Crash of a Convair CV-240-0 at Fort Leonard Wood AFB: 30 killed

Date & Time: Aug 4, 1955 at 1223 LT
Type of aircraft:
Operator:
Registration:
N94221
Survivors:
No
Schedule:
Tulsa – Joplin – Springfield – Saint Louis – New York
MSN:
40
YOM:
1948
Flight number:
AA476
Crew on board:
3
Crew fatalities:
Pax on board:
27
Pax fatalities:
Other fatalities:
Total fatalities:
30
Captain / Total flying hours:
15540
Captain / Total hours on type:
5000.00
Copilot / Total flying hours:
8500
Copilot / Total hours on type:
2500
Aircraft flight hours:
14865
Circumstances:
Flight 476 of August 4 was a scheduled operation between Tulsa, Oklahoma, and La Guardia Field, New York, with several intermediate stops including Joplin, Springfield, and St. Louis, Missouri. The flight departed Tulsa at 1006 (one minute behind schedule) with Captain Hugh C. Barren, First Officer William G. Gates, and Stewardess Thelma R. Ballard as crew. En route stops were made at Joplin and Springfield, and no discrepancies were reported or noted at either point. However, a traffic delay in the Joplin area resulted in the flight arriving and departing Springfield 21 minutes behind schedule. Two of the eight passengers deplaned at Springfield, 21 passengers boarded the flight there. Gross weight of the aircraft at takeoff was 38,663 pounds, 2,302 pounds under that allowable, and the center of gravity was located within prescribed limits. Flight 476 departed Springfield VFR for St. Louis, its next scheduled stop, at 1153 via Victor Airway 14 to cruise at 7,000 feet. It was off the ground at 1156. Twenty-one minutes later (1217) the crew initiated a general call asking, "Does anyone read 476?" Springfield company radio acknowledged but received no reply. Two other American Airlines flights, one cruising in the vicinity of Springfield at 7,000 feet, the other 30 miles north-northeast of St. Louis, heard a transmission from Flight 476 that No. 2 engine was on fire. This message was also heard by American's ground station at St. Louis. Three minutes later the American flight in the Springfield area intercepted the following message, "Springfield, are you reading 476? We have bad engine fire." This was the last message heard from the flight. All transmissions were on company frequency. During this interval numerous witnesses on the ground back along the flight path saw the aircraft with smoke and flame coming from the right engine. The aircraft was also tracked by a military radar installation near Springfield until it disappeared from the scope in the vicinity of Fort Leonard Wood. At approximately 1222 the operations officer on duty at Forney Field, Fort Leonard Wood, received a radio message from an Army pilot flying nearby that a two-engine aircraft with a fire in the right engine was on final approach to runway 14. The tower operator at Forney Field saw the approaching aircraft and gave it clearance to land. Before the operations officer could alert the crash crew another call from the Army pilot informed him that the airplane had crashed short of the runway. The time was 1223. Army personnel with portable fire-fighting equipment reached the wreckage on foot. There were no survivors. Heavy fire-fighting equipment and ambulances could not reach the scene until the Army engineers had bulldozed a road through the densely wooded area in which the crash occurred.
Probable cause:
The Board determines that the probable cause of this accident was installation of an unairworthy cylinder, the failure of which resulted in an uncontrollable fire and subsequent loss of a wing in flight. The following findings were reported:
- Weather was not a factor,
- N° 12 cylinder of the right engine was not airworthy and failed near its base after less than six hours of operation, causing a fire that the crew could not control,
- Visual inspection procedures being used by the carrier did not reveal the unairworthy condition of the cylinder,
- The right main tank fuel shutoff valve was open, which greatly increased the intensity and duration of the fire,
- Fire damage prevented the closing of this valve,
- Procedures recommended by the manufacturer and specified in the carrier's overhaul manual had been countermanded by verbal instructions approved by the carrier's engineering department and were not being followed by the carrier's inspectors with respect to the handling of cylinders.
Final Report:

