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Crash of a De Havilland DHC-2 Beaver in Lake Monduran: 3 killed

Date & Time: Dec 5, 1988 at 1200 LT
Type of aircraft:
Operator:
Registration:
VH-BSL
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bundaberg - Bundaberg
MSN:
1618
YOM:
1966
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The aircraft reported departing Bundaberg for Monduran Dam on a no SAR flight at 1135 hrs EST with three persons on board and an endurance of 270 minutes. The purpose of the flight was to complete the endorsement of the pilot under check and to assess the suitability of an area of water on the coast to where the passenger, who was the regular pilot of the aircraft, was to fly the aircraft the following day. The pilot in command had flown 27 hours in the previous three months, of which 9 were on type. The pilot under check had flown only one hour in the last three months. This flight had been in VH-BSL. At approximately 1200 hrs, the aircraft was observed in the Lake Monduran area. It flew two left hand circuits, landing into wind towards the dam wall each time. After the second takeoff, it turned left and was seen heading north from the lake. Nothing further was heard or seen of the aircraft. Following an extensive search, the wreckage was located six days later lying inverted in 15 metres of water approximately 2 km WNW of the dam wall in the area of the junction of the main east-west channel and a northsouth channel of the lake. Both floats had separated from the aircraft and the right float was severely torn for about half its length. There was substantial water impact damage to the windshield frame/cockpit roof area and to the upper leading edge surfaces of both wings.
Probable cause:
No fault was found with the aircraft or its systems which might have contributed to the accident. It could not be determined who was manipulating the controls of the aircraft at the time of the accident. Evidence was obtained that it was the habit of the check pilot to have pilots undergoing endorsement or check to fly two circuits landing into wind and then to carry out crosswind landings. The check pilot and the pilot under check had previously operated at the dam and alighted on to both the east/west and the north/south channels. Having been observed to fly two into wind circuits and then head north and not be sighted again, it is possible that the aircraft then commenced crosswind operations onto the north/south arm of the lake, landing in a southerly direction with a crosswind from the left. Information from the Bureau of Meteorology indicated that the surface wind in the area at the time of the accident was 090` magnetic at 15 knots. This information was confirmed by witnesses at the dam wall who observed white caps on the surface of the dam. The north/south channel of the lake was bounded on its east side by steep hills rising to 70 metres above water level. The effect of this high ground was to partially blanket the north/south channel from the easterly wind. The position of the wreckage was in the area where the wind shadow effect would have ended and where the wind would have blown at full strength along the main east/west channel of the lake. The crosswind limitation for the aircraft as stated in the flight manual was 8.7 knots. Commenting in early 1988 on an enquiry regarding the raising of this limit, the aircraft manufacturer emphasised the 8.7 knot limit and advised that any test work to raise the limit should proceed cautiously starting at or below the current (8.7 knot) limit. If the aircraft was conducting crosswind operations in the north/south channel, and suddenly encountered a 15 knot crosswind on exiting the wind shadow area, the control difficulties confronting the pilot could have been significant. The aircraft wreckage was intact except for the floats which had been torn off by water impact forces. The right float was severely damaged while the left was intact. The forward tip of the right float had been severed by the propeller. The remaining forward section had then been forced upwards and outboard and had broken off. This weakened the float support structure, causing it to fail, and allowing the remaining section of the right float to strike the right side of the fuselage just aft of the cabin. Damage of this type an magnitude was most probably caused by the nose of the right float digging into the surface of the lake at relatively high speed. For this to occur, the aircraft was banked to the right at float impact - a possible consequence of encountering a strong crosswind from the left. There was no evidence that the aircraft had hit a submerged object. The factors associated with the development of this accident could not be determined.
Final Report:

Crash of a Cessna 402C in Bundaberg: 4 killed

Date & Time: Jun 21, 1987 at 0318 LT
Type of aircraft:
Operator:
Registration:
VH-WBQ
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Bundaberg - Brisbane
MSN:
402C-0627
YOM:
1982
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The flight had been arranged to transport a critically injured patient to hospital in Brisbane. The pilot evidently experienced some difficulty in starting one of the engines. However, witnesses reported that the engines sounded normal as the aircraft commenced moving from the parking area. At 0310 hours the pilot contacted Brisbane Flight Service Unit and reported that the aircraft was taxying. He advised that he was in a hurry, and indicated that he would provide details of the flight after takeoff. Two minutes later he advised that takeoff was being commenced from Runway 14. No further transmissions were received from the aircraft. The aircraft was seen to become airborne and shortly afterwards enter a fog bank. Other witnesses subsequently reported hearing the sounds of an impact. The flight had been arranged to transport a critically injured patient to hospital in Brisbane. The pilot evidently experienced some difficulty in starting one of the engines. However, witnesses reported that the engines sounded normal as the aircraft commenced moving from the parking area. At 0310 hours the pilot contacted Brisbane Flight Service Unit and reported that the aircraft was taxying. He advised that he was in a hurry, and indicated that he would provide details of the flight after takeoff. Two minutes later he advised that takeoff was being commenced from Runway 14. No further transmissions were received from the aircraft. The aircraft was seen to become airborne and shortly afterwards enter a fog bank. Other witnesses subsequently reported hearing the sounds of an impact. The flight had been arranged to transport a critically injured patient to hospital in Brisbane. The pilot evidently experienced some difficulty in starting one of the engines. However, witnesses reported that the engines sounded normal as the aircraft commenced moving from the parking area. At 0310 hours the pilot contacted Brisbane Flight Service Unit and reported that the aircraft was taxying. He advised that he was in a hurry, and indicated that he would provide details of the flight after takeoff. Two minutes later he advised that takeoff was being commenced from Runway 14. No further transmissions were received from the aircraft. The aircraft was seen to become airborne and shortly afterwards enter a fog bank. Other witnesses subsequently reported hearing the sounds of an impact. The investigation revealed that the aircraft had collided with a tree 800 metres beyond the aerodrome boundary, while tracking about 10 degrees to the right of the extended centreline of the runway. It had then continued on the same heading until striking the ground 177 metres beyond the initial impact point. The wreckage was almost totally consumed by fire.
Probable cause:
The extensive fire damage hampered the investigation of the accident. The surviving passenger believed that the aircraft was on fire before the collision with the tree. No other evidence of an in-flight fire could be obtained, and it was considered possible that the survivor's recall of the accident sequence had been affected by the impact and the fire. Such discrepancies in recall are not uncommon among accident survivors. The elevator trim control jack was found to be in the full nose-down position, but it was not possible to establish whether the trim was in this position prior to impact. Such a pre-impact position could indicate either a runaway electric trim situation or that, in his hurry to depart, the pilot had not correctly set the trim for takeoff. The aircraft was known to have had an intermittent fault in the engine fire warning system. The fault apparently caused the fire warning light to illuminate, and the fire bell to sound, usually just after the aircraft became airborne. The pilot was aware of this fault. It was considered possible that, if the fault occurred on this occasion as the aircraft entered the fog shortly after liftoff, the pilot's attention may have been focussed temporarily on the task of cancelling the warnings. During this time he would not have been monitoring the primary flight attitude indicator, and would have had no external visual references. It was also possible that, if for some reason the pilot was not monitoring his flight instruments as the aircraft entered the fog, he suffered a form of spatial disorientation known as the somatogravic illusion. This illusion has been identified as a major factor in many similar accidents following night takeoffs. As an aircraft accelerates, the combination of the forces of acceleration and gravity induce a sensation that the aircraft is pitching nose-up. The typical reaction of the pilot is to counter this apparent pitch by gently applying forward elevator control, which can result in the aircraft descending into the ground. In this particular case, the pilot would probably have been more susceptible to disorientating effects, because he was suffering from a bronchial or influenzal infection. Although all of the above were possible explanations for the accident, there was insufficient evidence available to form a firm conclusion. The precise cause of the accident remains undetermined.
It is considered that some of the following factors may have been relevant to the development of the accident
1. The pilot was making a hurried DEPARTURE. It is possible that he did not correctly set the elevator trim and/or the engines may not have reached normal operating temperatures before the takeoff was commenced.
2. Shortly after liftoff the aircraft entered a fog bank, which would have deprived the pilot of external visual references.
3. The aircraft had a defective engine fire warning system. Had the system activated it may have distracted the pilot at a critical stage of flight.
4. The aircraft might have suffered an electric elevator trim malfunction, or an internal fire, leading to loss of control of the aircraft.
5. The pilot may have experienced the somatogravic illusion and inadvertently flown the aircraft into the ground. The chances of such an illusion occurring would have been increased because the pilot was evidently suffering from an infection.
Final Report:

Crash of an Avro 652 Anson I in Bundaberg

Date & Time: Dec 1, 1943
Type of aircraft:
Operator:
Registration:
AW906
Flight Type:
Survivors:
Yes
Schedule:
Bundaberg - Bundaberg
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a training exercise. For unknown reason, the aircraft overshot and collided with a boundary fence. While all four crew members were uninjured, the aircraft was damaged beyond repair.

Crash of an Avro 652 Anson I in Clayton

Date & Time: Nov 11, 1942
Type of aircraft:
Operator:
Registration:
AW866
Flight Phase:
Flight Type:
Survivors:
Yes
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
En route, the captain was forced to attempt an emergency landing due to fuel starvation. The twin engine aircraft crash landed in a cane field and was damaged beyond repair. All three crew members were unhurt.
Probable cause:
Fuel starvation.