Crash of a Cessna 550 Citation II in Greenwood

Date & Time: Nov 17, 2012 at 1145 LT
Type of aircraft:
Operator:
Registration:
N6763L
Flight Type:
Survivors:
Yes
Schedule:
Greenwood - Greenwood
MSN:
550-0673
YOM:
1991
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11592
Captain / Total hours on type:
903.00
Copilot / Total flying hours:
4501
Copilot / Total hours on type:
13
Aircraft flight hours:
8611
Circumstances:
The aircraft, registered to the United States Customs Service, and operated by Stevens Aviation, Inc., was substantially damaged during collision with a deer after landing on Runway 9 at Greenwood County Airport (GRD), Greenwood, South Carolina. The airplane was subsequently consumed by postcrash fire. The two certificated airline transport pilots were not injured. Visual meteorological conditions prevailed, and no flight plan was filed for the maintenance test flight, which was conducted under the provisions of Title 14 Code of Federal Regulations Part 91. According to the pilot, the purpose of the flight was to conduct a test of the autopilot and flight director systems on board the airplane, following a "cockpit modernization" their company had performed. The airplane completed the NDB/GPS RWY 27 instrument approach procedure and then circled to land on Runway 9. About 5 seconds into the landing rollout, a deer appeared from the wood line and ran into the path of the airplane. The deer struck the airplane at the leading edge of the left wing above the left main landing gear, and ruptured an adjacent fuel cell. The pilot was able to maintain directional control, and the airplane was stopped on the runway, spilling fuel and on fire. The crew performed an emergency shutdown of the airplane and egressed without injury.Greenwood County Airport did not have a fire station co-located on the airport facility. The fixed base operator called 911 at the time of the accident, and the fire trucks arrived approximately 10 minutes after notification.
Probable cause:
Collision with a deer during the landing roll, which resulted in a compromised fuel tank and a postimpact fire. In a telephone interview, the manager of the Greenwood County Airport explained that Greenwood was not an FAR Part 139 Airport, and while there was no published Wildlife Management Program for the airport, she had been very proactive about eradicating wildlife that could pose a hazard to safety on the airport property, primarily deer and wild turkey. She contacted the United States Department of Agriculture (USDA) for guidance and advice and she attended a wildlife management course. Among the suggestions offered by the USDA, was to remove the deer habitat. The manager proposed adding the area between the runway and taxiway to an approach clearing project in order to reduce the habitat. The manager worked with a local charity and local hunters with depredation permits to take deer on the airport property, and their efforts averaged 50 deer a year. The hunts were conducted in stands away from runways and on property not aviation related. The nearest deer stand was 1 mile from the runway, and the hunters fired only shotguns. The hunts were conducted between the hours of 0700 and 1000. On the morning of the accident, the last shot was fired at 0930.When asked why the hunters were still on the property at the time of the accident, the manager said they had stayed to eat lunch, and repeated that the hunt was long over and that the last shot was fired hours before the accident. She offered that the deer struck by the airplane was probably flushed from the woods by another deer or a coyote, whose population has also grown in recent years.After the accident, the Federal Aviation Administration contacted the state and had the Greenwood County Airport added to a list of airports where funding for improvements had been allotted. A second 10-foot perimeter fence was added around the existing 6-foot fence, and since its construction only 4 deer have been taken inside the perimeter, and no wild turkeys have been sighted
Final Report:

Crash of a Piper PA-31P-425 Navajo in Dalton: 1 killed

Date & Time: Jun 30, 2012 at 1620 LT
Type of aircraft:
Registration:
N33CG
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Dalton - Dalton
MSN:
31-7300157
YOM:
1973
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1685
Circumstances:
According to a friend of the pilot, the pilot was taking the airplane to have an annual inspection completed. The friend assisted the pilot before departure and watched as the airplane departed. He did not notice any anomalies with the airplane during the takeoff or the climbout. According to a witness in the vicinity of the accident site, he heard the airplane coming toward him, and it was flying very low. He looked up and saw the airplane approximately 200 feet over his house and descending toward the trees. As he watched the airplane, he noticed that the right propeller was not turning, and the right engine was not running. He stated that the left engine sounded as if it was running at full power. The airplane pitched up to avoid a power line and rolled to the right, descending below the tree line. A plume of smoke and an explosion followed. Examination of the right propeller assembly revealed evidence of significant frontal impact. The blades were bent but did not have indications of rotational scoring; thus they likely were not rotating at impact. One preload plate impact mark indicated that the blades were at an approximate 23-degree angle; blades that are feathered are about 86 degrees. Due to fire and impact damage of the right engine and related system components, the reason for the loss of power could not be determined. An examination of the airframe and left engine revealed no mechanical malfunctions or failures that would have precluded normal operation. A review of the airplane maintenance logbooks revealed that the annual inspection was 12 days overdue. According to Lycoming Service Instruction No. 1009AS, the recommended time between engine overhaul is 1,200 hours or 12 years, whichever occurs first. A review of the right engine maintenance logbook revealed that the engine had accumulated 1,435 hours since major overhaul and that neither engine had been overhauled within the preceding 12 years. Although the propeller manufacturer recommends that the propeller be feathered before the engine rpm drops below 1,000 rpm, a review of the latest revision of the pilot operating handbook (POH) revealed that the feathering procedure for engine failure did not specify this. It is likely that the pilot did not feather the right propeller before the engine reached the critical 1,000 rpm, which prevented the propeller from engaging in the feathered position
Probable cause:
The pilot’s failure to maintain airplane control following loss of power in the right engine for reasons that could not be determined because of fire and impact damage. Contributing to the accident was the pilot’s delayed feathering of the right propeller following the loss of engine power and the lack of specific emergency procedures in the pilot operating handbook indicating the need to feather the propellers before engine rpm falls below 1,000 rpm.
Final Report:

Crash of a Piper PA-31-325 Navajo C/R near Two Harbors: 1 killed

Date & Time: Jun 8, 2012 at 1427 LT
Type of aircraft:
Registration:
N174BH
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
South Saint Paul - South Saint Paul
MSN:
31-7612038
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
On June 8, 2012, about 1307 central daylight time, a Piper PA-31-325, N174BH, departed from the South St Paul Municipal Airport-Richard E Fleming Field (SGS), South St Paul, Minnesota for a maintenance test flight. The airplane reportedly had one of its two engines replaced and the pilot was to fly for about 4 hours to break-in the engine. The airplane did not return from the flight and was reported overdue. The airplane is missing and is presumed to have crashed. The airline transport pilot has not been located. The airplane was registered to Family Celebrations LLC, and was operated as a 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions prevailed and no flight plan was filed. The flight departed SGS with the intention of returning to SGS at the conclusion of the flight. The airplane was reported missing and an alert notification issued about 2225. The last reported contact with the airplane and pilot was about 1300 when the fixed base operator at SGS towed the airplane to the fuel pumps. When he returned about 15 minutes later, the airplane was no longer there. Aircraft radar track data from various ground based sources indicated that the airplane departed SGS about 1307. The airplane maneuvered east of SGS before turning toward the north. The airplane's track continued north toward Duluth, Minnesota. Once the airplane reached Duluth, it followed the west shoreline of Lake Superior. Radar track data indicated that the airplane was at a pressure altitude of 2,800 feet when it reached the shoreline. The airplane continued along the west shoreline toward Two Harbors, Minnesota, flying over the water while maintaining a distance of about 0.5 miles from the shore. As the airplane approached Two Harbors, it descended. The airplane's last recorded position at 1427 was about 30 miles northeast of Duluth, Minnesota, at an uncorrected pressure altitude of 1,600 feet. The Air Force Rescue Coordination Center coordinated a search for the missing airplane. The Civil Air Patrol, United States Coast Guard, and other entities participated in the search efforts. Search efforts were suspended on July 4, 2012.
Probable cause:
Undetermined because the airplane was not found
Final Report:

Crash of a Boeing 727-212 in Laguna Salada

Date & Time: Apr 27, 2012 at 1000 LT
Type of aircraft:
Operator:
Registration:
XB-MNP
Flight Type:
Survivors:
Yes
Site:
MSN:
21348/1287
YOM:
1977
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft departed Mexicali Airport with one pilot on board. The goal of the flight was a test experiment on behalf of the Mexican Civil Aviation Authority and various agencies to crash deliberately the aircraft in the Laguna Salada for a television program organized by British, German, Mexican and American Producers. While approaching the desert along the Mexican 5 Highway, about 30 km southwest of Mexicali, the pilot bailed out and the aircraft continued for few seconds in a slightly flat attitude. In a flaps down and gear down configuration, the aircraft touched down hard in a sandy area, lost its undercarriage, crashed and came to rest, broken in two.