Crash of a Convair CV-240-0 in Springfield: 13 killed

Date & Time: Mar 20, 1955 at 2236 LT
Type of aircraft:
Operator:
Registration:
N94234
Survivors:
Yes
Schedule:
Newark – Chicago – Saint Louis – Springfield – Tulsa
MSN:
66
YOM:
1948
Flight number:
AA711
Crew on board:
3
Crew fatalities:
Pax on board:
32
Pax fatalities:
Other fatalities:
Total fatalities:
13
Captain / Total flying hours:
9670
Captain / Total hours on type:
1324.00
Copilot / Total flying hours:
1922
Copilot / Total hours on type:
2
Aircraft flight hours:
13383
Circumstances:
American 711 reported en route to the company that it was over Vichy (a position along Victor Airway 14 about 100 miles from Springfield) and estimated it would reach the Springfield VOR station at 2233. Initial radio contact with Springfield Approach Control was established at 2218 and the flight gave it the same Springfield estimate. The approach controller transmitted the 2208 weather observation to the flight. Reported conditions were: Ceiling 400 feet overcast; visibility 10 miles; wind west 12; altimeter 29.68. In response to the controller’s question the flight then indicated it intended to land at Springfield. Immediately thereafter clearance was issued for a standard range approach, instructing flight 711 to report over the range station and when starting the procedure turn. Shortly thereafter the flight asked clearance to descend. There being no other traffic the controller cleared the flight for an approach and to descend whenever it wished. At 2229 the latest weather observation for the airport, completed at 2228, was transmitted to the flight. Conditions given were: Ceiling 500 feet overcast; visibility 8 miles, very light drizzle; wind west 10. The flight informed the controller it would make a circling approach to runway 31, the active runway. At 2234 the flight reported, “American 711, over the Omni at 34, proceeding to the field.” Approximately two minutes later an explosion was seen and heard north-northwest of the airport and attempts to contact the flight thereafter failed. The aircraft crashed about 0,25 miles short of runway 31 and was destroyed. Both pilots and 11 passengers were killed. A weather observation immediately following the accident was: Ceiling 500 feet overcast; visibility 5 miles, very light drizzle; wind northwest 8; altimeter 29.66.
Probable cause:
The Board determines that the probable cause of this accident was a descent to the ground while approaching the airport caused by the crew’s inattention to their flight instruments and a possible sensory illusion giving them an erroneous impression of the attitude of the aircraft. The following findings were reported:
- Weather conditions at Springfield were above the minimums for an American Airlines Convair aircraft to make a VOR instrument approach and to circle for the landing,
- The flight did not execute the CAA approved VOR instrument approach procedure but proceeded directly from the station toward the airport,
- Analysis of the existing weather conditions indicates that before the aircraft turned toward the airport visual reference with the ground was possible but not probable at the required altitude,
- While approaching the airport the aircraft was nearly on the 193-degree inbound radial required by the VOR instrument approach procedure and was flown visually below the overcast for several miles,
- The aircraft descended until it struck the ground approximately 1-1/14 miles north-northwest of the airport,
- There was no evidence found indicating malfunction or failure of the aircraft and there was no indication of an emergency aboard the aircraft.
Final Report:

Crash of a Convair CV-240-0 in Buffalo

Date & Time: Jan 20, 1954 at 1642 LT
Type of aircraft:
Operator:
Registration:
N94244
Flight Phase:
Survivors:
Yes
Schedule:
Buffalo – Saint Louis
MSN:
88
YOM:
1948
Flight number:
AA767
Crew on board:
3
Crew fatalities:
Pax on board:
21
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8671
Captain / Total hours on type:
4389.00
Copilot / Total flying hours:
4249
Copilot / Total hours on type:
2082
Aircraft flight hours:
11018
Circumstances:
While taxiing to Runway 23 the flight received an IFR (Instrument Plight Rules) clearance from ARTC (Air Route Traffic Control). Normal pre-takeoff checks were performed and the takeoff roll was started at 1640. The aircraft became airborne after using approximately one-half of the 5.630-foot runway. Immediately after leaving the ground the gear was raised and the first officer saw the left feathering button light come on dimly which indicated that the left propeller was in the process of being feathered by the auto-feathering system. After definitely determining the light was on and visually checking the left propeller, the auto-feathering system was disarmed and the captain., in an effort to stop the feathering cycle, pulled the feathering button to neutral. This effort was unsuccessful. the left propeller feathered, and the engine stopped. During the climb an air speed of 140 m.p.h. was reached and maintained., the right engine remaining at full takeoff power. Approximately 250 feet above the ground a shallow left turn was started and the first officer was ordered to reinstate the left engine. the captain believing the aircraft would climb no farther. In the effort to restart the left engine by unfeathering the left propeller. only 600 r.p.m. could be obtained and the captain felt a buffeting through the control yoke. The aircraft at this time had progressed in the left turn approximately 180 degrees from the takeoff direction and the captain. fearing he would be unable to clear obstructions. Including high tension lines, decided to make a wheels-up landing. The landing was made in a field approximately one mile south of the airport. When the aircraft stopped, the passengers and crew evacuated it in an expeditious and orderly manner. The airplane was damaged beyond repair.
Probable cause:
The Board determines that the probable cause of this accident was (1) a mechanical failure of the torquemeter boost pump that automatically feathered the left propeller immediately after becoming airborne., and (2) the use of an incorrect procedure for unfeathering which resulted from the ambiguity of the instruction for unfeathering contained in the company's manual. The following findings were reported:
- Immediately after takeoff the left propeller automatically feathered due to a mechanical failure of the torquemeter boost pump,
- The engine stopped as a result of the feathering and was capable of being restarted,
- The procedure used to unfeather the propeller and reach starting r.p.m. was incorrect due to an ambiguity of the unfeathering instructions outlined in the flight manual,
- The first officer did not reinstate the mixture control to "auto-rich" because starting r.p.m. was not reached,
- The windmilling propeller drag. the existing weather and the banked attitude of the aircraft caused it to lose altitude,
- A forced landing was made one mile south of the Buffalo Airport shortly after becoming airborne.
Final Report:

Crash of a Convair CV-240-0 in Albany: 28 killed

Date & Time: Sep 16, 1953 at 0834 LT
Type of aircraft:
Operator:
Registration:
N94255
Survivors:
No
Schedule:
Boston – Hartford – Albany – Chicago
MSN:
116
YOM:
1948
Flight number:
AA723
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
25
Pax fatalities:
Other fatalities:
Total fatalities:
28
Captain / Total flying hours:
7500
Captain / Total hours on type:
2000.00
Copilot / Total flying hours:
1400
Copilot / Total hours on type:
215
Aircraft flight hours:
9920
Circumstances:
American Airlines' Flight 723 of September 16, 1953, was a scheduled operation between Boston Massachusetts, and Chicago, Illinois, with intermediate stops among which were Hartford, Connecticut, and Albany, New York. The crew consisted of Captain J. W. Stentz, First Officer W. J. Schanken, and Stewardess J. G. Thornquist, Prior to departing Boston the crew filed a company VFR (Visual Flight Rules) flight plan to Chicago following which the company issued a flight clearance to proceed to Albany INSTOP (Instrument or On Top of Clouds Authorize d) 2 with an intermediate landing at Bradley Field, the airport serving Hartford, Connecticut, and Springfield, Massachusetts. The alternate airport was Syracuse, New York. At the time this flight clearance was issued, the weather en route to Albany was good mid the conditions at Albany were above minimums. The portion of the flight to Bradley Field was without incident and the aircraft arrived there at 0657. At Bradley Field Captain Stentz reviewed the latest weather reports in the company's operations office and was advised that Bradley Field had been added to his flight clearance as a second alternate in addition to Syracuse because the weather at Albany at this time was below the company's landing minimums 3 was forecast to improve to within limits by the time the flight arrived there. The special Albany 0642 weather report available to the captain at this time was: ceiling indefinite zero, sky obscured, visibility zero, fog. The en route weather was clear. According to the company's records, the gross takeoff weight of the aircraft at Hartford was 37,889 pounds which was within the allowable gross take-off weight of 40,503 pounds; the load was properly distributed with respect to the center of gravity limits of the aircraft. Departure from Bradley Field was made at 0714 with 25 passengers. Immediately before departing, the flight advised the tower it was proceeding to Albany VFR. At 0737, a message from the company's dispatcher at New York was relayed to Captain Stentz through the company radio at Albany as follows: "If Albany still below limits on your arrival, if OK with you, suggest hold vicinity until at least 0830 EST. Expect Albany to have limits 0730-0800 EST. Advise fuel on board when over Albany." Flight 723 acknowledged and advised. "We will hold." At 0740, the flight reported to Albany Approach Control that it was over Montgomery Ward, an in-range visual check point, VFR, and requested a clearance of at least 500 feet on top of clouds to the Albany Range Station. This request was approved and the flight was cleared to maintain at least 500 feet on top and to hold north of the Range Station. The 0739 Albany special weather report was given the flight: "Ceiling indefinite, 100 feet, sky obscured, visibility 1/4 mile, fog, wind west-southwest one mile per hour." Flight 723 reported aver the Range Station at 0742. During the holding period the number of aircraft in this pattern varied from six to nine. The special Albany weather report issued at 0750 indicated thin obscurement, ceiling estimated 4,000, overcast, fog, visibility 3/4 miles. At 0753, the first of the aircraft in the holding pattern, American Airlines' Flight 750, was cleared for an instrument approach to Runway 19. At 0800, this aircraft missed its approach and was immediately cleared to climb toward the south and to again remain at least 500 feet on top of clouds. A second aircraft which was holding was then cleared to make a similar approach and it too was forced to execute a missed approach procedure. At 08163 an instrument approach mid a landing on Runway 19 were successfully completed by one of the holding aircraft. Immediately following this landing. Flight 723 was cleared to make an instrument approach to Runway 19. Three minutes later the flight advised the tower that its approach was being abandoned because the aircraft's flaps could not be lowered. It was then still at least 500 feet on top of clouds and was advised by the tower to remain there until further advised. At approximately 0830, the following message was transmitted from the Albany Tower: "All aircraft holding Albany. It now appears to be pretty good for a contact approach from the west. It looks much better than to the north." Immediately following this message, Flight 723 was asked by the tower if it would accept a contact approach from the west for a landing on Runway 10. After requesting and receiving current weather including altimeter setting (29.74) and the length of Runway 10 (4,500 feet). the flight stated it would accept a contact approach. Clearance was then issued the flight to make a contact approach to Runway 10. Acknowledgement of this clearance was the last radio contact with the flight. At approximately 0834, Flight 723 struck the radio towers and crashed. The weather reported at the time of the accident was thin scattered clouds at 500 feet, ceiling estimated 4,500 feet, broken clouds, visibility 1-1/2 miles, fog.
Probable cause:
The Board determines that the probable cause of this accident was that during the execution of a contact approach, and while maneuvering for alignment with the runway to be used, descent was made to an altitude below obstructions partially obscured by fog in a local area of restricted visibility. The following findings were reported:
- Upon arrival of the flight, Albany weather was below authorized landing minimums and the aircraft was required to hold,
- A standard instrument approach was started and later abandoned because of mechanical failure of the wing flap mechanism,
- A contact approach to Runway 10 was later accepted because improved weather, especially to the west of the airport, made this runway most feasible,
- The aircraft made a wide right turn southwest of the airport to align with Runway 10,
- The latter part of the approach was at low altitude through weather conditions which prevented adequate visual reference,
- Under existing conditions the pilot should have abandoned the approach,
- The aircraft struck radio towers, the upper portions of which were obscured by fog,
- These towers were hazard-painted and lighted in accordance with accepted standards,
- All CAA navigational and landing facilities were functioning properly,
- No evidence was found in the residual wreckage not destroyed by impact or fire to indicate that structural or mechanical failure occurred prior to impact other than to the wing flap mechanism.
Final Report:

Crash of a Convair CV-240-0 in Elizabeth: 30 killed

Date & Time: Jan 22, 1952 at 1544 LT
Type of aircraft:
Operator:
Registration:
N94229
Survivors:
No
Site:
Schedule:
Buffalo – Rochester – Syracuse – Newark
MSN:
54
YOM:
1948
Flight number:
AA6780
Crew on board:
5
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
30
Captain / Total flying hours:
7062
Captain / Total hours on type:
2483.00
Copilot / Total flying hours:
2174
Copilot / Total hours on type:
405
Aircraft flight hours:
6633
Circumstances:
The approach to Newark was completed in marginal weather conditions with a ceiling at 400 feet and a 3/4 mile visibility. For unknown reason, the aircraft deviated from the approach path to the left and, in a relative flat attitude, hit an obstacle and eventually crashed in flames on several houses located in the city of Elizabeth, about three miles from runway 06 threshold. All 23 occupants on board the aircraft and seven people in the ground were killed while nine others were injured. Few houses were destroyed.
Probable cause:
The Board determines that there is insufficient evidence available at this time upon which to predicate a probable cause. The following findings were pointed out:
- The flight was routine from Buffalo and was cleared to descend and make an ILS approach, monitored by GCA, to the Newark airport,
- Weather conditions below the 4,000-foot level at Newark were favorable to the formation of carburetor ice,
- The flight reported over Linden, New Jersey, at 1,500 feet inbound to the airport at 1541,
- The Newark weather conditions at 1540 were reported as indefinite ceiling 400 feet, obscurement, visibility 3/4 mile, light rain and fog, altimeter 29 97,
- The aircraft vanished from the GCA screens at a point approximately 900 feet to the right of the glide path and while at an altitude of 400 feet, due to ground interference,
- The weather information indicated lower ceilings and visibilities near the scene of the accident (about three miles southwest of the airport) than were reported at the airport,
- The aircraft was headed in an easterly direction, below the overcast, in a near level attitude, for a distance of approximately 1,300 feet, before it crashed into buildings.
Final Report:

Crash of a Douglas DC-6 in Dallas: 28 killed

Date & Time: Nov 29, 1949 at 0549 LT
Type of aircraft:
Operator:
Registration:
N90728
Survivors:
Yes
Schedule:
New York – Washington DC – Dallas – Mexico City
MSN:
42895
YOM:
1947
Flight number:
AA157
Crew on board:
5
Crew fatalities:
Pax on board:
41
Pax fatalities:
Other fatalities:
Total fatalities:
28
Aircraft flight hours:
5260
Circumstances:
Flight 157 originated at LaGuardia Field, New York, for Mexico City, Mexico, with stops scheduled at Washington, D C., and Dallas, Tex. Departure from LaGuardia was at 2147, November 28 Between LaGuardia and Washington the flight was reported to be uneventful with all of the aircraft's components functioning normally. At Washington, a flight plan was filed with, and approved by, Airway Route Traffic Control It specified Instrument Flight Rules to Dallas, with Wichita Falls, Tex, as the alternate, a cruising altitude of 18,000 feet, and a flight time of 5 hours and 4 minutes The gross height of the aircraft at takeoff was 82,298 pounds, which was 3,577 pounds less than the maximum allowable gross weight of 85,875 pounds, and the disposable load was distributed so that the center of gravity was within prescribed limits. At 0206 the flight requested and received permission to change its flight plan to Visual Flight Rules A posit-,on report was made over Nashville at 16,000 feet at 0254 and a descent was started to 6,000 feet When approaching Nashville, 1 No 1 engine had started backfiring at intervals of about 20 seconds Various corrective measures, including the application of alcohol and carburetor heat, and the richening of fuel mixture, were applied but were not successful and the backfiring continued. The captain and the flight engineer discussed the malfunctioning following which No 1 engine was feathered at a point about 25 miles southwest of Nashville at approximately 0300, however, the feathering was not reported to the company until 0429, where the flight was in the vicinity of Altheimer, Ark, a routine position reporting point about 125 miles beyond Memphis At that time, the crew advised a change of aircraft on arrival at Dallas. When 15 miles northeast of Dallas, at 0536, the flight was given permission to enter the traffic pattern at Love Field, Dallas, with a right-hand turn and instructed to land on Runway 36 The altimeter setting of 29 83 inches and the weather, which included unlimited ceiling, a visibility of 15 miles and a north-northeast wind of 5 mph, were given the flight The captain and the flight engineer conferred regarding returning No 1 engine to service and decided against doing so. The crew then went through the pre-landing cheek The landing lights were turned or and the Plans were lowered to the 20 degree position. The flight turned -flight to final approach when approximately over the Range Station which is 2 2 miles south of the approach end of Runway 36 At this time its altitude was estimated to be 1200 feet AFL 2 by the captain and 800 feet AFL by the first officer At a distance of about 1 1/2 miles from the approach end of the runway, the landing gear was extended. Shortly thereafter the flaps were extended fully, the turn to final placed be aircraft to the left of the runway Accordingly an "S" turn was made to correct the misalignment During this "S" turn the aircraft skidded to Its left, the air speed dropped abruptly and the aircraft settled rapidly. At this point the captain increased power to engines Nos. 2, 3 and 4 in an attempt to maintain control. Control tower operators watching the approach estimated that the aircraft cleared by 75 to 100 feet obstruction lights mounted on 30-foot poles on a power line located 800 feet south of the approach end of the runway. The aircraft continued in a generally northwest direction, across the airport on a heading about 40 degrees to the left of Runway 36, in a tail low attitude. Its air speed continued to fall, its attitude became increasingly nose-high. and a stall developed just prior to striking a hangar and other buildings on the northwest side of the airport. Both pilots and 26 passengers were killed.
Probable cause:
It was determined that the accident was caused by a faulty execution of an engine-out approach on part of the crew.
The following findings were noted:
- The captain failed to align the aircraft with the runway centerline after the final turn,
- After realizing the misalignment, the captain attempted to correct it with a risky "S"-turn at low altitude. There is little room for error if a problem arises during this maneuver because as the angle of the bank increases, so does the probability of stalling the airplane,
- The crew made no attempt to balance the airplane’s fuel load after the No. 1 engine failed. The DC-6 is equipped with four main fuel tanks that serve individual engines, while a network of valves allow fuel to be transferred from one engine’s tank to feed other engines. The crew did not cross feed fuel from the tank serving the failed engine to balance the plane's weight as recommended in the flight operations manual. Flight 157 had flown for almost three hours with the No. 1 engine out, and the CAB concluded that the No. 1 main fuel tank was holding about 1,400 lbs (635 kg) more gasoline than the other three main tanks when the plane arrived at Love Field. The investigators primarily attributed the left wing’s sharp drop to the excessive weight of the fuel at its outboard end,
- The captain applied excessive rudder during the “S”-turn, causing a condition known in aviation terminology as a skid. This maneuver would have caused the plane’s airspeed to drop, and according to the CAB findings, it caused the fuel in the No. 4 main tank to slosh away from the fuel outlet, lowering the engine’s fuel pressure,
- The captain’s application of full throttle to both right-hand engines caused to airplane to turn further to the left due to the relative lack of thrust from the single functioning left-hand engine. This exacerbated his loss of directional control,
- The first officer disobeyed the captain’s order to raise the wing flaps, and did not tell the captain,
- The first officer misinterpreted the No. 4 engine’s fuel pressure drop as a sign of incipient engine failure and feathered the prop. However, the CAB partially exonerated Lewis for this act, concluding that the craft was so close to the ground at that point that his mistake probably had little influence on the final outcome,
- Excessive elevator input by the captain caused the aircraft to stall.
The CAB concluded that the accident could have been avoided if the crew had held the plane straight and level when the misalignment was first noticed, then raised the flaps, climbed to a safe altitude, circled the airport, and attempted another landing. The CAB concluded that there were no factors present that would compel the crew to land immediately despite the sloppy approach, such as rapidly deteriorating weather or a shortage of fuel.
Final Report:

Crash of a Convair CV-240-0 in Memphis

Date & Time: Jun 22, 1949 at 1313 LT
Type of aircraft:
Operator:
Registration:
N94266
Flight Phase:
Survivors:
Yes
Schedule:
Dallas – Texarkana – Little Rock – Memphis – Washington DC
MSN:
139
YOM:
1949
Flight number:
AA402
Crew on board:
3
Crew fatalities:
Pax on board:
41
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8239
Captain / Total hours on type:
469.00
Copilot / Total flying hours:
7077
Copilot / Total hours on type:
135
Circumstances:
After 2.700 feet of takeoff roll the aircraft became airborne with an estimated air speed of 120 miles per hour, but at an altitude from 20 to 50 feet the right engine failed and the right propeller automatically feathered. Retraction of the landing gear was accomplished after momentary hesitation as the flight continued straight ahead, gaining altitude very slowly. It passed over the end of the runway at about 50 feet. A power transmission line, 11,700 feet from the start of the takeoff roll. was located across the flight's course. Two towers of this transmission line between which the aircraft was flown extended to an elevation of 371 feet, or a height of 111 feet above the southwest end of Runway 2 from where the takeoff was started. Elevation of the lowest point of the top series of wires as they hung between the two towers was 335 feet or 75 feet above the southwest end of Runway 2. The flight cleared these wires at this lowest point by 10 to 20 feet. Just before flying over the power lines at an air speed of 110 miles per hour, a slow retraction of the flaps was started. After crossing the power lines, the air speed fell to 105 miles per hour even though the left engine continued to develop full takeoff power. Not being able to hold altitude, a shallow right turn was made to relatively clear terrain where the aircraft was crash landed 18,713 feet northeast from the starting point of the takeoff. The aircraft slid over the ground for a distance of 217 feet, skidded over an embankment and a highway, then came to rest. Control tower personnel had observed the feathering of the right propeller and the slow rate of climb. Feeling that the aircraft would not remain airborne, the airport controller instructed another air carrier flight, then on a landing approach to Memphis, to circle the Convair so as to keep the tower advised of its position. Instructions were immediately transmitted to the field's fire and crash personnel following which the city fire and police departments and hospitals were notified. Since fire and crash equipment had actually been dispatched while the aircraft was still in flight, it arrived only two or three minutes after the crash. Fire which started in the left engine nacelle after landing was quickly extinguished, and prompt medical attention was available for all occupants. Although the stewardess had received minor injuries, she, with the aid of one of the passengers, had opened two emergency exits. She had then deplaned all passengers. Thirteen passengers and one crew member received serious injuries, and 18 passengers and two crew members received minor injuries.
Probable cause:
The Board determines that the probable cause of this accident was a reduction in air speed resulting from flying the aircraft at a steep climbing attitude after power failure of the right engine. followed by retraction of the flaps which destroyed the aircraft's climb performance.
The following factors were considered as contributory:
- Failure of the right engine resulted from failure of the impeller shaft thrust bearing which caused the flow of fuel into the induction system of the right engine to be interrupted,
- Retraction of the landing gear was accomplished shortly after failure of the right engine,
- The left engine developed full takeoff power continuously during takeoff and climb,
- The manner in which the flaps were to be used under emergency conditions was left to the captain's discretion and was not specifically pointed out in the manual of operation,
- The aircraft was flown 10 to 20 feet over wires which were 75 feet above and 11,700 feet from the point of takeoff,
- Just before flying over the wires and at an air speed of 110 miles per hour, flaps were slowly but fully retracted from the takeoff position of 16 degrees,
- After crossing the wires, the air speed fell to 105 miles per hour.
Final Report:

Crash of a Douglas C-54B-1-DC Skymaster in Dallas

Date & Time: Mar 10, 1948
Type of aircraft:
Operator:
Registration:
N90426
Survivors:
Yes
Schedule:
Tulsa – Los Angeles
MSN:
10433
YOM:
1944
Crew on board:
3
Crew fatalities:
Pax on board:
33
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll in Tulsa, the nose gear hit a snowdrift. After departure, during initial climb, the crew was unable to raise the nose gear so the captain decided to divert to Dallas-Love Field for a safe landing. After touchdown, the aircraft slid on its nose and came to rest. There were no casualties but the aircraft was written off.
Probable cause:
Collision with a snowdrift on takeoff.

Crash of a Douglas DC-6 in Gallup

Date & Time: Nov 11, 1947
Type of aircraft:
Operator:
Registration:
NC90741
Survivors:
Yes
Schedule:
San Francisco – Chicago
MSN:
43046
YOM:
1947
Crew on board:
5
Crew fatalities:
Pax on board:
20
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9747
Captain / Total hours on type:
435.00
Copilot / Total flying hours:
3572
Copilot / Total hours on type:
417
Aircraft flight hours:
142
Circumstances:
Enroute from San Francisco to Chicago, the crew informed ATC that a fire erupted in the rear compartment of the aircraft and decided to divert to Gallup Airport for an emergency landing. The aircraft was difficult to maneuver and landed in flames. After it came to a halt, all 25 occupants were quickly disembarked and helped by local rescuers before the aircraft being totally destroyed by fire.
Probable cause:
The Board determines that the probable cause of these accidents was the combustion of gasoline which had entered the cabin heater combustion air intake scoop from the No 3 alternate tank vent due to inadvertent overflow during the transfer of fuel from the No 4 alternate tank.
The failure of the manufacturer and the Civil Aeronautics Administration to exercise full caution in the analysis of the fuel system of the DC-6 relative to proper location of fuel tank vents to provide non-hazardous location for fuel drainage, as required by existing regulations, and the insufficient attentiveness on the part of the manufacturer, the Civil Aeronautics Administration, and the air carriers to the procedures of fuel management employed by pilots operating DC-6 aircraft, were contributing factors.
This case was categorized as similar as the United Airlines' DC-6 that crashed in Bryce Canyon on October 24, 1947, killing all 52 occupants.
Final Report:

Crash of a Douglas DC-3C off New York-La Guardia: 3 killed

Date & Time: Aug 8, 1947 at 1849 LT
Type of aircraft:
Operator:
Registration:
NX88787
Flight Type:
Survivors:
Yes
Schedule:
New York – Rochester
MSN:
19639
YOM:
1944
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
4934
Captain / Total hours on type:
2000.00
Copilot / Total flying hours:
4760
Copilot / Total hours on type:
1500
Aircraft flight hours:
2035
Circumstances:
The aircraft took off on runway 13 of La Guardia Airport at 1843LT, having been cleared on an instrument flight plan to Rochester, New York, with Toronto, Ontario, as an alternate. Approximately 2 minutes after take-off the flight called La Guardia Tower and reported that it was in the vicinity of the south end of Whitestone Bridge, approximately 2 1/2 miles northeast of La Guardia Airport. The flight advised that the oil pressure was low on one engine, and requested clearance to land on runway 22. The request was approved, and the tower informed the crew that the wind was calm. When asked if emergency equipment was desired to stand by, the flight replied in the negative. Shortly thereafter, NX88787 reported that it was on the final approach, and that it was over the sand barges, located approximately one-half mile off the approach end of runway 22. In reply the flight was again given clearance to land. The aircraft was first seen at an altitude of approximately 800 feet, and about 1,300 feet off the approach end of runway 22 with the landing gear extended. The flaps were lowered, and the aircraft started a steep descent to runway 22,but it passed over the approach end of the runway at an altitude of approximately 300 feet. The flight then requested and was granted permission by the tower to make a right turn, however, the aircraft continued straight ahead over the runway, gradually losing altitude. When one-third of the way down the runway, the right propeller was feathered. When over the intersection of runways 22 and 18 and at an altitude of 200 feet the flaps were raised, which resulted in an additional loss of altitude. During or directly after raising the flaps, a right turn was initiated, and the landing gear was observed to retract slowly. Competent witnesses stated that the right turn was made at a very slow speed, at a high angle of attack, and at an altitude appearing never to have exceeded 200 feet. Over Bowery Bay the aircraft on two occasions almost settled into the water. When in a flat right turn toward runway 13 it lost altitude to about 50 feet. Approximately 2,000 feet from the end of the runway, the landing gear started to extend, and became fully extended when the aircraft was aligned with runway 13. At this time the airplane attitude appeared to be that of a steep climb. The wings were seen to wobble slightly, then the left wing and nose dropped, and the airplane struck the water at an angle of approximately 20 degrees. The forward movement of the aircraft continued on the surface of the water for 40 to 50 feet, throwing up a great spray as the tail rose to a vertical position, after which the aircraft continued over on its back and sank in about 5 minutes.
Probable cause:
The Board determines that the probable cause of this accident was that, following an attempted landing, a miss-approach procedure was attempted for a second landing without sufficient air speed for single engine operation.
The following factors were considered as contributory:
- The oil screen cover plate gasket on the right engine was either fractured when installed immediately prior to the flight of August 8, 1947, or failed during the initial part of that flight,
- As a result of the fractured oil screen cover plate gasket, oil pressure for the right engine dropped below normal, and the crew feathered the right propeller,
- Insufficient air speed was maintained in a landing approach to runway 13 at the La Guardia Airport, after an attempted landing and "go around" had been made on runway 22, and as a result the airplane stalled and crashed into Bowery Bay.
Final Report: