Crash of a Beechcraft E18S in Davenport: 6 killed

Date & Time: Apr 19, 1973 at 1704 LT
Type of aircraft:
Operator:
Registration:
N310WA
Survivors:
No
Schedule:
Muscatine - Davenport - Chicago
MSN:
BA-12
YOM:
1954
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
6000
Captain / Total hours on type:
2000.00
Circumstances:
On approach to Davenport Airport, the right wing detached. The twin engine airplane went out of control and crashed in an open field located few miles from the airfield. The aircraft was totally destroyed and all six occupants were killed.
Probable cause:
Structural failure of the right wing on descent due to fatigue cracks. The following factors were reported:
- Airframe, wings spars,
- Fatigue fracture,
- Inadequate inspection of aircraft on part of the maintenance personnel,
- Preexisting crack on lower spar cap WS-81 that was discernible but not detected over a 6-year period,
- Right wing folded upward.
Final Report:

Crash of a Beechcraft C90 King Air in Cedar Rapids: 5 killed

Date & Time: Jan 3, 1973 at 1722 LT
Type of aircraft:
Operator:
Registration:
N936K
Survivors:
No
Schedule:
Omaha - Cedar Rapids
MSN:
LJ-539
YOM:
1972
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
4225
Captain / Total hours on type:
25.00
Circumstances:
The crew started an ILS approach to Cedar Rapids Airport in poor weather conditions when control was lost. The airplane dove into the ground and crashed in an open field located few miles from the airport. The twin engine airplane was totally destroyed and all five occupants have been killed. It was determined that in poor weather conditions, the left wing, left engine and tail separated in flight, causing the aircraft to be uncontrollable.
Probable cause:
Improper in-flight decisions on part of the pilot-in-command who exceeded the designed stress limits of the aircraft. The following factors were reported:
- Overload failure,
- Separation in flight,
- Low ceiling, fog and snow,
- Turbulences associated with clouds and thunderstorms,
- Began the descent to ILS approach too late,
- It is believed that the crew expedited the descent,
- The left wing, the left engine and the tail separated in flight.
Final Report:

Crash of a Piper PA-31-310 Navajo in Iowa City

Date & Time: Feb 18, 1971 at 1915 LT
Type of aircraft:
Operator:
Registration:
N8000Y
Survivors:
Yes
Schedule:
Detroit – Iowa City
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10025
Captain / Total hours on type:
620.00
Circumstances:
The pilot started the approach to Iowa City Airport by night and marginal weather conditions. Due to poor visibility, he made a go-around and followed a circuit for few minutes before starting a second approach. In half mile visibility with ceiling at 300 feet, he continued the approach and passed below the MDA when the airplane struck the ground and crashed. All four occupants were injured and the aircraft was destroyed.
Probable cause:
Improper IFR operation on part of the pilot, The following factors were reported:
- Electrical failure,
- Low ceiling (300 feet), 0.5 mile visibility, rain,
- The pilot stated that VOR DME fluctuated,
- Right alternator inoperative,
- The pilot descended below the published MDA on second VOR approach.
Final Report:

Ground collision of a Beechcraft E18S in Keokuk

Date & Time: Sep 29, 1970 at 0135 LT
Type of aircraft:
Registration:
N29W
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Keokuk – Detroit
MSN:
BA-107
YOM:
1955
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4128
Captain / Total hours on type:
600.00
Circumstances:
The crew was preparing the aircraft for a cargo flight to Detroit. On ground, the crew proceeded to an instruments check and started both engines without making an external visual check. A private Cessna 337 just landed and its pilot was taxiing to the parking when the Beechcraft moved and collided with the Cessna. Both aircraft caught fire and all three occupants were seriously injured.
Probable cause:
The crew started the engine without proper assistance and his attention was diverted from operation of the aircraft at that time. The following contributing factors were reported:
- The crew was preoccupied by cockpit check,
- Neither aircraft was chocked for engine start,
- No line personnel was available.
Final Report:

Crash of a Beechcraft E18S in Sioux City: 2 killed

Date & Time: May 19, 1970 at 1103 LT
Type of aircraft:
Operator:
Registration:
N139K
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Atlanta - North Sioux City - Willmar
MSN:
BA-188
YOM:
1956
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3075
Captain / Total hours on type:
525.00
Circumstances:
Few minutes after takeoff from North Sioux City-Graham Field, South Dakota, while climbing, the crew encountered technical difficulties and feathered the left propeller. Shortly later, control was lost and the airplane crashed in flames in an open field located near Sioux City. The aircraft was destroyed and both pilots were killed.
Probable cause:
Uncontrolled descent following an in-flight fire for undetermined reason. The following findings were reported:
- Left propeller found feathered for unknown reason,
- Investigations showed no engine malfunction.
Final Report:

Crash of a Douglas DC-9-15 in Sioux City

Date & Time: Dec 27, 1968 at 0711 LT
Type of aircraft:
Operator:
Registration:
N974Z
Flight Phase:
Survivors:
Yes
Schedule:
Sioux Falls – Sioux City – Chicago
MSN:
47034/162
YOM:
1967
Flight number:
OZ982
Location:
Crew on board:
4
Crew fatalities:
Pax on board:
64
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
19146
Captain / Total hours on type:
63.00
Copilot / Total flying hours:
6048
Copilot / Total hours on type:
20
Aircraft flight hours:
3458
Circumstances:
At approximately 0711LT, the aircraft crashed while taking off from the Sioux City Airport, Iowa. There were no fatalities. Among the 64 passengers and four crewmembers, 10 passengers were hospitalized with minor injuries and three crew members received serious injuries. The aircraft was destroyed in the crash. There was no fire. Flight 982 began its takeoff on Runway 35 with the flight crew aware that ice was present on the wings. The aircraft lifted off and the landing gear was selected to the up position by the first officer. The captain began turning off the landing and taxi lights. As the landing gear began to retract, the aircraft rolled abruptly and violently to the right to an angle of bank estimated by the flight crew to have reached 900. The captain applied additional power and left rudder in an attempt to level the wings. When no immediate response was noted, he then applied left aileron. With the application of left aileron, the right wing came up; however, the roll continued to the left until the left wing contacted the runway. At this point, the captain discontinued the takeoff. He approximately 110 feet beyond the departure threshold of Runway 35. succeeded in leveling the wings prior to final ground contact, The aircraft came to rest in a grove of trees approximately 1,181 feet beyond the departure end of Runway 35.
Probable cause:
A stall near the upper limits of ground effect, with subsequent loss of control as a result of aerodynamic and weight penalties of airfoil icing. The flight crew failed to have the airfoil ice removed prior to the attempted take-off from Sioux City. The Board also finds that the crew selected an improper takeoff thrust for the existing gross weight condition of the aircraft.
Final Report:

Crash of a Hawker-Siddeley HS.125-1A in Des Moines

Date & Time: Feb 24, 1966 at 1357 LT
Type of aircraft:
Operator:
Registration:
N1135K
Flight Phase:
Survivors:
Yes
Schedule:
Des Moines – Omaha
MSN:
25019
YOM:
1965
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7330
Captain / Total hours on type:
375.00
Circumstances:
During the takeoff roll, the pilot-in-command attempted to rotate when an unexpected situation was encountered. The captain decided to abort the takeoff and started an emergency braking procedure. Unable to stop within the remaining distance, the airplane overran and struck ditches before coming to rest in a field. While all four passengers were unhurt, both pilots were seriously injured. The aircraft was written off.
Probable cause:
Inadequate preflight preparation on part of the crew who attempted to takeoff with the gust locks still engaged. Delayed action in aborting the takeoff was considered as a contributing factor.
Final Report:

Crash of a Douglas C-47B-15-DK in Clinton

Date & Time: Mar 6, 1955
Operator:
Registration:
43-49549
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
15365/26810
YOM:
1944
Location:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances. There were no casualties.

Crash of a Convair CV-340-13 near Dexter

Date & Time: Jan 19, 1955 at 1625 LT
Type of aircraft:
Operator:
Registration:
N73154
Flight Phase:
Survivors:
Yes
Schedule:
Newark – Allentown – Youngstown – Akron – Cleveland – Chicago – Moline – Iowa City – Des Moines – Omaha – Lincoln
MSN:
180
YOM:
1954
Flight number:
UA329
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
36
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7578
Captain / Total hours on type:
750.00
Copilot / Total flying hours:
2123
Copilot / Total hours on type:
1147
Aircraft flight hours:
1502
Circumstances:
Flight 329 departed Des Moines on a VFR (Visual Flight Reed) night plan at 1608 for Omaha, Nebraska. The gross weight of the aircraft was 45,215 pounds 1,685 pounds less than the allowable 46,900 pounds. According to company records, the load was properly distributed with respect to the canter of gravity of the aircraft. The climb to 5,000 feet was uneventful but at that altitude the crew noticed vibration and a slight fore-and-aft movement of the control column. The climb was continued to 6,000 feet, where the aircraft was leveled off and power was reduced. As the vibration was still present at this time, the captain attempted to dampen it by engaging the autopilot; however, this was unsuccessful and it was immediately disengaged. The first officer next lowered the flaps, first to 5 degrees and then to 15 degrees, without any noticeable effect. The “Fasten Seat Belt" sign was turned on and the captain told the first officer to advise the company of their difficulty via radio. About this time a sudden failure in the control system was felt and it was with extreme difficulty that any semblance of elevator control was maintained. The first officer again tried lowering the flaps, this time to the 24-degree position, but as this did not help to maintain control he returned them to the 15-degree position, where it was found the most favorable results were attained. Accordingly, the first officer transmitted "Mayday” (distress call) on the radio and said that they were attempting to return to Des Moines but were experiencing control trouble. The buffeting became so severe it was then necessary for the copilot to help the can hold the control column. However, the buffeting lessened and the captain advised the first officer to depressurize the aircraft and tell the stewardess to prepare the passengers for an emergency landing. This was done. By that time the aircraft had descended below 3,000 feet. Both throttles were retarded in turn to see if the trouble could possibly be caused by one of the engines. This also proved to no avail. The vibration built up to high level and suddenly another failure in the control system was felt and the air-plane went into a steep climb. As it seemed that a stall was imminent, the captain quickly moved the propellers to a high r. p. m. and pushed the throttles forward until about 50 inches of manifold pressure was seen on the gauges. The airplane then nosed over and began to dive at a very steep angle. During this rapid descent the captain reduced power and headed toward open country to his right. When the aircraft reached 500 feet above the ground the captain was successful in flaring the aircraft and it struck the ground in a flat attitude. All occupants were quickly deplaned as soon as the aircraft stopped.
Probable cause:
The Board determines that the probable cause of this accident was a series of omissions made by maintenance personnel during a scheduled inspection which resulted in the release of the aircraft in an unairworthy condition and an almost complete loss of elevator control during flight. The following findings were reported:
- During a routine maintenance inspection of the aircraft an explanation was not written on the non-routine job card that the bolt had been removed and replaced finger-tight pending the arrival of a new bolt,
- Final inspection of the servo tab system failed to disclose its unairworthy condition and the aircraft was released for service,
- Vibration backed off an unsafetied not in the servo tab system resulting in a sequence of structural failures that ended in almost complete loss of control of the aircraft elevators.
Final Report:

Crash of a Douglas C-47-DL near Mason City: 12 killed

Date & Time: Aug 22, 1954 at 1703 LT
Operator:
Registration:
N61451
Survivors:
Yes
Schedule:
Memphis – Little Rock – Fort Smith – Muskogee – Tulsa – Kansas City – Des Moines – Waterloo – Mason City – Austin – Rochester – Minneapolis
MSN:
4630
YOM:
1942
Flight number:
BN152
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
12
Captain / Total flying hours:
11077
Captain / Total hours on type:
8000.00
Copilot / Total flying hours:
5682
Copilot / Total hours on type:
2700
Aircraft flight hours:
23062
Probable cause:
The Board determines that the probable cause of this accident was that the flight while endeavouring to traverse a thunderstorm area encountered very heavy rain, divergent winds, and strong downdrafts that forced the aircraft to the ground. The following findings were reported:
- The flight was observed to enter and disappear in a thunderstorm,
- The aircraft crashed in an area where severe storm ground damage occurred,
- The US Weather Bureau Kansas City received the USAF severe weather advisories but considered their forecast in effect at the time to be adequate,
- The weather forecast issued by the Weather Bureau and Braniff did not indicate the severity of the storm that was encountered.
Final Report: