code

CT

Crash of a Cessna 560XLS+ Citation Excel in Plainville: 4 killed

Date & Time: Sep 2, 2021 at 0951 LT
Registration:
N560AR
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Plainville – Manteo
MSN:
560-6026
YOM:
2009
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
17400
Copilot / Total flying hours:
5594
Aircraft flight hours:
2575
Circumstances:
The flight crew was conducting a personal flight with two passengers onboard. Before departure, the cockpit voice recorder (CVR) captured the pilots verbalizing items from the before takeoff checklist, but there was no challenge response for the taxi, before takeoff, or takeoff checklists. Further, no crew briefing was performed and neither pilot mentioned releasing the parking brake. The left seat pilot, who was the pilot flying (PF) and pilot-in-command (PIC), initiated takeoff from the slightly upsloping 3,665-ft-long asphalt runway. According to takeoff performance data that day and takeoff performance models, the airplane had adequate performance capability to take off from that runway. Flight data recorder (FDR) data indicated each thrust lever angle was set and remained at 65° while the engines were set and remained at 91% N1. During the takeoff roll, the CVR recorded the copilot, who was the pilot monitoring (PM) and second-in-command (SIC), making callouts for “airspeed’s alive,” “eighty knots cross check,” “v one,” and “rotate.” A comparison of FDR data from the accident flight with the previous two takeoffs showed that the airplane did not become airborne at the usual location along the runway, and the longitudinal acceleration was about 33% less. At the time of the rotate callout, the airspeed was about 104 knots calibrated airspeed, and the elevator was about +9° airplane nose up (ANU). Three seconds after the rotate callout, the CVR recorded the sound of physical straining, suggesting the pilot was likely attempting to rotate the airplane by pulling the control yoke. The CVR also captured statements from both the copilot and pilot expressing surprise that the airplane was not rotating as they expected. CVR and FDR data indicated that between the time of the rotate callout and the airplane reaching the end of the airport terrain, the airspeed increased to about 120 knots, the weight-on-wheels (WOW) remained in an on-ground state, and the elevator position increased to a maximum value of about +16° ANU. However, the airplane’s pitch attitude minimally changed. After the airplane cleared the end of the airport terrain where the ground elevation decreased 20 to 25 ft, FDR data indicate that the WOW transitioned to air mode with near-full ANU elevator control input, and the airplane pitched up nearly 22° in less than 2 seconds. FDR data depicted forward elevator control input in response to the rapid pitch-up, and the CVR recorded a stall warning then stick shaker activation. An off airport witness reported seeing the front portion of the right engine impact a nearby pole past the departure end of the runway. The airplane then rolled right to an inverted attitude, impacted the ground, then impacted an off airport occupied building. The airplane was destroyed by impact forces and a post crash fire and all four occupants were killed. On ground, four other people were injured, one seriously.
Probable cause:
The pilot-in-command’s failure to release the parking brake before attempting to initiate the takeoff, which produced an unexpected retarding force and airplane-nose-down pitching moment that prevented the airplane from becoming airborne within the takeoff distance available and not before the end of the airport terrain. Contributing to the accident were the airplane’s lack of a warning that the parking brake was not fully released and the Federal Aviation Administration’s process for certification of a derivative aircraft that did not identify the need for such an indication.
Final Report:

Crash of a Boeing B-17G-30-BO Flying Fortress in Windsor Locks: 7 killed

Date & Time: Oct 2, 2019 at 0953 LT
Operator:
Registration:
N93012
Flight Type:
Survivors:
Yes
Schedule:
Windsor Locks - Windsor Locks
MSN:
7023
YOM:
1942
Crew on board:
3
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
14500
Captain / Total hours on type:
7300.00
Copilot / Total flying hours:
22000
Copilot / Total hours on type:
23
Aircraft flight hours:
11388
Circumstances:
The vintage, former US military bomber airplane was on a tour that allowed members of the public to purchase an excursion aboard the airplane for an LHFE flight. The accident flight was the airplane’s first flight of the day. During the initial climb, one of the pilots retracted the landing gear, and the crew chief/flight engineer (referred to as the loadmaster) left the cockpit to inform the passengers that they could leave their seats and walk around the airplane. One of the pilots reported to air traffic control that the airplane needed to return to the airport because of a rough magneto. At that time, the airplane was at an altitude of about 600 ft above ground level (agl) on the right crosswind leg of the airport traffic pattern for runway 6. The approach controller asked the pilot if he needed any assistance, to which the pilot replied, “negative.” When the loadmaster returned to the cockpit, he realized that the airplane was no longer climbing, and the pilot, realizing the same, instructed the copilot to extend the landing gear, which he did. The loadmaster left the cockpit to instruct the passengers to return to their seats and fasten their seat belts. When the loadmaster returned again to the cockpit, the pilot stated that the No. 4 engine was losing power; the pilot then shut down that engine and feathered the propeller without any further coordination or discussion. When the airplane was at an altitude of about 400 ft agl, it was on a midfield right downwind leg for runway 6. Witness video showed that the landing gear had already been extended by that time, even though the airplane still had about 2.7 nautical miles to fly in the traffic pattern before reaching the runway 6 threshold. During final approach, the airplane struck the runway 6 approach lights in a right-wing-down attitude about 1,000 ft before the runway and then contacted the ground about 500 ft before the runway. After landing short of the runway, the airplane traveled onto the right edge of the runway threshold and continued to veer to the right. The airplane collided with vehicles and a deicing fluid tank before coming to rest upright about 940 ft to the right of the runway. A postcrash fire ensued. Both pilots and five passengers were killed and all six other occupants as well as one people on the ground were injured, five seriously.
Probable cause:
The pilot’s failure to properly manage the airplane’s configuration and airspeed after he shut down the No. 4 engine following its partial loss of power during the initial climb. Contributing to the accident was the pilot/maintenance director’s inadequate maintenance while the airplane was on tour, which resulted in the partial loss of power to the Nos. 3 and 4 engines; the Collings Foundation’s ineffective safety management system (SMS), which failed to identify and mitigate safety risks; and the Federal Aviation Administration’s inadequate oversight of the Collings Foundation’s SMS.
Final Report:

Crash of an Eclipse EA500 in Danbury

Date & Time: Aug 21, 2015 at 1420 LT
Type of aircraft:
Operator:
Registration:
N120EA
Flight Type:
Survivors:
Yes
Schedule:
Oshkosh – Danbury
MSN:
199
YOM:
2008
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7846
Captain / Total hours on type:
1111.00
Aircraft flight hours:
858
Circumstances:
**This report was modified on April 2, 2020. Please see the public docket for this accident to view the original report.**
After the airplane touched down on the 4,422-ft-long runway, the airline transport pilot applied the brakes to decelerate; however, he did not think that the brakes were operating. He continued "pumping the brakes" and considered conducting a go-around; however, there was insufficient remaining runway to do so. The airplane subsequently continued off the end of the runway, impacted a berm, and came to rest upright, which resulted in substantial damage to the right wing. During postaccident examination of the airplane, brake pressure was obtained on both sets of brake pedals when they were depressed, and there was no bleed down or reduction in pedal firmness when the brakes were pumped several times. Examination revealed no evidence off any preimpact anomalies with the brake system that would have precluded normal operation. In addition, the pilot indicated that he was not aware of and was not trained on the use of the ALL INTERRUPT button, which is listed as a step in the Emergency Procedures section of the airplane flight manual and is used to disable the anti-skid brake system functions and restore normal braking when the brakes are ineffective; thus, the pilot did not follow proper checklist procedures. According to data downloaded from the airplane's diagnostic storage unit (DSU), the airplane touched down 1,280 ft beyond the runway threshold, which resulted in 2,408 ft of runway remaining (the runway had a displaced threshold of 734 ft) and that it traveled 2,600 ft before coming to rest about 200 ft past the runway. The airplane's touchdown speed was about 91 knots. Comparing DSU data from previous downloaded flights revealed that the airplane's calculated deceleration rate during the accident landing was indicative of braking performance as well as or better than the previous landings. Estimated landing distance calculations revealed that the airplane required about 3,063 ft when crossing the threshold at 50 ft above ground level. The target touchdown speed was 76 knots. However, the airplane touched down with only 2,408 ft of remaining runway faster than the target touchdown speed, which resulted in the runway overrun.
Probable cause:
The pilot's failure to attain the proper touchdown point and exceedance of the target touchdown speed, which resulted in a runway overrun.
Final Report:

Crash of a Rockwell 690B Turbo Commander in New Haven: 4 killed

Date & Time: Aug 9, 2013 at 1121 LT
Registration:
N13622
Flight Type:
Survivors:
No
Site:
Schedule:
Teterboro - New Haven
MSN:
11469
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
2067
Aircraft flight hours:
8827
Circumstances:
The pilot was attempting a circling approach with a strong gusty tailwind. Radar data and an air traffic controller confirmed that the airplane was circling at or below the minimum descent altitude of 720 feet (708 feet above ground level [agl]) while flying in and out of an overcast ceiling that was varying between 600 feet and 1,100 feet agl. The airplane was flying at 100 knots and was close to the runway threshold on the left downwind leg of the airport traffic pattern, which would have required a 180-degree turn with a 45-degree or greater bank to align with the runway. Assuming a consistent bank of 45 degrees, and a stall speed of 88 to 94 knots, the airplane would have been near stall during that bank. If the bank was increased due to the tailwind, the stall speed would have increased above 100 knots. Additionally, witnesses saw the airplane descend out of the clouds in a nose-down attitude. Thus, it was likely the pilot encountered an aerodynamic stall as he was banking sharply, while flying in and out of clouds, trying to align the airplane with the runway. Toxicological testing revealed the presence of zolpidem, which is a sleep aid marketed under the brand name Ambien; however, the levels were well below the therapeutic range and consistent with the pilot taking the medication the evening before the accident. Therefore, the pilot was not impaired due to the zolpidem. Examination of the wreckage did not reveal any preimpact mechanical malfunctions.
Probable cause:
The pilot's failure to maintain airspeed while banking aggressively in and out of clouds for landing in gusty tailwind conditions, which resulted in an aerodynamic stall and uncontrolled descent.
Final Report:

Crash of a Learjet 35A off Groton: 2 killed

Date & Time: Jun 2, 2006 at 1440 LT
Type of aircraft:
Operator:
Registration:
N182K
Survivors:
Yes
Schedule:
Atlantic City - Groton
MSN:
35-293
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
18750
Captain / Total hours on type:
7500.00
Copilot / Total flying hours:
3275
Copilot / Total hours on type:
289
Aircraft flight hours:
11704
Circumstances:
The crew briefed the Instrument Landing System approach, including the missed approach procedures. Weather at the time included a 100-foot broken cloud layer, and at the airport, 2 miles visibility. The approach was flown over water, and at the accident location, there was dense fog. Two smaller airplanes had successfully completed the approach prior to the accident airplane. The captain flew the approach and the first officer made 100-foot callouts during the final descent, until 200 feet above the decision height. At that point, the captain asked the first officer if he saw anything. The first officer reported "ground contact," then noted "decision height." The captain immediately reported "I got the lights" which the first officer confirmed. The captain reduced the power to flight idle. Approximately 4 seconds later, the captain attempted to increase power. However, the engines did not have time to respond before the airplane descended into the water and impacted a series of approach light stanchions, commencing about 2,000 feet from the runway. Neither crew member continued to call out altitudes after seeing the approach lights, and the captain descended the airplane below the decision height before having the requisite descent criteria. The absence of ground references could have been conducive to a featureless terrain illusion in which the captain would have believed that the airplane was at a higher altitude than it actually was. There were
no mechanical anomalies which would have precluded normal airplane operation.
Probable cause:
The crew's failure to properly monitor the airplane's altitude, which resulted in the captain's inadvertent descent of the airplane into water. Contributing to the accident were the foggy weather conditions, and the captain's decision to descend below the decision height without sufficient visual cues.
Final Report:

Crash of a Learjet 35A in Groton: 2 killed

Date & Time: Aug 4, 2003 at 0639 LT
Type of aircraft:
Registration:
N135PT
Flight Type:
Survivors:
No
Schedule:
Farmingdale - Groton
MSN:
35-509
YOM:
1983
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4300
Copilot / Total flying hours:
9000
Aircraft flight hours:
9287
Circumstances:
About 5 miles west of the airport, the flightcrew advised the approach controller that they had visual contact with the airport, canceled their IFR clearance, and proceeded under visual flight rules. A witness heard the airplane approach from the east, and observed the airplane at a height consistent with the approach minimums for the VOR approach. The airplane continued over the runway, and entered a "tight" downwind. The witness lost visual contact with the airplane due to it "skimming" into or behind clouds. The airplane reappeared from the clouds at an altitude of about 200 feet above the ground on a base leg. As it overshot the extended centerline for the runway, the bank angle increased to about 90-degrees. The airplane then descended out of view. The witness described the weather to the north and northeast of the airport, as poor visibility with "scuddy" clouds. According to CVR and FDR data, about 1.5 miles from the runway with the first officer at the controls, and south of the extended runway centerline, the airplane turned left, and then back toward the right. During that portion of the flight, the first officer stated, "what happens if we break out, pray tell." The captain replied, "uh, I don't see it on the left side it's gonna be a problem." When the airplane was about 1/8- mile south of the runway threshold, the first officer relinquished the controls to the captain. The captain then made an approximate 60-degree heading change to the right back toward the runway. The airplane crossed over the runway at an altitude of 200 feet, and began a left turn towards the center of the airport. During the turn, the first officer set the flaps to 20 degrees. The airplane reentered a left downwind, about 1,100 feet south of the runway, at an altitude of 400 feet. As the airplane turned onto the base leg, the captain called for "flaps twenty," and the first officer replied, "flaps twenty coming in." The CVR recorded the sound of a click, followed by the sound of a trim-in-motion clicker. The trim-in-motion audio clicker system would not sound if the flaps were positioned beyond 3 degrees. About 31 seconds later, the CVR recorded a sound similar to a stick pusher stall warning tone. The airplane impacted a rooftop of a residential home about 1/4-mile northeast of the approach end of the runway, struck trees, a second residential home, a second line of trees, a third residential home, and came to rest in a river. Examination of the wreckage revealed the captain's airspeed indicator reference bug was set to 144 knots, and the first officer's was set to 124 knots. The flap selector switch was observed in the "UP" position. A review of the Airplane Flight Manual revealed the stall speeds for flap positions of 0 and 8 degrees, and a bank angle of 60 degrees, were 164 and 148 knots respectfully. There were no charts available to calculate stall speeds for level coordinated turns in excess of 60 degrees. The flightcrew was trained to apply procedures set forth by the airplane's Technical Manual, which stated, "…The PF (Pilot Flying) will call for flap and gear extension and retraction. The PNF (Pilot not flying) will normally actuate the landing gear. The PNF will respond by checking appropriate airspeed, repeating the flap or gear setting called for, and placing the lever in the requested position... The PNF should always verify that the requested setting is reasonable and appropriate for the phase of flighty and speed/weight combination."
Probable cause:
The first officer's inadvertent retraction of the flaps during the low altitude maneuvering, which resulted in the inadvertent stall and subsequent in-flight collision with a residential home. Factors in the accident were the captain's decision to perform a low altitude maneuver using excessive bank angle, the flight crews inadequate coordination, and low clouds surrounding the airport.
Final Report: