Crash of a Mitsubishi MU-300 Diamond IA in Goodland: 3 killed

Date & Time: Dec 15, 1993 at 1305 LT
Type of aircraft:
Registration:
N710MB
Survivors:
No
Schedule:
Scott City - Goodland
MSN:
78
YOM:
1984
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
17365
Captain / Total hours on type:
80.00
Aircraft flight hours:
2593
Circumstances:
The flight was cleared for the ILS approach to runway 30. The flying pilot was the pilot-in-command. According to the cockpit voice recorder transcripts, the flying pilot had difficulty making a stabilized approach. During the initial descent the airplane entered an overspeed condition and the airplane flew through the localizer. During his attempt to re-establish the airplane on the localizer, the pilot allowed the airspeed to decrease to the point where the prestall 'stick-shaker' activated. The stick shaker continued until the airplane departed controlled flight and impacted terrain. No evidence of any preimpact mechanical anomalies were discovered during the investigation. All three occupants were killed.
Probable cause:
The pilot-in-command's inadvertent stall of the airplane. A factor associated with the accident is the pilot-in-command's poor ifr procedures.
Final Report:

Crash of a Canadair RegionalJet CRJ-100ER in Byers: 3 killed

Date & Time: Jul 26, 1993 at 1352 LT
Operator:
Registration:
C-FCRJ
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wichita - Wichita
MSN:
7001
YOM:
1991
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3836
Captain / Total hours on type:
875.00
Aircraft flight hours:
771
Aircraft flight cycles:
800
Circumstances:
The crew was performing a lateral and directional stability test. Changes from earlier tests combined new leading edge fairing, new flap setting, lower reference airspeed, and trial settings for the stall protection system (shaker and pusher). Engineers had briefed the crew data would be sufficient if the steady heading sideslip (shss) maneuver ended at a 15° sideslip, or at onset of stall warning; crew agreed to end at stall warning. During the test the capt continued past stall warning to 21° sideslip at full rudder. The airplane rolled rapidly through 360 deg° and entered a deep stall. The copilot attempted to deploy the anti-spin chute. However, all the chute system cockpit switches were not properly preset; instead of assisting recovery, the chute parted from the airplane. Full control was not regained before impact. The chute system design allowed deployment of the chute even when the hyd lock switch was in the unlocked position and the hooks clasping the chute shackle to the airframe were open. System tested ok before flight. All three crew members were killed.
Probable cause:
The captain's failure to adhere to the agreed upon flight test plan for ending the test maneuver at the onset of prestall stick shaker, and the flightcrew's failure to assure that all required switches were properly positioned for anti-spin chute deployment. A factor which contributed to the accident was the inadequate design of the anti-spin chute system which allowed deployment of the chute with the hydraulic lock switch in the unlocked position. (When in the unlocked position, the hooks clasping the chute shackle to the airframe are open).
Final Report:

Crash of a Rockwell Grand Commander 690 in Wichita: 2 killed

Date & Time: Nov 2, 1991 at 1206 LT
Registration:
N799V
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wichita - Phoenix
MSN:
690-11407
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4900
Captain / Total hours on type:
1078.00
Aircraft flight hours:
3480
Circumstances:
The pilot and his wife departed Wichita, Kansas with a destination of Phoenix, Arizona. Eight minutes after takeoff, while in a climb to 15,000 feet, the passenger contacted departure control and communicated that she thought that her husband might be dead. While departure control was getting a pilot to assist in the situation, the passenger, who was not a pilot attempted to fly the aircraft. A witness reported a rapid series of climbs and descents just before both horizontal stabilizers and the rudder separated from the aircraft. The aircraft then entered a spin terminating with ground impact. The aircraft was consumed by a post-crash fire. Both occupants were killed.
Probable cause:
Incapacitation of the pilot in command, followed by the loss of control and an inflight breakup with a unqualified person on the controls.
Final Report:

Crash of a Rockwell Aero Commander 500 in Silica: 1 killed

Date & Time: Jul 31, 1991 at 0759 LT
Operator:
Registration:
N904DF
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wichita - Hays
MSN:
500-1057-46
YOM:
1961
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3358
Captain / Total hours on type:
724.00
Aircraft flight hours:
11546
Circumstances:
Both aircraft departed Wichita on IFR flight plan in VFR weather conditions. They flew northwest toward their respective destinations, and cancelled IFR about 20 minutes before the accident. ATC observed the airplanes on radar, and stated they were 'dogfighting back and forth' prior to the collision. One pilot's roommate reported the two pilots, who were close friends as well as co-workers, often cancelled IFR and flew in formation if the weather was VFR. He reported the pilots often videotaped each other, and he had watched some of the tapes. He stated 'it was hard to tell from the videotape how close they were because they could use the zoom feature, etc. You could read the N numbers.' Investigation revealed brown paint transfer on the bottom of the right wing of the blue and white airplane, which had separated and was located 1.5 miles from the main wreckage. There were light colored scuff marks on the top of the left engine nacelle of the brown and white airplane. Both aircraft and both pilots were killed.
Probable cause:
The failure of both pilots to maintain adequate separation during formation flight. Related factors are overconfidence in personal ability and poor planning/decision.
Final Report:

Crash of a Rockwell Aero Commander 500 in Silica: 1 killed

Date & Time: Jul 31, 1991 at 0759 LT
Operator:
Registration:
N702CA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wichita - Great Bend
MSN:
500-1298-113
YOM:
1963
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1590
Captain / Total hours on type:
322.00
Aircraft flight hours:
12747
Circumstances:
Both aircraft departed Wichita on IFR flight plan in VFR weather conditions. They flew northwest toward their respective destinations, and cancelled IFR about 20 minutes before the accident. ATC observed the airplanes on radar, and stated they were 'dogfighting back and forth' prior to the collision. One pilot's roommate reported the two pilots, who were close friends as well as co-workers, often cancelled IFR and flew in formation if the weather was VFR. He reported the pilots often videotaped each other, and he had watched some of the tapes. He stated 'it was hard to tell from the videotape how close they were because they could use the zoom feature, etc. You could read the N numbers.' Investigation revealed brown paint transfer on the bottom of the right wing of the blue and white airplane, which had separated and was located 1.5 miles from the main wreckage. There were light colored scuff marks on the top of the left engine nacelle of the brown and white airplane. Both aircraft and both pilots were killed.
Probable cause:
The failure of both pilots to maintain adequate separation during formation flight. Related factors are overconfidence in personal ability and poor planning/decision.
Final Report:

Crash of a Rockwell Aero Commander 500B in Garden City: 1 killed

Date & Time: Jan 19, 1988 at 1946 LT
Registration:
N611CA
Flight Type:
Survivors:
No
Schedule:
Garden City - Wichita
MSN:
500-0922-7
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2125
Captain / Total hours on type:
58.00
Aircraft flight hours:
6713
Circumstances:
The aircraft departed Garden City under extremely poor weather conditions. More than half way to Dodge City, the pilot reported engine problems to Kansas City (ARTCC). Vectors were provided to the Dodge City Airport, but the pilot did not maintain assigned headings. The aircraft headed back towards Garden City to attempt an instrument approach. Radar vectors were provided for the localizer approach. Radar indicated that the aircraft did not become stabilized on the approach. There was a significant loss of ground speed as the pilot was attempting to get established on the localizer. Radar contact was lost about 2 miles from the airport at a speed approaching stall speed for this aircraft. The aircraft crashed about 2 miles short and to the right of course. The aircraft impacted in a vertical nose down attitude on heading which indicated a turn away from the airport. The left prop was found in the feather position. No mechanical problem was discovered. The right engine appeared to be producing full power at impact. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of engine power (partial) - nonmechanical
Phase of operation: cruise - normal
Findings
1. 1 engine
2. (c) powerplant - undetermined
3. Propeller feathering - performed - pilot in command
4. (f) light condition - dark night
----------
Occurrence #2: loss of control - in flight
Phase of operation: approach - faf/outer marker to threshold (ifr)
Findings
5. (f) proper alignment - not maintained - pilot in command
6. (f) missed approach - not performed - pilot in command
7. (c) airspeed (vmc) - not maintained - pilot in command
8. (c) stall - inadvertent - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
9. Terrain condition - frozen
10. (f) lack of total experience in type of aircraft - pilot in command
Final Report:

Crash of a Cessna 414A Chancellor in Olathe

Date & Time: Dec 24, 1986 at 2249 LT
Type of aircraft:
Registration:
N414LL
Survivors:
Yes
Schedule:
Kirkville - Olathe
MSN:
414A-0627
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4117
Captain / Total hours on type:
23.00
Aircraft flight hours:
2403
Circumstances:
The pilot stated that this was not a charter flight and, as such, he decided to attempt the loc 17 approach to Olathe even though the area was forecasting zero-zero conditions. According to the pilot, the last thing he remembers during the flight is bracketing the loc and reading 1,600 feet on the altimeter. Subsequently, the pilot further stated, he remembers being on the ground inside the wreckage, mitigating the injuries suffered and trying to stay warm. A post-accident invest revealed that the aircraft was to the left of the localizer course when it struck two trees 12 feet agl (1,062 feet msl), while in a 30° right bank. The aircraft made a flat 360 right pirouette over some small trees, tearing off the left wing before impacting the ground and sliding approximately 600 feet. A post-crash fire erupted from the right wing tank but it extinguished itself. A dot FAA operational flight test found the localizer to be within limits. A leak check of the aircraft static system and a bench check of both altimeters were satisfactory.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: approach - faf/outer marker to threshold (ifr)
Findings
1. (f) weather condition - fog
2. (f) light condition - dark night
3. Object - tree(s)
4. (f) in-flight planning/decision - improper - pilot in command
5. (f) not performed - pilot in command
6. (c) ifr procedure - not followed - pilot in command
7. (c) minimum descent altitude - not maintained - pilot in command
8. (c) missed approach - not performed - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: approach - faf/outer marker to threshold (ifr)
----------
Occurrence #3: fire
Phase of operation: other
Findings
9. (c) fuel system, tank - burst
Final Report:

Crash of a Rockwell Sabreliner 75A in Liberal

Date & Time: Sep 29, 1986 at 1204 LT
Type of aircraft:
Operator:
Registration:
N64
Flight Type:
Survivors:
Yes
Schedule:
Oklahoma City - Liberal
MSN:
380-35
YOM:
1975
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8448
Captain / Total hours on type:
1540.00
Aircraft flight hours:
7327
Circumstances:
The right main landing gear downlock pin retracted just before or during touchdown. The airplane touched down 21 feet short of the runway. It traveled that 21 feet, traveled the full length of the 6999- foot runway, then traveled another one-fourth of a mile and stopped on a golf course. No pre-touchdown mechanical, hydraulic or electrical problems could be found. All four occupants escaped uninjured.
Probable cause:
Occurrence #1: gear collapsed
Phase of operation: landing - flare/touchdown
Findings
1. (c) procedures/directives - not followed - pilot in command
2. (c) gear retraction - inadvertent - copilot/second pilot
----------
Occurrence #2: loss of control - on ground/water
Phase of operation: landing - roll
----------
Occurrence #3: on ground/water encounter with terrain/water
Phase of operation: landing - roll
Findings
3. (f) terrain condition - ditch
----------
Occurrence #4: on ground/water collision with object
Phase of operation: landing - roll
Findings
4. (f) object - fence
----------
Occurrence #5: on ground/water encounter with terrain/water
Phase of operation: landing - roll
Findings
5. (f) terrain condition - water, glassy
Final Report: