1120N
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pellston - Lansing
MSN:
208B-0386
YOM:
1994
Flight number:
MRA605
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1921
Captain / Total hours on type:
34.00
Aircraft flight hours:
10132
Circumstances:
The pilot landed at the airport to refuel the airplane and pick up cargo. The pilot spoke with three employees of the fixed base operator who stated that he seemed alert and awake but wanted to make a "quick turn." After the airplane was fueled and the cargo was loaded, the pilot departed; the airplane crashed 1 minute later. Night visual meteorological conditions prevailed at the time. An aircraft performance GPS and simulation study indicated that the airplane entered a right bank almost immediately after takeoff and then made a 42 degree right turn and that it was accelerating throughout the flight, from about 75 knots groundspeed shortly after liftoff to about 145 knots groundspeed at impact. The airplane was climbing about 500 to 700 feet per minute to a peak altitude of about 260 feet above the ground before descending. The simulation showed a gas generator speed of about 93 percent throughout the flight. The study indicated that the load factor vectors, which were the forces felt by the pilot, could have produced a somatogravic illusion of a climb, even while the airplane was descending. The postaccident examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. Based on the findings from the aircraft performance GPS and simulation study, the degraded visual reference conditions present about the time of the accident, and the forces felt by the pilot, it is likely that he experienced spatial disorientation, which led to his inadvertent controlled descent into terrain.
Probable cause:
The pilot's inadvertent controlled descent into terrain due to spatial disorientation. Contributing to the accident was lack of visual reference due to night conditions.
Final Report:

Crash of a Cessna 404 Titan II in Lansing

Date & Time: Apr 15, 2000 at 0743 LT
Type of aircraft:
Operator:
Registration:
N26SA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lansing - Caro
MSN:
404-0225
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3600
Aircraft flight hours:
17393
Circumstances:
The pilot was departing from Lansing, Michigan, when he reported engine problems. The aircraft subsequently lost power to both engines. Fuel receipts were found that indicate that the aircraft was serviced with 25 gallons of jet fuel in each wing tank. No preexisting anomalies were found with regard to the aircraft or its systems. An FAA inspector interviewed the person that had fueled the aircraft and that person stated he had used a JET-A fuel truck to fuel the accident aircraft. The inspector also interviewed the safety director of the company that provided the fueling service. The safety director told the inspector that the fuel truck used to fuel the accident aircraft was found to have a small nozzle installed on one of the hoses and not the wide nozzle used on jet fueling trucks. He also said that, '...the small nozzle was used for the purpose of fueling tugs at the airport and that the small nozzles were immediately removed from all jet refueling trucks so that this could not happen again.'
Probable cause:
A loss of engine power due to improper fuel. Also causal was the improper aircraft service by the fixed base operator personnel and the unsuitable terrain for the forced landing encountered by the pilot. Factors were the improper grade of fuel and the lack of suitable terrain for the landing.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Pontiac: 1 killed

Date & Time: Dec 4, 1998 at 2045 LT
Registration:
N59902
Flight Type:
Survivors:
No
Schedule:
Lansing - Troy
MSN:
31-7652125
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1866
Captain / Total hours on type:
129.00
Circumstances:
The airplane collided with the tops of trees during an ILS approach near the middle marke. Witnesses heard the airplane strike the trees and a '...whop, whop, whop sound...' it made as it continued its flight. Other witnesses observed the airplane flying a curved, descending, flight path until the aircraft impacted the ground. Visibility was reported as 1/2 mile at the airport. The on-scene examination revealed no airframe or engine anomalies that would prevent flight. A section of the right propeller and other pieces of airframe were found along the approach path after initial impact with trees. The trees along the flight path were about 30 to 60 feet high. The tops of the taller trees were broken or had fresh cut marks on their limbs. The pilot's blood alcohol level was 216 (mg/dL, mg/hg).
Probable cause:
The pilot's descent below the decision height for the instrument approach.
Final Report:

Crash of a Cessna 401 in Crystal

Date & Time: Jan 22, 1997 at 1326 LT
Type of aircraft:
Operator:
Registration:
N5AS
Flight Phase:
Survivors:
Yes
Schedule:
Crystal – Lansing
MSN:
401-0208
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3745
Captain / Total hours on type:
409.00
Circumstances:
After landing at the airport, the airplane was taxied to a fixed base operator to pick up a passenger. Rime ice, as thick as two inches was seen on the airplane, and the pilots of the airplane attempted to manually remove the ice. The airplane was topped off with fuel before departure. During departure from runway 31R, the airplane collided with a fence. Numerous areas of ice were found on the airplane following the accident. Both propellers had similar damage. The pilots had reported to the FAA that the left engine had sustained a loss of power. The passenger reported that he did not notice any loss of power from either engine. No preimpact part failure or malfunction of the left engine was found.
Probable cause:
Failure of the pilot-in-command to ensure adequate removal of airframe ice from the aircraft during preflight.
Final Report:

Crash of a Rockwell Grand Commander 690A in Lansing: 2 killed

Date & Time: Sep 27, 1993 at 1123 LT
Registration:
N242TC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Lansing - Battle Creek
MSN:
690-11219
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
8790
Aircraft flight hours:
4373
Circumstances:
The airplane departed in IMC conditions on an IFR flight plan. Shortly after takeoff the pilot told the departure controller he had '...a problem.' The airplane's flight path was a series of left hand turns while performing descents and ascents. Reports of engine sounds varied from high rpm to low rpm. Many witnesses reported the airplane descending out of, and climbing into, clouds. The airplane was observed in a 45° angle descent, right wing low, as it collided with trees and the ground. The on-scene investigation found an intermittent electric gyro system inverter, a broken filament on the inverter power 'out' light bulb, electrically powered gyro's rotors did not have rotational damage, and a vacuum powered attitude indicator rotor with rotational damage. The pilot's toxicology report stated 45 mg/dl of ethanol detected in his muscle tissue.
Probable cause:
The pilot-in-command not maintaining aircraft control during the intermittent operation of the electrically operated attitude gyro. Factor's associated with this accident are an fluctuating (intermittent) electrical system inverter and the pilot-in-command not performing remedial action by using the vacuum powered attitude gyro and other flight instruments once the airplane was making a series of climbs, descents, and heading changes.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Troy: 2 killed

Date & Time: Jan 29, 1986 at 1314 LT
Operator:
Registration:
N68653
Flight Phase:
Survivors:
No
Schedule:
Troy - Lansing
MSN:
421C-1070
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1750
Aircraft flight hours:
1275
Circumstances:
At rotation the right engine failed. The aircraft entered a skidding turn to the right and continued to climb to about 100 feet agl. During the turn 110° from takeoff. Heading aircraft rolled inverted and descended into a car port. Extensive post impact fire destroyed aircraft, car port and three vehicles. Gear was not retracted and propellers was not feathered. During post accident exam of the right engine extensive internal damage was found. Both occupants were killed.
Probable cause:
Occurrence #1: loss of engine power (partial) - mech failure/malf
Phase of operation: takeoff - initial climb
Findings
1. (c) engine assembly - failure, total
----------
Occurrence #2: loss of control - in flight
Phase of operation: descent
Findings
2. (f) gear retraction - not performed - pilot in command
3. (f) propeller feathering - not performed - pilot in command
4. (f) directional control - not maintained - pilot in command
5. (f) throttle/power control - improper use of - pilot in command
----------
Occurrence #3: in flight collision with object
Phase of operation: descent - uncontrolled
Findings
6. Object - tree(s)
7. Object - residence
8. Object - vehicle
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith Aerostar 601) in Grand Rapids: 4 killed

Date & Time: Jan 19, 1979 at 1922 LT
Operator:
Registration:
N7437S
Survivors:
Yes
Schedule:
Lansing - Marquette
MSN:
61-0008-025
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
2646
Captain / Total hours on type:
195.00
Circumstances:
Few minutes after takeoff from Lansing Airport, while climbing in poor weather conditions, the pilot was cleared to divert to Grand Rapids-Kent County Airport. On approach, the airplane became uncontrollable and crashed. Two passengers were seriously injured while four other occupants were killed.
Probable cause:
Uncontrolled collision with ground on approach after the pilot initiated flight in adverse weather conditions. The following contributing factors were reported:
- Failed to follow approved procedures,
- Airframe ice,
- Icing conditions including sleet, freezing rain,
- Windshear,
- Ice on windshield,
- Visibility 2 miles or less.
Final Report:

Crash of a Beechcraft H18 in Iron Mountain: 1 killed

Date & Time: Oct 17, 1974 at 0151 LT
Type of aircraft:
Operator:
Registration:
N72FA
Flight Type:
Survivors:
No
Schedule:
Lansing - Iron Mountain
MSN:
BA-631
YOM:
1962
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
12345
Captain / Total hours on type:
4000.00
Circumstances:
During a night approach to Iron Mountain Airport, the pilot descended below the MDA when the twin engine airplane struck tree tops and crashed in a wooded area located few hundred yards short of runway threshold. The aircraft was destroyed and the pilot, sole on board, was killed.
Probable cause:
Collision with trees on a night approach following improper IFR operation. The following contributing factors were reported:
- Instruments misread or failed to read,
- High obstructions,
- Descended below clearance limit of 3,000 feet.
Final Report:

Crash of a Beechcraft H18 in Iron Mountain: 1 killed

Date & Time: Jul 3, 1974 at 0145 LT
Type of aircraft:
Operator:
Registration:
N73FA
Flight Type:
Survivors:
No
Schedule:
Lansing - Iron Mountain
MSN:
BA-649
YOM:
1963
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6070
Circumstances:
On a night approach to Iron Mountain-Ford Airport, the pilot encountered poor weather conditions and very limited visibility. On final, he failed to realize his altitude was too low when the airplane struck a dirt bank and crashed in flames. The aircraft was destroyed and the pilot, sole on board, was killed.
Probable cause:
Improper in-flight decisions on part of the pilot who continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Failed to initiate a go-around,
- Incorrect altimeter setting,
- Not aligned with runway,
- Weather considerably worse than forecast,
- Heavy fog.
Final Report:

Crash of a Cessna 411 in Lansing

Date & Time: Dec 14, 1973 at 1106 LT
Type of aircraft:
Operator:
Registration:
N1056R
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lansing - Columbus
MSN:
411-0245
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4000
Captain / Total hours on type:
800.00
Circumstances:
Just after liftoff, while in initial climb, the twin engine airplane stalled and crashed onto the runway and came to rest. Both occupants were uninjured while the aircraft was damaged beyond repair.
Probable cause:
Engine malfunction during initial climb caused the aircraft to stall and to crash. The following factors were reported:
- Improper operation or powerplant,
- Foreign material affecting normal operations,
- Fuel system: ram air assembly,
- The pilot attention diverted from operation of aircraft,
- Failed to obtain/maintain flying speed,
- Partial loss of power on both engines,
- Engine air intake openings restricted by snow,
- Pilot did not use alternate air,
- Pilot elected to land cartwheeled.
Final Report: