Crash of a Cessna 680A Citation Latitude in Elizabethton

Date & Time: Aug 15, 2019 at 1537 LT
Operator:
Registration:
N8JR
Flight Type:
Survivors:
Yes
Schedule:
Statesville - Elizabethton
MSN:
680A-0010
YOM:
2015
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5800
Captain / Total hours on type:
765.00
Copilot / Total flying hours:
11000
Copilot / Total hours on type:
1165
Aircraft flight hours:
1165
Circumstances:
The pilots were conducting a visual flight rules cross-country flight with three passengers onboard. The preflight, departure, and cruise portions of the flight were uneventful. During the initial approach to the airport, the flight crew discussed having some difficulty visually acquiring the airport. They also discussed traffic in the area and were maneuvering around clouds, which may have increased the pilots' workload. As the approach continued, the airplane crossed a ridgeline at 710 ft above ground level (agl), which triggered a terrain awareness and warning system (TAWS) alert. Further, the flight crew made several comments about the airplane flying too fast and allowed the airspeed to increase well above the reference speed (Vref) for the approach. At 1535:57 (about 1 minute 52 seconds before landing), the pilot pulled back the throttles to idle, where they stayed for the remainder of the approach. In an attempt to slow the airplane for landing, the pilot partially extended the speedbrakes when the airplane was below 500 ft agl, which is prohibited in the airplane flight manual (AFM). Five seconds before touchdown, the airplane's descent rate was 1,500 ft per minute (fpm), which exceeded the maximum allowed for landing per the AFM of 600 fpm. When the airplane first touched down, it was traveling about 18 knots above Vref. The pilot did not extend the speedbrakes upon touchdown, which the landing checklist required, but instead attempted to deploy the thrust reversers immediately after touchdown, which was a later item on the landing checklist. However, the thrust reversers did not unlock because the airplane bounced and was airborne again before the command could be executed, which was consistent with system design and logic: the thrust reversers will not unlock until all three landing gear are on the ground. The airplane touched down four times total; on the third touchdown (after the second bounce), when all three landing gear contacted the runway, the thrust reversers unlocked as previously commanded during the first touchdown. Although the pilot subsequently advanced the throttles to idle, which would normally stow the thrust reversers, the airplane had bounced a third time and had already become airborne again before the thrust reversers could stow. When the airplane became airborne, the system logic cut hydraulic power to the thrust reverser actuators; thus the reversers would not stow. The thrust reversers were subsequently pulled open due to the aerodynamic forces. The pilot attempted to go around by advancing the throttles when the airplane was airborne. However, the electronic engine controls prevented the increase in engine power because the thrust reversers were not stowed. When the airplane touched down the fourth and final time, the pilot attempted to land straight ahead on the runway; the airplane touched down hard and the right main landing gear then collapsed under the wing. The airplane departed the paved surface and came to rest about 600 ft beyond the runway threshold. The passengers and crew eventually evacuated the airplane through the main cabin door, and the airplane was destroyed in a postaccident fire. A postaccident examination of the airplane systems, structure, powerplants, and landing gear revealed no evidence of mechanical malfunctions or anomalies that would have precluded normal operation. The airplane's approach was unstabilized: its airspeed during the approach and landing well exceeded Vref and its descent rate exceeded the maximum allowed for landing just seconds before touchdown. Both the pilot and copilot commented on the airplane's high speed several times during the approach. During short final, the pilot asked the copilot if he should go around, and the copilot responded, "no." Although the copilot was the director of operations for the flight department and the direct supervisor of the pilot, the pilot stated that the copilot's position did not influence his decisions as pilot-in-command nor did it diminish his command authority. Neither the pilot nor copilot called for a go-around before landing despite awareness that the approach was unstabilized. As the airplane touched down, the pilot failed to follow the AFM guidance and used the thrust reversers before the speedbrakes. According to the airplane manufacturer's calculations, the airplane could have stopped within the length of runway available if the airplane had not bounced and the speedbrakes and wheel brakes were used at the point of the first touchdown. After the third touchdown, when the airplane became airborne again, the pilot attempted a go-around; the AFM prohibits touch-and-go landings after the thrust reversers are deployed. It is critical for pilots to know the point at which they should not attempt a go-around; a committed-to-stop (CTS) point is the point at which a go-around or rejected landing procedure will not be initiated and the only option will be bringing the aircraft to a stop. Establishing a CTS point eliminates the ambiguity for pilots making decisions during time-critical events. The FAA issued Information for Operators 17009, "Committed-toStop Point on Landings," to inform operators and pilots about the importance of establishing a CTS point; however, the director of operations was not aware of the concept of a CTS point during landing.
Probable cause:
The pilot's continuation of an unstabilized approach despite recognizing associated cues and the flight crew's decision not to initiate a go-around before touchdown, which resulted in a bounced landing, a loss of airplane control, a landing gear collapse, and a runway excursion. Contributing to the accident was the pilot's failure to deploy the speedbrakes during the initial touchdown, which may have prevented the runway excursion, and the pilot's attempt to go around after deployment of the thrust reversers.
Final Report:

Crash of a Piper PA-46-350P Malibu Mirage in Statesville

Date & Time: Aug 1, 2014 at 2100 LT
Operator:
Registration:
N472ST
Flight Type:
Survivors:
Yes
Schedule:
Manassas – Statesville
MSN:
46-36472
YOM:
2010
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2556
Captain / Total hours on type:
1200.00
Aircraft flight hours:
1656
Circumstances:
According to the pilot, she was flying an instrument landing system approach when she noted that the glide slope was out of service. She transitioned to a localizer-only approach and continued. Night, instrument meteorological conditions prevailed with a 400-foot ceiling. She noticed that the airplane was "high and fast" on final approach, so she used speed brakes and flaps to slow the airplane and descend to the minimum descent altitude. As the airplane descended below the ceiling, she observed runway lights and attempted to land on the runway. The airplane landed long, departed the runway at the departure end, and struck an embankment before coming to rest. An inspector from the Federal Aviation Administration examined the airplane and confirmed substantial damage to the fuselage, wings, and empennage. The pilot reported no pre-impact mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable cause:
The pilot's failure to maintain a proper glide path and airspeed on final approach, which resulted in a long landing and runway excursion.
Final Report:

Crash of a Douglas C-47A-85-DL in Statesville

Date & Time: Feb 29, 1968 at 1345 LT
Registration:
N525W
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
20054
YOM:
1944
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12000
Captain / Total hours on type:
150.00
Circumstances:
Shortly after takeoff from Statesville Airport, while in initial climb, the left engine failed. The pilot-in-command reduced power on the right engine and attempted an emergency landing in an open field. While all four occupants escaped uninjured, the airplane was damaged beyond repair.
Probable cause:
Improper operation of powerplant on part of the crew who failed to use anti-icing/deicing systems prior to takeoff. Icing conditions conducted to the icing of the carburetor and induction systems on the left engine that failed during initial climb. Takeoff was completed with reduced power.
Final Report:

Crash of a Pitcairn PA-5 Mailwing in Statesville

Date & Time: Aug 15, 1928
Type of aircraft:
Operator:
Registration:
NC3836
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
10
YOM:
1928
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances in Old Fort, 2 km north of Statesville. The pilot was injured and the aircraft was damaged beyond repair.