Crash of a Mitsubishi MU-2B-35 Marquise in Smyrna

Date & Time: Sep 21, 1995 at 0425 LT
Type of aircraft:
Registration:
N309MA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Smyrna - Louisville
MSN:
602
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2140
Captain / Total hours on type:
112.00
Aircraft flight hours:
4304
Circumstances:
A witness stated he observed the airplane on climbout from runway 32. The airplane started a right turn estimated at about 30 to 45° angle of bank. The airplane stopped climbing and began descending. Subsequently, it collided with a tree line, while in a right bank, and then it impacted the ground. Weather conditions at the time of accident were described by the witness as very dark, with no ambient light or visible horizon. Examination of the airframe, flight control system, engine assembly, and propeller assembly revealed no evidence of a precrash failure or malfunction. The autopilot was found in the off position, and the autopilot circuit breakers were not tripped. The pilot and passenger were seriously injured and had no memory of the flight. A radio transcript revealed that after taking off, the flight had made one radio transmission to request an ifr clearance.
Probable cause:
Failure of the pilot to maintain a proper climb rate after takeoff, and his inadvertent entry in a descending spiral, which he failed to correct. Factors relating to the accident were: darkness, and the pilot becoming spatially disoriented during the initial climb while attempting to obtain an ifr clearance.
Final Report:

Crash of a Beechcraft B60 Duke near Gatlinburg: 1 killed

Date & Time: Feb 11, 1995 at 1327 LT
Type of aircraft:
Registration:
N6749S
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Knoxville - Knoxville
MSN:
P-519
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1500
Aircraft flight hours:
2488
Circumstances:
The pilot departed Knoxville on a local pleasure flight to the Gatlinburg area. A few minutes into the flight, the pilot requested the ILS approach to Knoxville. About two minutes after the initial request, he requested immediate radar vectors. The controller requested the flight's altitude, but there was no reply from the pilot. The aircraft collided with trees at the 3,500 foot level of rising terrain seven miles southwest of gatlinburg. A hiker reported hearing, the sound of the engines running until the airplane collided with trees. The hiker also stated that clouds obscured the tops of the mountains. Examination of the accident site disclosed that wreckage debris was scattered over an area 650 feet long and 75 feet wide. The wreckage examination failed to disclose a mechanical problem. Sole on board, the pilot was killed.
Probable cause:
The pilot's continued visual flight into instrument weather conditions that resulted in a collision with rising terrain.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Elizabethton: 2 killed

Date & Time: Apr 7, 1994 at 0810 LT
Operator:
Registration:
N64LB
Flight Type:
Survivors:
No
Schedule:
Augusta - Elizabethton
MSN:
31-7852127
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
7800
Aircraft flight hours:
2910
Circumstances:
The ATP and his passenger were en route to pick up a patient for transport to a VA hospital. The destination airport was uncontrolled, and VFR only. The pilot cancelled with ATC and reported the field in sight. The airport was reporting VFR conditions, but rising, mountainous terrain existed to the northeast, and local authorities reported that the top third of the mountain was obscured in clouds during the morning of the accident. After cancelling IFR, no subsequent radio calls were received from the flight, and the flight did not arrive at its destination. The wreckage was found several hours later near the crest of holston mountain, 1/2 mile east of the Holston mountain VOR. An examination of the wreckage indicated the aircraft impacted upsloping, wooded terrain, while at a climb angle of 8°. Disintegration of the wreckage was indicative of a high speed impact. No evidence of mechanical malfunction or failure was found during the examination of the wreckage. Both occupants were killed.
Probable cause:
The pilot's attempted VFR flight into imc conditions, and his failure to maintain a proper altitude over mountainous terrain. Factors were the clouds and obscuration at the accident site.
Final Report:

Crash of a Swearingen SA227TT Merlin IIIC in Bristol: 4 killed

Date & Time: Apr 1, 1993 at 2128 LT
Operator:
Registration:
N500AK
Survivors:
No
Schedule:
Knoxville - Bristol
MSN:
TT-527
YOM:
1983
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
19105
Captain / Total hours on type:
235.00
Aircraft flight hours:
2294
Circumstances:
N500AK encountered icing in flight before start of ILS approach. Radar data showed that before reaching outer marker, it slowed in a manner that was consistent with a power reduction (or partial loss of power), then it entered a steep descent and crashed. Examination revealed engines were not operating at impact and that propellers had been feathered. No preimpact part failure or malfunction of engines, propellers or anti-ice system was found. There was evidence that engine inlet anti-ice annunciator lights and stability augmentation system (SAS) fault warning light were illuminated during impact. The engine manufacturer reported that flameouts had occurred in other aircraft, during or following operation in icing conditions, sometimes after descent into warmer air. Flight manual noted that if icing was encountered with anti-ice system off, select continuous ignition and then select engine and propeller heat (1 engine at a time, ensuring first engine was operating satisfactorily before selecting second engine) and engage sas heat. All four occupants were killed.
Probable cause:
Failure of the pilot to follow procedures concerning use of the engine inlet anti-ice system and/or continuous ignition while operating in icing conditions, which resulted in probable ice ingestion and loss of engine power; and the pilot's failure to maintain sufficient airspeed while coping with the engine problem, which resulted in a stall. Factors related to the accident were: darkness, icing conditions, and engine inlet (nacelle) ice.
Final Report:

Crash of a Cessna 402B in Tullahoma: 1 killed

Date & Time: Mar 23, 1993 at 0328 LT
Type of aircraft:
Registration:
N405PC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tullahoma - Harrisburg
MSN:
402B-1381
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4302
Aircraft flight hours:
7693
Circumstances:
A witness reported that the airplane used the entire runway to get airborne, reached about 300 feet agl after liftoff, and drifted right. It then impacted trees about 1/3 mile from the departure end of the runway. Damage to the trees indicated that the airplane was in a right bank at impact. Both propellers showed evidence of rotation at impact. Estimated weight calculations showed that the airplane was at least 165 lbs in excess of max gross weight; this does not include an unknown amount of fuel on board prior to the last refueling. The pilot, sole on board, was killed.
Probable cause:
The pilot's failure to maintain control of the airplane during takeoff. Factors which contributed to the accident were: the pilot's failure to ensure that the airplane maximum gross takeoff weight was not exceeded, the dark night, and rain.
Final Report:

Crash of a BAe 3101 Jetstream 31 in Knoxville: 2 killed

Date & Time: Mar 12, 1992 at 0013 LT
Type of aircraft:
Operator:
Registration:
N165PC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Knoxville - Knoxville
MSN:
683
YOM:
1985
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4929
Captain / Total hours on type:
4400.00
Aircraft flight hours:
10607
Circumstances:
After a series of instrument procedures, the flight returned to Knoxville and landed. On the next takeoff, the first officer dropped the airplane's checklist and the check airman elected to continue the flight without using the checklist. On the next visual approach, the check airman and first officer attempted a landing without lowering the landing gear. The airplane touched down and both propeller assemblies struck the concrete runway surface. The pilot reported the gearup touchdown to the control tower and elected to go around. During the climbout the check airman lowered the landing gear, established a teardrop pattern for the opposite runway and feathered the right propeller. Crash fire rescue (cfr) equipment was alerted and was in position for the second landing attempt. While on short final, the check airman called for max power, a reduction in the flap setting, and initiated a single engine go-around below 200 feet. There is no operational procedure for a single engine go-around below 200 feet. The airplane climbed briefly and crashed inverted about 7,500 feet from the approach end of the runway. Both pilots were killed.
Probable cause:
The pilot's failure to use the airplane checklist which resulted in a gear up landing; and the pilot's failure to maintain flying speed which resulted in an uncontrolled collision with the ground.
Final Report:

Crash of a Cessna 401 in Jackson

Date & Time: Sep 11, 1991 at 1902 LT
Type of aircraft:
Registration:
N13DT
Flight Type:
Survivors:
Yes
Schedule:
Raleigh - Jackson
MSN:
401-0247
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1681
Captain / Total hours on type:
659.00
Circumstances:
The pilot had cancelled his ifr flight plan, and was proceeding to the airport visually. During his approach, the left engine quit, followed by the right engine. He then realized that he had failed to switch from the auxiliary fuel tanks to the main fuel tanks prior to the approach, and exhausted the auxiliary fuel supply. With insufficient altitude to attempt a restart, he force landed the airplane in a bean field short of the airport. After the airplane came to a stop, the occupants egressed, and the fuselage was consumed in a post-crash fire.
Probable cause:
The pilot's failure to select the main fuel tanks prior to the approach, resulting in fuel starvation and engine stoppage.
Final Report:

Crash of a Learjet 23 in Columbia

Date & Time: Jul 2, 1991 at 1856 LT
Type of aircraft:
Operator:
Registration:
N500FM
Flight Type:
Survivors:
Yes
Schedule:
Youngstown - Columbia
MSN:
23-088
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4964
Captain / Total hours on type:
4039.00
Aircraft flight hours:
13594
Circumstances:
The pilot had computed landing performance information for a landing on a wet runway with anti-skid; sufficient runway surface was available. Touchdown was normal, however during the braking process, the airplane started to fishtail and the pilot believed that the anti-skid system had failed. Therefore, the pilot turned the antiskid system off and continued the rollout with normal braking. The airplane went off the departure end of runway 05 and sustained substantial damage. Performance data indicated more runway surface was required for a safe landing on a wet runway without anti-skid assistance. The braking sequence of events described by the pilot resembled dynamic hydroplaning where there was a complete loss of braking effectiveness rather than an anti-skid malfunction. An examination of the airplane failed to disclose any mechanical problems.
Probable cause:
The pilot's premature decision to turn off the anti-skid during landing roll. Factors to this accident were hydroplaning conditions.

Crash of a Mitsubishi MU-2B-36 Marquise in Nashville: 1 killed

Date & Time: Sep 6, 1990 at 1131 LT
Type of aircraft:
Operator:
Registration:
N82MA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Nashville - Murfreesboro
MSN:
665
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
9379
Captain / Total hours on type:
5854.00
Aircraft flight hours:
6714
Circumstances:
On a previous flight, low power was noted in the right engine, the right engine fuel flow was 5 to 8 gal/hr less than the left engine and the right engine temperature (itt) was about 500° less than the left. A decision was made to ferry the aircraft to a maint facility to have the right engine examined. The pilot took off on a 5,186 feet runway (unrway 02C) with a light tail wind in 95° temperature, though the airport had longer runways (7,702 feet, 8,000 feet and 8,500 feet). A witness noted the aircraft lifted off at the end of the runway (charts showed the takeoff roll with normal power should have been about 3,100 feet). Witnesses reported the aircraft remained low (nearly hitting a 55 feet light standard) until it rolled right and 'dropped like a rock.' Impact occurred in a right wing low attitude about 2 miles from the departure end of runway 02C. The aircraft was extensively damaged by impact and fire; no preimpact part failure was found. Both engines had evidence of engine rotation at the time of impact. The operator's lead mechanic had reported for duty about 3 hours before the accident flight, but he had not been informed of the engine problem before the aircraft took off. The pilot, sole on board, was killed.
Probable cause:
The company/operator management's decision to operate the aircraft with a known deficiency without further maintenance, the pilot's improper planning/decision and the pilot's failure to abort the takeoff (while there was sufficient runway remaining). Factors related to the accident were: lack of power in the right engine, and the unfavorable meteorological conditions at the airport.
Final Report:

Crash of an Embraer EMB-110P1 Bandeirante in Columbia: 1 killed

Date & Time: May 6, 1989 at 0144 LT
Operator:
Registration:
N95PB
Flight Type:
Survivors:
Yes
Schedule:
Memphis - Columbia
MSN:
110-330
YOM:
1981
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
11020
Captain / Total hours on type:
250.00
Aircraft flight hours:
11387
Circumstances:
After conducting ground training all day, the instructor/director of operations and his trainee flew an EMB-110P1 to Memphis to exchange airplanes. Ground fog had started to form prior to departure. After exchanging airplanes, they made the return flight to Columbia. They obtained radar vectors to the final approach course for the SDF at Columbia. The thick fog resulted in a missed approach. During the missed approach, the runway was visible from above and the crew indicated that they would try for a VFR approach and landing. The airplane collided with trees 2,350 feet from the runway in a wings level attitude. The tops of the trees were broken 41 feet above the runway threshold altitude. The trainee had been without rest for at least 30 hours prior to the accident. One pilot was killed while the second was seriously injured.
Probable cause:
Pilot attempted to make a VFR landing in instrument conditions that were below minimums for the published instrument approach and collided with trees and the ground after allowing the airplane to descend below the proper altitude.
Final Report: