Crash of a Cessna 421C Golden Eagle III near Cleveland: 6 killed

Date & Time: Dec 21, 1995 at 1442 LT
Registration:
N421EP
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tulsa - Aspen
MSN:
421C-1236
YOM:
1982
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
1320
Circumstances:
At 1350 cst, a McAlester FSS specialist gave a preflight briefing to a Cessna 421 pilot concerning IMC (instrument meteorological conditions) along the route & advised that VFR flight was not recommended. Cloud tops were at 12,000', & freezing level was at 1,600'. A PIREP at 1416 cst reported light mixed icing from 6,400' to 9,000' at Oklahoma City. At 1424 cst, the pilot departed Tulsa (VFR), then radar service was terminated. No further communication was received from the airplane. Radar data showed that it climbed westerly, reaching 9,800' at 1440 cst; during the next 88 seconds, its heading & altitude deviated until it descended through 3,200'. Ground witnesses saw the airplane descend out of low clouds in a 'flat spin' & crash. No preimpact mechanical failure was found. The airplane's gross weight was about 150 lbs over its maximum limit. In November 1995, the pilot received 10 hrs of Cessna 421 simulator training; his instructor noted in training records that he met minimum standards for VFR, but 'under IMC conditions,' he 'could not maintain altitude within 1,300 feet or heading within 40 degrees.' Postmortem toxicology tests showed 0.079 mcg/ml Nordiazepam (metabolite of Valium) in kidney fluid, 0.044 mcg/ml Desipramine (metabolite of Imipramine, an antidepressant) in spleen fluid, 0.733 mcg/ml Diphenhydramine (Benadryl) in spleen fluid, & 0.353 mcg/ml Diphenhydramine in lung fluid. These medications are not approved by the FAA for use while flying. The airplane was equipped for flight in icing & IFR
conditions.
Probable cause:
The pilot's continued VFR flight into instrument meteorological conditions (IMC), and his failure to maintain control of the airplane after encountering adverse weather conditions, which resulted in a stall/spin. Factors relating to the accident were: pilot impairment due to a medication that was not approved by the FAA for use while flying, the adverse weather conditions, and the pilot's lack of instrument proficiency in the Cessna 421 airplane.
Final Report:

Crash of a Rockwell Grand Commander 690A in Taos: 1 killed

Date & Time: Mar 29, 1992 at 1900 LT
Registration:
N111FL
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Taos - Tulsa
MSN:
690-11163
YOM:
1974
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2200
Captain / Total hours on type:
120.00
Aircraft flight hours:
3404
Circumstances:
The airplane impacted slightly rising terrain in a 15° left bank, slight nose up attitude while descending shortly after takeoff in dark night IMC. There were rain and snow showers in the area and it was devoid of visible ground reference lights. The difference between the takeoff heading and the impact heading was 75° and the airplane had traveled 3,987 feet from the departure end of the runway at initial impact. The wreckage subsequently traveled an additional 837 feet through the brush. The pilot stated that the takeoff was normal in all aspects and all of the airplane systems were operating normally. He stated that the last thing he remembered was passing through 8,500 feet with a rate of climb of 1,500 feet per minute. The airport elevation was 7,091 feet. He did not recall the radio altimeter alert or the warning light activating. No evidence of pre-impact failure or malfunction was found during the investigation. Rescue of the occupants were delayed due to the weather, darkness, and spurious elt signals masked by the wreckage.
Probable cause:
The pilot in command's failure to maintain the climb after departing the runway environment. Factors were the weather conditions and the dark night.
Final Report:

Crash of a Learjet 25B in Carlsbad

Date & Time: Dec 23, 1991 at 0825 LT
Type of aircraft:
Registration:
N44PA
Flight Type:
Survivors:
Yes
Schedule:
Tulsa - Carlsbad
MSN:
25-144
YOM:
1974
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6180
Captain / Total hours on type:
117.00
Aircraft flight hours:
8117
Circumstances:
The pilot and copilot reported in their written statements that the airplane was above glideslope on the final approach. They said the airplane touched down about 1,500 feet from the approach end of the 4,700 feet long runway. The pilot said he applied the brakes but could not stop the airplane on the runway. The airplane departed the end of the runway and continued forward over rough and uneven terrain. The main landing gear sheared off and penetrated both wings. The airplane came to a stop in a gully. Other witnesses located on the ground and in the air traffic control tower reported the airplane was 'high and fast' and touched down at about midfield or after.
Probable cause:
The pilot not attaining the proper touchdown point because of excessive altitude and airspeed, and the pilot's failure to perform a go-around. A factor in this accident was the rough and uneven terrain which was encountered after the aircraft departed the runway.
Final Report:

Crash of a Mitsubishi MU-2B-20 Marquise in Kenefic: 1 killed

Date & Time: May 7, 1991 at 0510 LT
Type of aircraft:
Registration:
N106MA
Flight Phase:
Survivors:
No
Schedule:
Tulsa - Dallas
MSN:
0184
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3850
Captain / Total hours on type:
1400.00
Circumstances:
The pilots of Mitsubishi MU-2, N106MA, and a Cessna 310 with no registration number elected to fly in formation at night, though neither pilot had formal training in formation flying nor experience in night formation. They joined up in flight and the MU-2 pilot was flying on the wing of the Cessna 310. The MU-2 pilot communicated that he was going to change positions from the right side to the left side of the 310C. The Cessna 310 pilot and his passenger lost sight of the MU-2 when it dropped back to a position in the rear of the Cessna 310. Soon thereafter, the two aircraft collided and the MU-2 went out of control and crashed. The right horizontal stabilizer was torn from the Cessna 310 and the 310's empennage, right wing and props were damaged, but it was landed without injury to its occupants. An investigation revealed the tail light of the Cessna 310 was inoperative. Sole on board, the pilot was killed.
Probable cause:
Improper planning/decision by the pilots of both aircraft, and the mitsubishi pilot's misjudgment of his position, while attempting to fly formation at night with an aircraft that did not have all navigation lights operative. Factors related to the accident were: both pilot's lack of training in the type of operation, darkness, inoperative navigation (tail) light on the Cessna 310, and the lack of visual perception that would have been available to the mitsubishi pilot.
Final Report:

Crash of a Mitsubishi MU-2B-60 Marquise in Tulsa: 3 killed

Date & Time: Feb 22, 1991 at 1519 LT
Type of aircraft:
Registration:
N274MA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tulsa - Tulsa
MSN:
786
YOM:
1980
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
4910
Captain / Total hours on type:
445.00
Aircraft flight hours:
6094
Circumstances:
Airplane was departing on a required maintenance test flight following replacement of both engines. Witnesses stated that the takeoff roll and initial climb appeared normal, but that at about 500 feet agl, the airplane entered a right bank which continued until the wings were vertical and the nose fell through. Airplane impacted in an inverted steep nose down attitude. Examination of wreckage revealed that the right engine had been secured and feathered. Subsequent investigation did not reveal any evidence of pre-impact failure or malfunction of either engine or any of the airframe systems. Engine mounting/rigging continuity could not be established due to impact damage. The pilot was a principal in the operator's organization and not one of the regular line pilots. Evidence indicated that the gear was up and that the left spoiler was deployed at impact. Emerg procedure taught in transition training is to use rudder trim as soon as possible after engine failure to preclude deployment of spoilers. Rudder trim found in neutral position. All three occupants were killed.
Probable cause:
The shutdown of one engine for undetermined reasons, and the pilot's failure to maintain VMCA during a critical phase of flight. A factor in the accident was the pilot's improper emergency procedure.
Final Report:

Crash of a Northrop YC-125B Raider in Tulsa

Date & Time: Jun 29, 1988 at 0625 LT
Type of aircraft:
Registration:
N3756Q
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Tulsa - Dayton
MSN:
2518
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6274
Captain / Total hours on type:
56.00
Circumstances:
The pilot did not hold a type rating or written authorization to act as pilot in command. The copilot did not hold a type rating or written authorization to act as second in command and his medical had expired. The aircraft did not have an airworthiness certificate nor had a special flight permit been issued. The left propeller went into reverse during the initial climb due to corrosion and deterioration of the wiring that controlled the propeller. The aircraft crashed out of control after colliding with power lines during takeoff. It struck the ground and went through a fence then down a slope and over an embankment. The aircraft then bounced across a street while turning around and colliding with a power line pole tail first. The aircraft had traveled about 537 feet from initial ground contact. All 3 engines were still producing power when the aircraft came to rest. Both occupants escaped uninjured.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: takeoff - initial climb
Findings
1. (c) electrical system - corroded
2. (f) inadeq substantiation process, inadequate documentation - company/operator mgmt
3. (c) electrical system - deteriorated
4. (c) propeller system/accessories,reversing system - engaged
5. (c) procedures/directives - disregarded - pilot in command
6. (c) operation with known deficiencies in equipment - attempted - pilot in command
7. (f) lack of total experience in type of aircraft - pilot in command
8. (f) lack of total experience in type of aircraft - copilot/second pilot
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Beechcraft C90 King Air in Fort Wayne: 1 killed

Date & Time: Oct 24, 1983 at 1615 LT
Type of aircraft:
Registration:
N4TS
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Wayne - Tulsa
MSN:
LJ-541
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
18980
Aircraft flight hours:
3821
Circumstances:
At 1604 est, the aircraft departed Fort Wayne on a ferry flight. IFR conditions prevailed and the pilot had filed an IFR flight plan. While climbing after takeoff, the pilot passed his assigned altitude of 2,500 feet msl and flew to 4,200 feet. Also, he failed to turn to his initial assigned heading of 130°. He had problems contacting departure control as he was not on the assigned frequency. He reported problems with his heading indicator and his 'gyro'. Shortly after his last transmission, the aircraft left 4,200 feet msl and crashed in a steep dive. Before takeoff, the atp pilot reported he had flown all King Air aircraft and was currently flying the Beech 200. A review of his last log book revealed over 2,000 hours in the Beech 200, but showed no time in the Beech C90. A witness that reviewed the aircraft with the pilot before the flight believed he (the pilot) was very familiar with the aircraft systems. During an inspection of the wreckage, no evidence was found to verify a pre-impact malfunction or failure of the aircraft or engines. All instruments were destroyed. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: climb
Findings
1. (c) reason for occurrence undetermined
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Piper PA-31T Cheyenne II in Pontiac: 3 killed

Date & Time: Feb 19, 1981 at 1903 LT
Type of aircraft:
Operator:
Registration:
N321SS
Survivors:
No
Schedule:
Tulsa - Pontiac
MSN:
31-8020035
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
1700
Captain / Total hours on type:
33.00
Circumstances:
On approach to Pontiac-Oakland County Airport runway 09, the pilot encountered poor visibility due to low ceiling and fog. On final, the twin engine airplane struck two 40 feet approach lite towers located 2,400 and 2,200 feet from the approach end of the runway. The airplane lost height and crashed, bursting into flames. All three occupants were killed.
Probable cause:
Collision with wires/poles on final approach due to improper IFR operation. The following contributing factors were reported:
- Low ceiling,
- Fog,
- Visibility down to zero,
- Weather conditions below minimums.
Final Report:

Crash of a Beechcraft 60 Duke near Jackson: 8 killed

Date & Time: Nov 6, 1978 at 2046 LT
Type of aircraft:
Registration:
N135D
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Montgomery - Tulsa
MSN:
P-7
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
2000
Captain / Total hours on type:
60.00
Circumstances:
The twin engine aircraft was completing a demo flight from Montgomery, Alabama, to Tulsa, Oklahoma, carrying seven passengers and a pilot. While cruising at an altitude of 14,000 feet in icing conditions, the pilot informed ATC about an engine failure and was cleared to divert to Jackson-Municipal Airport. On descent, the aircraft went out of control and crashed few miles from Jackson Airport. The aircraft was destroyed and all eight occupants were killed.
Probable cause:
Uncontrolled collision with ground on final approach due to powerplant failure for undetermined reasons. The following contributing factors were reported:
- Diverted attention from operation of aircraft,
- Improper in-flight decisions,
- Icing conditions including sleet, freezing rain,
- Fog,
- Complete failure on one engine,
- Weather briefing included freezing level 13,000 to 15,000 feet,
- Cruising altitude 14,000 feet.
Final Report:

Crash of a Rockwell 1121 Jet Commander near Flatwoods: 2 killed

Date & Time: Apr 27, 1978 at 1548 LT
Registration:
N250UA
Flight Phase:
Survivors:
No
Schedule:
Lafayette - Tulsa
MSN:
1121-121
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
20000
Captain / Total hours on type:
20000.00
Circumstances:
En route from Lafayette to Tulsa, the crew was cleared to climb from FL230 to FL350 when the airplane disintegrated in the air. It entered an uncontrolled descent and eventually crashed in the region of Flatwoods. Debris were found on a wide area and both occupants were killed.
Probable cause:
The exact cause of the in-flight disintegration was not determined. However, the following findings were reported:
- Flight control surfaces: elevator assembly, attachments,
- Flight control surfaces: horizontal stabilizer, attachments,
- Overload failure,
- Separation in flight,
- Loss of control occurred after leaving FL230 for FL350,
- General disintegration.
Final Report: