Country
code

Helmand

Crash of an Antonov AN-12B in Camp Dwyer: 7 killed

Date & Time: May 18, 2016 at 1407 LT
Type of aircraft:
Operator:
Registration:
4K-AZ25
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Camp Dwyer – Mary – Baku
MSN:
3 3 412 09
YOM:
1963
Country:
Region:
Crew on board:
9
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
22628
Captain / Total hours on type:
3953.00
Copilot / Total flying hours:
4625
Copilot / Total hours on type:
836
Aircraft flight hours:
19828
Aircraft flight cycles:
9107
Circumstances:
On May 18, 2016 the crew of An-12B 4K-AZ25 aircraft operated by Silk Way Airlines including the Captain, First Officer, navigator, flight mechanic, flight radio operator and loadmaster was planned to fly via route Baku (Azerbaijan) - Bagram (Afghanistan) - Dwyer (Afghanistan) - Mary (Turkmenistan) - Baku. There were also two maintenance mechanics and an engineer on board the a/c. The preliminary training of the crew was conducted on 29.12.2015 by the Chief Navigator of Silk Way Airlines. The pre-flight briefing was conducted on 18.05.2016 by a captain-instructor and a navigator-instructor. The following has been determined so far. According to the information available at the moment the flight to Dwyer aerodrome was conducted in an acceptable way. At 09:11:27 the crew started up the engines at Dwyer aerodrome, Engine #2 was the last to be started up at 09:47:37. Before the takeoff the Captain distributed the duties within the crew, nominating the FO as the PF, and himself as PM. After the engine startup the crew initiated taxiing to perform takeoff with heading 229°. The concrete RWY of Dwyer aerodrome is measured 2439 m by 37 m. The a/c TOW and CG were within the AFM limitations. In the course of the takeoff, at 09:57:56 the flight mechanic reported an increase in MGT of Engine #3 above the acceptable level: "Engine #3, look, engine temperature over six hundred, over seven hundred", which was confirmed by the FO: "Yes, it's getting temperature" while the Captain asked to be more attentive. According to the crew reports the takeoff was performed with Flaps 15. As the checklist was being read, the Captain ordered to lock the propellers. After the Captain's order to lock the propellers a slight increase in torque-measuring device values was recorded on Engine #1 and #4, and in 17 seconds also Engine #2, which indirectly implies that propellers #1, #2 and #4 were at stops. There is no evidence that propeller of Engine #3 was locked. At 09:59:42 the crew initiated the takeoff. Before the takeoff the ATC advised the crew on the wind direction and speed on the RWY: 280° 14 knots (7 m/sec) gusting 26 knots (13 m/sec). Thus it was quartering headwind and the headwind component might have been 5 to 9 m/sec. While performing takeoff the crew first increased thrust on Engines #1 and #4 and then on Engine #2 after 10 seconds. The thrust of the three engines was about 50 kg/sq.cm as per torque indicator (lower than takeoff mode). The third engine was still operating in the ground idle mode, though the CVR did not record any crew callouts concerning Engine #3 operation parameters. Based on the CCTV system of Dwyer aerodrome the takeoff roll was initiated almost from the RWY threshold and was conducted to the left of the RWY centerline. No significant deviations from the takeoff course during the takeoff roll were recorded. During the takeoff roll the rudder was deflected left close to extreme. Probably the pilots were also applying differential control on Engine #2 to decrease the right torque moment. At 10:00:14 at approximately 120 km/h IAS the "Engine #3 negative thrust" signal was started to be recorded and was recorded on up to the end of the record. At that time the a/c was about 430 m away from the start of the takeoff roll. At 10:00:42 Engines #1 and #4 thrust was increased up to 63 kg/sq.cm as per torque indicator (consistent with takeoff mode for the actual flight conditions). At that time the IAS was about 150 km/h Engine #2 thrust was increased up to the same value only 23 seconds later at about 200 km/h IAS. At that time the a/c was about 840 m away from the RWY end. Engine #3 was still operating in ground idle mode. Approximately 260 m before the RWY end at a speed of 220 km/h IAS (maximum speed reached) the FDR recorded the start of nose up input on the control column. The a/c did not lift off After rolling all along the RWY the a/c overran the RWY onto the ground at a speed of 220 km/h While moving on the ground the aircraft sustained significant damage, which led to post-crash fire that destroyed most of the aircraft structures. Out of the nine persons on board seven were killed and two were seriously injured and taken to hospital.
Final Report:

Crash of an Antonov AN-12BP at Camp Dwyer AFB

Date & Time: Jul 28, 2010
Type of aircraft:
Operator:
Registration:
3X-GEQ
Flight Type:
Survivors:
Yes
MSN:
4 3 422 10
YOM:
1964
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing at Camp Dwyer AFB (Forward Operating Base Dwyer) located in the Helmand Province, the aircraft went out of control, veered off runway, collided with a fence and came to rest into a ravine, broken in two. All six occupants were uninjured while the aircraft was damaged beyond repair. It was later dismantled by the US Air Force. The aircraft was carrying a load of fresh fruits and dairy products.

Crash of a Lockheed C-130 Hercules C.1P in Lashkar Gah

Date & Time: May 24, 2006 at 1530 LT
Type of aircraft:
Operator:
Registration:
XV206
Flight Type:
Survivors:
Yes
Schedule:
Kabul - Lashkar Gah
MSN:
4231
YOM:
1967
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
20
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The RAF Hercules was on a routine operational flight providing support to the Provincial Reconstruction Team (PRT) at Lashkar Gar, Afghanistan at the time of the accident. The LKG Tactical Landing Zone (TLZ) is 6,800 feet long by 150 feet wide with a surface of compacted sand and gravel located on the south side of LKG town. The TLZ is used by UK forces and other agencies including the UN and Red Cross. The aircraft took off at 08:50 UTC from Kabul International Airport (KBL) to fly a routine logistics sortie to deliver cargo and personnel to LKG TLZ. After an uneventful medium level transit the aircraft landed at LKG at 10:20 UTC. Using a standard tactical landing technique the aircraft touched down some 500ft in from the runway threshold, reverse thrust was selected and speed reduced without the need for wheel braking. After 3 seconds, as the speed was nearing 70 kts there was a loud bang from the port side of the aircraft in the vicinity of the port main landing gear, the force of which was felt throughout the aircraft. At the same time the flight deck crew saw tyre debris flying up in front of the aircraft and then became aware of structural damage to the number 2 engine. The captain ordered the Emergency Engine Shutdown Drill (EESD) on the number 2 engine. He maintained directional control with nosewheel steering. Immediately after the shutdown of number 2 engine crew members observed a large amount of fuel leaking from the port wing area in the vicinity of the external tank pylon and that there was a fire in the vicinity of No.1 engine. The captain ordered the shut down of the No.1 engine using the EESD. Whilst this drill was carried out crew members observed that the fire was spreading across the whole wing. Realising the severity of the situation the captain brought the aircraft to a halt near the northern end of the landing zone some 6,400 feet from the touchdown point. He ordered the passengers and crew to immediately carry out the Emergency Evacuation Drill. Once all personnel had evacuated the aircraft, fire rapidly destroyed the aircraft and cargo.
Probable cause:
The Board concluded that XV206 was destroyed after detonating an explosive device that was buried in the surface of the LKG TLZ. After extensive investigation the Board concluded that the device was an anti-tank landmine. This resulted in aircraft debris puncturing the port wing fuel tanks, causing a major leak of fuel that ignited, leading to an uncontrollable fire originating in the port wing in the vicinity of the n°1 engine.
The Board concluded that the following contributed to the loss of XV206:
a. The lack of permanent force protection at LKG TLZ allowed uncontrolled access to persons wishing to carry out a hostile act;
b. The TLZ clearance procedures proved to be inadequate for detecting subsurface mines.

Crash of an Antonov AN-32B in Lashkar Gah: 5 killed

Date & Time: Apr 24, 2006 at 1145 LT
Type of aircraft:
Registration:
ZS-PDV
Flight Type:
Survivors:
Yes
Schedule:
Kandahar – Lashkar Gah
MSN:
30 03
YOM:
1992
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
12
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The aircraft was dispatched in Afghanistan on behalf of the US Department of State, carrying members of the Bureau of International Narcotics and Law Enforcement Affairs. Following an uneventful flight from Kandahar, the crew landed at Lashkar Gah Airport. After touchdown, a truck crossed the active runway so the pilot-in-command initiated a turn to avoid the collision. Doing so, the aircraft veered off runway and collided with nearby houses. Both pilots as well as three people on the ground were killed. All other occupants were injured, some seriously.