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Leicestershire

Crash of a Beechcraft C90 King Air in East Midlands: 1 killed

Date & Time: Jan 25, 1988 at 2247 LT
Type of aircraft:
Registration:
G-BNAT
Flight Type:
Survivors:
No
Schedule:
Stansted – East Midlands
MSN:
LJ-614
YOM:
1974
Flight number:
646
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2900
Captain / Total hours on type:
600.00
Circumstances:
The twin engine aircraft was completing a cargo flight from Stansted to East Midlands, carrying approximately 800 kilos of various goods. As the aircraft was on approach 1 nm from touchdown, ATC advised that the RVR for landing had reduced to 900 meters and, very soon afterwards, notified a further deterioration to 800 meters. Immediately after this last ATC transmission, the pilot transmitted 'National Six Four Six got to go-around'. Ten seconds later he transmitted 'crashing...National'. The aircraft subsequently struck the ground at a point approximately 350 meters to the right of the runway 09 centerline and 750 meters beyond the threshold. The aircraft was destroyed by a post crash fire and the pilot, sole on board, was killed.
Probable cause:
It was determined that the the aircraft's weight was 90 kilos above its maximum authorised takeoff weight at Stansted Airport and after allowing for the fuel used on route, it would have arrived at least 160 kilos above its maximum authorised landing weight. Furthermore, the steep angle of impact was suggestive of a dive following a stall.
Final Report:

Crash of a Fokker F27 Friendship 200 in East Midlands

Date & Time: Jan 18, 1987 at 1415 LT
Type of aircraft:
Operator:
Registration:
G-BMAU
Flight Type:
Survivors:
Yes
Schedule:
East Midlands - East Midlands
MSN:
10241
YOM:
1963
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8345
Captain / Total hours on type:
2983.00
Copilot / Total flying hours:
5220
Copilot / Total hours on type:
572
Aircraft flight hours:
38487
Aircraft flight cycles:
44761
Circumstances:
The BMA Fokker F-27 aircraft was engaged on crew training at East Midlands Airport (EMA). The commander, who was an experienced training captain, occupied the right pilot's seat and a first officer undergoing training for conversion to captaincy occupied the left seat as handling pilot. Another captain refreshing on type sat on the jump seat behind the pilots' seats, the intention being that he should move into the left seat after the first officer's training period. The weather was: wind 150 degrees at 7 kts, visibility 4 km and cloud 7 oktas stratus, base 1000 feet. The surface temperature was 2 °C and the QNH 1030. The training session began with a practice abandoned takeoff after which the aircraft took off at 13:08 and flew three practice ILS approaches followed by touch-and-go landings on runway 09, climbing to 2000 feet above mean sea level (amsl) after each takeoff. The runway in use was then changed and the aircraft flew a simulated asymmetric ILS approach to runway 27 followed by a missed approach (go-around) with the left engine throttled back. The runway was then changed again and an ILS approach to runway 09 was flown with the left engine still throttled back. This approach was followed by a touch-and-go landing during which both engines were brought up to full power. Very soon after becoming airborne the training captain again simulated failure of the left engine and the aircraft was climbed to 2000 feet amsl. Soon after the aircraft levelled off, the handling pilot commented on the large amount of rudder required to counteract the simulated failure of the left engine after takeoff. The training captain then said that he was deliberately putting more drag on the left side than would have been the case if the propeller had auto-feathered so that the climb performance corresponded better with that of an aircraft with passengers on board. He went on to say that if the handling pilot could cope with that extra drag, he could expect to control the aircraft if the failed engine auto-feathered because the rudder pedal force would then not be quite so great. The crew then began a procedural NDB approach to runway 09, for which instrument screens were fitted in front of the handling pilot. It was intended that the aircraft should be landed after the NDB approach for the pilot in the jump seat to take over as handling pilot. Decision altitude for the approach was 740 feet and touchdown altitude was 305 feet. It was company practice for beacon passage to be identified by the movement of the radio compass needle and, as the aircraft passed about one third of a mile north of the marker beacon inbound, descending through approximately 1300 feet amsl, the handling pilot said "Over the beacon now". No audio signal from the marker beacon was heard on the cockpit voice recorder. The landing checklist was completed during the following 20 seconds, including confirmation that the undercarriage was down, fuel heaters were off, two blue propeller lights were illuminated and fuel was trimmed up. 48 seconds after passing the beacon the aircraft reached decision altitude, and the training captain asked the handling pilot "How long and where is it?", to which the handling pilot replied "Got about a minute and ten seconds to go - should be straight in front". 22 seconds later and some 36 seconds before impact the training captain said "Why are we at 650 feet?" and pointed out that the handling pilot had allowed the aircraft to descend below decision altitude when he was, for training purposes, still in IMC. The handling pilot responded by saying "Intend going around then", or words to that effect. The training captain then said "Yes, well I'll let you see it now. There it is". As the training captain was saying this, the sound of an engine power increase was heard on the CVR, and, about 25 seconds before impact, the rpm of one engine was increased to 14,800 rpm, a setting 200 rpm below maximum continuous power. 10 seconds later the training captain was heard to say "Hang on, that's the - that's the field there. See it?" The handling pilot then said "Hold tight", at which point, some 13 seconds before impact, the CVR recorded the sound of another engine increasing power to 14,800 rpm. A moment later the handling pilot said "Haven't got it", and the training captain said "I've got it". The F-27 yawed to the left before banking steeply to the right. The aircraft struck the ground on the northern side of the Castle Donington motor racing circuit in a nose-down attitude, banked to the left and with considerable left sideslip. After the accident an accumulation of mixed rime and glaze ice was found on the leading edges of the wings and tail surfaces which had formed rough-surfaced horns one inch high above and below the airflow stagnation point. No ice was found on the flaps or landing gear.
Probable cause:
The probable cause of the accident was that the aircraft became uncontrollable at an airspeed well above both its stalling speed and minimum control speed because its flying and handling characteristics were degraded by an accumulation of ice. The decision by the training captain not to operate the airframe de-icing system was an underlying cause but he could not have been expected to foresee this at the time. A contributory factor was that the operating crew allowed the airspeed to fall below the normal approach speed during the latter stages of the approach.
Final Report:

Crash of a Short 360-100 in East Midlands

Date & Time: Jan 31, 1986 at 1851 LT
Type of aircraft:
Operator:
Registration:
EI-BEM
Survivors:
Yes
Schedule:
Dublin - East Midlands
MSN:
3642
YOM:
1984
Flight number:
EI328
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
33
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7528
Captain / Total hours on type:
123.00
Copilot / Total flying hours:
4299
Copilot / Total hours on type:
1240
Aircraft flight hours:
3226
Circumstances:
The Shorts 360 aircraft was scheduled to fly from Dublin (DUB) to East Midlands Airport (EMA) as Aer Lingus flight 328. During the pre-flight briefing the crew learned that at East Midlands the precision radar was unserviceable and that, although the visual approach slope indicators (VASI) had been withdrawn, the precision approach path indicators (PAPI) were operational. The en-route weather was reported as being overcast for the whole journey, with cloud tops at FL70 and a probability of icing when flying in the cloud. There had also been a pilot's report of severe icing between FL30 and FL70 in the Birmingham area, some 30 nm south-west of East Midlands Airport. The terminal area forecast for East Midlands suggested a brisk north-easterly wind and a cloud base of 1200 feet. The aircraft took off at 17:25. The crew report that they exercised the wing and tail de-icing system during the climb to FL 90, the level which had been assigned for the flight, and that at that level they were above the layers of stratiform cloud. Following an uneventful flight, via Wallasey, to the NDB at Whitegate, they were taken under radar control directly towards the airport and given descent clearance, eventually to 3000 feet, to intercept the ILS approach path for runway 09. During the descent and before entering the cloud tops at about FL60, the crew switched on the aircraft's anti-ice system, which heats the windscreen, engine air intakes, propellers, static air vents and pitot probes but, in accordance with normal operating procedure, they did not use the wing and tail de-icing system. At this time, the freezing level (0°C isotherm) was at 1000 feet, the temperature at FL 60 was minus 6°C and the air was saturated. Whilst in the cloud, which according to the non-handling pilot was particularly dense, ice thrown from the propellers was heard striking the side of the aircraft fuselage, and it was suggested that the propeller rpm be increased to expedite the removal of the ice. Both pilots state that, at some time during the descent, they visually checked the aircraft for ice but saw none. Nevertheless, several other flights during that evening have since reported the occurrence of severe icing. Having levelled at 3000 feet, still in and out of cloud, the aircraft was directed by radar to intercept the ILS and was fully established on the glideslope and centreline by 10 nm, at which point the final descent was initiated. A normal approach was established and continued, past the outer marker beacon situated at 3.9 nm from touchdown, down to around 1000 feet above the runway threshold height. The crew state that up to this point they had neither experienced any significant turbulence nor observed any ice forming on the aircraft. The last meteorological information passed to the crew gave the wind as 060 degrees /15 kt, however, over the previous hour the wind speed in the area, although not automatically recorded at the airport, is reported as gusting up to 30 kt. As the aircraft descended through about 1000 feet, it suddenly rolled very sharply to the left without apparent cause. With the application of corrective aileron and rudder the aircraft rolled rapidly right, well beyond the wings level position. This alternate left and right rolling motion continued with the angles of bank increasing for some 30 seconds, causing the commander to believe that the aircraft might roll right over onto its back. The angles of bank then gradually decreased. During this period and the subsequent few seconds the aircraft established a very high descent rate approaching 3000 feet/min. Subsequently, with the aid of full engine power, the airspeed increased and the rate of descent was arrested just as the aircraft struck an 11 KV power cable. It continued through another similar cable, two of the supporting wooden poles and the tops of two trees, before coming to rest nose into a small wood edging a field of barley, some 460 metres from the impact with the first power cable. The cockpit and passenger cabin were relatively undamaged and there was no fire. The aircraft came to rest lying virtually upright and the passengers, and subsequently the crew, successfully evacuated from the front and rear emergency exits.
Probable cause:
The accident most probably occurred as a result of the effects of a significant accumulation of airframe ice degrading the aircraft's stability and control characteristics, such that the crew were unable to maintain control. Turbulence and or downdraught may have contributed to the accident. Other contributory factors were the difficulty in detecting clear ice at night on the SD3-60 which resulted in the airframe de-icing system not being used. The delay in application of go-around power may have also contributed to the accident.
Final Report:

Crash of an Avro 748-108-2A in Nailstone: 3 killed

Date & Time: Jun 26, 1981 at 1811 LT
Type of aircraft:
Operator:
Registration:
G-ASPL
Flight Type:
Survivors:
No
Schedule:
Londres-Gatwick – East Midlands
MSN:
1560
YOM:
1964
Flight number:
DA240
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
8418
Captain / Total hours on type:
1393.00
Copilot / Total flying hours:
5611
Copilot / Total hours on type:
1711
Aircraft flight hours:
34592
Circumstances:
The aircraft was engaged on a mail flight from London-Gatwick Airport to East Midlands Airport. During the initial descent in preparation for landing at its destination, the attendant in the cabin reported that the mechanical indicators on one of the cabin doors were showing an unlocked condition. Shortly afterwards the right hand rear door (baggage door) came open, detached from its hinge mountings and became lodged on the leading edge of the right horizontal tailplane. The aircraft became uncontrollable and went into an increasingly steep dive which terminated in several abrupt pitch oscillations. Both the mainplanes and the horizontal tailplanes were subjected to overstressing in upload which resulted in their detachment from the fuselage. The aircraft was totally destroyed and all three crew members were killed.
Probable cause:
The accident was caused by the baggage door becoming lodged on the leading edge of the right tailplane after it had opened and detached in flight. This produced changes in the aerodynamic characteristics of the aircraft which rendered it uncontrollable resulting in overstressing of the wings and tailplane leading to an in-flight structural failure. A contributory factor was the mis-rigged state of the door operating mechanism which allowed the top and the bottom pairs of claw catches to lose synchronisation. The failure of the door warning arrangements to give adequate warning of door safety was a further contributory factor.
Final Report:

Crash of a Vickers 736 Viscount in East Midlands

Date & Time: Feb 20, 1969
Type of aircraft:
Operator:
Registration:
G-AODG
Survivors:
Yes
Schedule:
Glasgow – East Midlands
MSN:
77
YOM:
1955
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
48
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On approach to East Midlands Airport, the crew encountered poor weather conditions (snow falls) and the captain decided to go-around. During a second attempt to land on runway 10, the pilot-in-command failed to realize his exact position when the airplane struck the ground 1,000 feet prior to the touchdown zone. Upon impact, the nose gear was torn off and the aircraft came to rest in a snow covered field, broken in two. All 53 occupants escaped uninjured while the aircraft was written off.
Probable cause:
Wrong approach configuration in poor weather conditions.

Crash of an Avro 685 York C.1 in RAF Desford

Date & Time: Aug 11, 1948
Type of aircraft:
Operator:
Registration:
MW259
Flight Type:
Survivors:
Yes
MSN:
MW259
YOM:
1946
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
En route, the crew informed ATC that the engine number four failed. He received the permission to divert to RAF Desford to attempt an emergency landing. To lower the risk of fire, the crew decided to shut down the engine number three and feathered the propeller as well. Due to a loss of speed, the aircraft was unable to maintain a safe altitude. During the last segment, the aircraft stalled and hit violently the runway surface. On impact, the aircraft broke in two and came to rest in flames. All four crew members were evacuated safely while the aircraft was destroyed.
Probable cause:
Failure of the engine number four in flight. The exact cause of the failure remains unknown.

Crash of a Douglas C-47A-25-DK Dakota III near RAF Wymeswold

Date & Time: Apr 17, 1946
Operator:
Registration:
KG594
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
13317
YOM:
1944
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Enroute, an engine failed and the crew was unable to feather the propeller. Due to strong drag, the captain could not maintain a safe height so he decided to attempt an emergency landing. The aircraft belly landed in a field located 2 miles southeast of RAF Wymeswold. There were no casualties but the aircraft was written off.
Probable cause:
Engine failure.

Crash of an Avro 683 Lancaster IB in Wigston: 6 killed

Date & Time: Feb 4, 1946
Type of aircraft:
Operator:
Registration:
PA269
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Faldingworth - Faldingworth
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
While overflying Wigston in very poor weather conditions, the aircraft went out of control and spiraled into the ground. During the descent, the aircraft disintegrated in the air and crashed in the city of Wigston. Debris were found on a large area and several houses were damaged. While there were no casualties on the ground, all six crew members were killed.
Crew (300th Squadron):
W/Cdr R. Sulinski, pilot,
F/O W. Jedrzejczyk, navigator,
F/O C. Sulgut, air gunner,
W/O W. Brzezinski, wireless operator,
W/O M. Szwandt, air bomber,
F/Sgt F. Mikula, flight engineer.
Probable cause:
The aircraft may have been struck by lightning while flying in very bad weather conditions (clouds with turbulence and thunderstorm activity).

Crash of a Douglas DC-3 Dakota III in RAF Castle Donington

Date & Time: Aug 14, 1945
Operator:
Registration:
KG611
Flight Type:
Survivors:
Yes
MSN:
13370
YOM:
1944
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed on approach to RAF Castle Donington. There were no casualties.

Crash of a Douglas DC-3 Dakota IV in Sileby: 3 killed

Date & Time: Jan 10, 1945
Type of aircraft:
Operator:
Registration:
KJ835
Flight Phase:
Flight Type:
Survivors:
No
MSN:
25619/14174
YOM:
1944
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
Few minutes after take off from a local RAF station, the crew encountered poor weather conditions with snow falls and icing. After the carburetors got iced, control was lost and the aircraft dove into the ground and crashed in a field, killing all three crew members.
Crew (108th OTU):
W/O Frederick Edward Henry Dobson, pilot,
Sgt Edgar James Wilmot, navigator,
Sgt Ronald James Hillsdon, wireless operator.