Crash of a Socata TBM-700 in Hollywood

Date & Time: Oct 12, 2011 at 1334 LT
Type of aircraft:
Operator:
Registration:
N37SV
Flight Type:
Survivors:
Yes
Site:
Schedule:
North Perry - North Perry
MSN:
441
YOM:
2008
Flight number:
SC332
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11071
Captain / Total hours on type:
4053.00
Copilot / Total flying hours:
2500
Copilot / Total hours on type:
5
Aircraft flight hours:
593
Circumstances:
The airplane, registered to SV Leasing Company of Florida, operated by SOCATA North America, Inc., sustained substantial damage during a forced landing on a highway near Hollywood, Florida, following total loss of engine power. Visual meteorological conditions prevailed at the time and an instrument flight rules (IFR) flight plan was filed for the 14 Code of Federal Regulations (CFR) Part 91 maintenance test flight from North Perry Airport (HWO), Hollywood, Florida. The airline transport pilot and pilot-rated other crew member sustained minor injuries; there were no ground injuries. The flight originated from HWO about 1216. The purpose of the flight was a maintenance test flight following a 600 hour and annual inspection. According to the right front seat occupant, in anticipation of the flight, he checked the fuel load by applying electrical power and noted the G1000 indicated the left fuel tank had approximately 36 gallons while the right fuel tank had approximately 108 gallons. In an effort to balance the fuel load with the indication of the right fuel tank, he added 72.4 gallons of fuel to the left fuel tank. At the start of the data recorded by the G1000 for the accident flight, the recorded capacity in the left fuel tank was approximately 105 gallons while the amount in the right fuel tank was approximately 108 gallons. The PIC reported that because of the fuel load on-board, he could not see the level of fuel in the tanks; therefore, he did not visually check the fuel tanks. By cockpit indication, the left tank had approximately 105 gallons and the right tank had approximately 108 gallons. The flight departed HWO, but he could not recall the fuel selector position beneath the thrust lever quadrant. He further stated that the fuel selector switch on the overhead panel was in the "auto" position. After takeoff, the flight climbed to flight level (FL) 280, and levelled off at that altitude about 20 minutes after takeoff. While at that altitude they received a "Fuel Low R" amber warning CAS message on the G1000. He checked the right fuel gauge which indicated 98 gallons, and confirmed that the fuel selector automatically switched to the left tank. After about 10 seconds the amber warning CAS message went out. He attributed the annunciation to be associated with a failure or malfunction of the sensor, and told the mechanic to write this issue down so it could be replaced after the flight. The flight continued and they received an amber warning CAS message, "Fuel Unbalance" which the right fuel tank had more fuel so he switched the fuel selector to supply fuel from the right tank to the engine. The G1000 indicates they remained at that altitude for approximately 8 minutes. He then initiated a quick descent to 10,000 feet mean sea level (msl) and during the descent accelerated to Vmo to test the aural warning horn. They descended to and maintained 10,000 feet msl for about 15 minutes and at an unknown time, they received an amber warning CAS message "Fuel Low R." Once again he checked the right fuel gauge which indicated it had 92 gallons and confirmed that the fuel tank selector automatically switched to the left tank. After about 10 seconds the CAS message went out. Either just before or during descent to 4,000 feet, they received an amber CAS message "Fuel Unbalance." Because the right fuel gauge indicated the fullest tank was the right tank, he switched the fuel selector to supply fuel to the engine from the right tank. The flight proceeded to the Opa-Locka Executive Airport, where he executed an ILS approach which terminated with a low approach. The pilot cancelled the IFR clearance and proceeded VFR towards HWO. While in contact with the HWO air traffic control tower, the flight was cleared to join the left downwind for runway 27L. Upon entering the downwind leg they received another amber CAS message "Fuel Unbalance" and at this time the left fuel gauge indicated 55 gallons while the right fuel gauge indicated 74 gallons. Because he intended on landing within a few minutes, he put the fuel selector to the manual position and switched to the fullest (right) tank. Established on final approach to runway 27L at HWO with the gear down, flaps set to landing, and minimum speed requested by air traffic for separation (85 knots indicated airspeed). When the flight was at 800 feet, the red warning CAS message "Fuel Press" illuminated and the right seat occupant with his permission moved the auxiliary fuel boost pump switch from "Auto" to "On" while he, PIC manually moved the fuel selector to the left tank. In an effort to restore engine power he pushed the power lever and used the manual over-ride but with no change. Assured that the engine had quit, he put the condition lever to cutoff, the starter switch on, and then the condition lever to "Hi-Idle" attempting to perform an airstart. At 1332:42, a flight crew member of the airplane advised the HWO ATCT, "…just lost the engine"; however, the controller did not reply. The PIC stated that he looked to his left and noticed a clear area on part of the turnpike, so he banked left, and in anticipation of the forced landing, placed the power lever to idle, the condition lever to cutoff, the fuel tank selector to off, and put the electrical gang bar down to secure the airplane's electrical system. He elected to retract the landing gear in an effort to shorten the landing distance. The right front seat occupant reported that the airplane was landed in a southerly direction in the northbound lanes of the Florida Turnpike. There were no ground injuries.
Probable cause:
The pilot’s failure to terminate the flight after observing multiple conflicting errors associated with the inaccurate right fuel quantity indication. Contributing to the accident were the total loss of engine power due to fuel starvation from the right tank, the inadequate manufacturing of the right fuel gauge electrical harness, and failure of maintenance personnel to recognize and evaluate the reason for the changing fuel level in the right fuel tank.
Final Report:

Ground accident of a Dassault Falcon 20F in Newnan

Date & Time: Oct 3, 2011
Type of aircraft:
Registration:
XA-NCC
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
264
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
A technician was in charge to ferry the airplane to a hangar for a maintenance control. While taxiing, the Falcon went out of control, rolled down an embankment and collided with a utility pole. The nose was severely damaged and the aircraft was damaged beyond repair. According to the technician, who escaped uninjured, the brakes failed while taxiing.
Probable cause:
No investigation was conducted by the NTSB.

Crash of a Piper PA-31P-425 Pressurized Navajo in Monterrey: 2 killed

Date & Time: Sep 12, 2011 at 1345 LT
Type of aircraft:
Operator:
Registration:
N69DJ
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Monterrey - Monterrey
MSN:
31-7300155
YOM:
1973
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The twin engine aircraft was engaged in a local post maintenance test flight at Monterrey-Del Norte Airport. Shortly after takeoff, the airplane encountered difficulties to gain height when it stalled and crashed in a field located 500 metres past the runway end, bursting into flames. The aircraft was destroyed by fire and both occupants were killed.

Crash of a Beechcraft C90 King Air in Kaduna: 2 killed

Date & Time: May 24, 2011 at 1154 LT
Type of aircraft:
Operator:
Registration:
N364UZ
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Old Kaduna - Old Kaduna
MSN:
LJ-805
YOM:
1979
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Aircraft flight hours:
9665
Circumstances:
On 24th May, 2011 at 11:54 h, a Beechcraft C90 aircraft with nationality and registration marks N364UZ, operated by Shoreline Energy International Limited (SEIL), departed Old Kaduna (Military) airport on a test flight with a pilot and another person onboard with three hours fuel endurance. The test flight was on a visual flight rules (VFR) flight plan. According to an eye witness, the aircraft sound was unusual and the aircraft seemed not to be gaining altitude after takeoff. Another eye witness (a local farmer), stated that he saw the aircraft moving up and down with increasing and decreasing engine sound. Thereafter, the aircraft impacted a mango tree, turned and crashed. The local farmer further stated that he and some military personnel tried all they could to rescue the occupants inside the aircraft but their efforts were not successful. At 11:59 h, the aircraft crashed on a farm-land 878 meters short of RWY 23 (military) and engulfed into flames. The two occupants were fatally injured. Dornier Aviation Nigeria AIEP (DANA) and Nigerian Air Force (NAF) fire-fighting personnel were dispatched immediately. There was no direct access between the runway and the accident site, which delayed the fire trucks from reaching the aircraft at accident site on time. The accident occurred in day light, in visual meteorological conditions (VMC).
Probable cause:
Causal Factor:
Inability of the pilot to control the aircraft to landing due to inadequate power to enable the pilot maintain the appropriate approach profile (height, speed and glide path) to cover the required distance to threshold.
Contributory factors:
1. Non-adherence to approved storage procedure.
2. Non-adherence to approved return from storage procedure.
3. Inadequate regulatory oversight by the authority on flight operation and maintenance of foreign registered aircraft in Nigeria.
Final Report:

Crash of a Gulfstream G650 in Roswell: 4 killed

Date & Time: Apr 2, 2011 at 0934 LT
Type of aircraft:
Operator:
Registration:
N652GD
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Roswell - Roswell
MSN:
6002
YOM:
2010
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
11237
Captain / Total hours on type:
263.00
Aircraft flight hours:
434
Circumstances:
On April 2, 2011, about 0934 mountain daylight time, an experimental Gulfstream Aerospace Corporation GVI (G650), N652GD, crashed during takeoff from runway 21 at Roswell International Air Center, Roswell, New Mexico. The two pilots and the two flight test engineers were fatally injured, and the airplane was substantially damaged by impact forces and a post crash fire. The airplane was registered to and operated by Gulfstream as part of its G650 flight test program. The flight was conducted under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed at the time of the accident. The accident occurred during a planned one-engine-inoperative (OEI) takeoff when a stall on the right outboard wing produced a rolling moment that the flight crew was not able to control, which led to the right wingtip contacting the runway and the airplane departing the runway from the right side. After departing the runway, the airplane impacted a concrete structure and an airport weather station, resulting in extensive structural damage and a post crash fire that completely consumed the fuselage and cabin interior.
Probable cause:
An aerodynamic stall and subsequent uncommanded roll during a one engine-inoperative takeoff flight test, which were the result of (1) Gulfstream’s failure to properly develop and validate takeoff speeds for the flight tests and recognize and correct the takeoff safety speed (V2) error during previous G650 flight tests, (2) the G650 flight test team’s persistent and increasingly aggressive attempts to achieve V2 speeds that were erroneously low, and (3) Gulfstream’s inadequate investigation of previous G650 uncommanded roll events, which indicated that the company’s estimated stall angle of attack while the airplane was in ground effect was too high. Contributing to the accident was Gulfstream’s failure to effectively manage the G650 flight test program by pursuing an aggressive program schedule without ensuring that the roles and responsibilities of team members had been appropriately defined and implemented, engineering processes had received sufficient technical planning and oversight, potential hazards had been fully identified, and appropriate risk controls had been implemented and were functioning as intended.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 100 in Clayton: 2 killed

Date & Time: Mar 8, 2011 at 1140 LT
Operator:
Registration:
N157KM
Flight Type:
Survivors:
No
Schedule:
Clayton - Clayton
MSN:
57
YOM:
1967
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1255
Captain / Total hours on type:
492.00
Aircraft flight hours:
16541
Aircraft flight cycles:
20927
Circumstances:
The airplane had not been flown for about 5 months and the purpose of the accident flight was a maintenance test flight after both engines had been replaced with higher horsepower models. Witnesses observed the airplane depart and complete two uneventful touch-and-go landings. The airplane was then observed to be struggling to gain altitude and airspeed while maneuvering in the traffic pattern. One witness, who was an aircraft mechanic, reported that he observed the airplane yawing to the left and heard noises associated with propeller pitch changes, which he believed were consistent with the "Beta" range. The airplane stalled and impacted trees in a wooded marsh area, about 1 mile from the airport. It came to rest about 80-degrees vertically. Examination of the wreckage did not reveal any preimpact malfunctions; however, the lack of flight recorders and the condition of the wreckage precluded the gathering of additional relevant information. Damage observed to both engines and both propellers revealed they were likely operating at symmetrical power settings and blade angles at the time of the impact, with any differences in scoring signatures likely the result of impact damage. The reason for the yawing and the noise associated with propeller pitch changes that were reported prior to the stall could not be determined.
Probable cause:
The pilot did not maintain airspeed while maneuvering, which resulted in an aerodynamic stall.
Final Report: